1 preparation for the 3 he injection test 05/2008 duke d. dutta*, h. gao, m. busch, q. ye, x. qian,...
TRANSCRIPT
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Preparation for the 3He Injection Test
05/2008 Duke
D. Dutta*, H. Gao, M. Busch, Q. Ye, X. Qian, W.
Zheng, X. Zhu (Duke University)
ASU, BU, Caltech, LANL, MIT, MSU, NCSU, SFU
And others in nEDM collaboration
*Mississippi State University.
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Outline
• Introduction• Safety • Magnets• Glassware• Cryogenics • pNMR• Summary
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Dilutionrefrigerator
tricoil
Helium bath vesselHelium gasFilling pipe
To ABS 50K
4k
Film burner
Helium @0.35k
Pyrex cell
Heat exchanger
1.3k
0.7k
0.24k
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Update• Problem with jacket pyrex cell
– Seal <1K and safety when boil off
• Cool the cell with OFHC copper foil
Measurement cell @.35K
Copper foil to cool the cell
DR MX at 0.24K
To ABS
DR 1K pot
Cs ring
Filling pipe for L-He
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Safety I: Boil off of LHe within pyrex cell
• 23.58 cc LHe within pyrex cell• boil off rate: ~1 mol/s
– Heat rate: 60000 W/m2, in worst case• Effuse through ABS beamline, pressure
difference ~25.2 Pa– Gas density at 273 K and 1 atm – Id: 0.04 m, L=1.0 m– Flow velocity: 17.8 m/s– Reynold constant: Re = 6842.4– Resistance coefficient, K=0.9
– From T. Ito and Applied Fluid Dynamics Handbook
– Effect of thermal baffles not included
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Protection for ABS vacuum system
Vacuum
Gauge and
pump
ABS low Beam lin
e
Gate
valve
ABS
Non-magnetic
Pneumatic
valve
Rupture disk/
Pressure re
lief
If P>10-5 torrActivate the Pneumatic valve
• A pneumatic valve to protect ABS beamline
• A rupture disc for pressure relief
5”
5”
2”
2”
Catastrophic Boil off
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Safety II: boil off of LHe within Tricoil can
• Siphon pipe to fill LHe into tricoil can
• Pipe for safety venting– Heat rate: 2 kW/m2
– Pressure drop: 5.5 psi• Gas
density@50K,1atm– By J. Long
• Venting velocity: 97m/s
• 1.375” ID, 45” length• Reynold number:
5.7x105
• resistant coefficient: 0.49
– Rupture disc@4K• Avoiding Taconis
resonance
Siphon pipe
Vacuumvent pipe
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Safety III: No problem with superconductor
quench • Energy within tri-coil:
714.15J– Energy within transport
solenoid coil: 6.3mJ, negligible
• Quench will evaporate 2.84 liter of He gas at 4K
– Amount to 8.67 mol He• The volume of tri-coil
container: ~17 liter – Bottom :14 lit, top: 3 lit.
• The pressure will increase by <50%
– Assume space of coil : 7 lit• Acceptible to tricoil vessel
• FEA analysis done by E. Iholff
Pressure<2atm
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Tricoil Magnet system
• Tricoil current lead– 300K to 50K: copper wire, #11 AWG– 50K to 4K: silver wire with
filaments of HTS ceramic (BiPbSrCaCuO)
• Low thermal conductivity– From American Superconductor
• Solder with eutectic InAg with no flux
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Cryogenics• Heat load to DR mix:~ 5mW
– ~2.5mW from superfluid film burner
– By G. Seidel
– 0.5mW for pNMR and support
– 1.1mW for gas introduction tube
– 13.8mW cooling power @0.24K
• Cs ring to slow down superfluid flow rate
– Torch to chase Cs vapor– Dry ice to condense Cs
effectively • Sealing test undergoing
– Pyrex to copper adapter– After fail and try, kapton
gasket seals well with copper flange
Kapton gasket
Epoxy2850GT
Cs ringMade by dry ice
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pNMR system
• Faraday cage– Two tunable capacitor – Resonant coil– Copper [email protected]
• Semi-rigid coax– Center: Ag coated BeCu– Dielectric: teflon– Sheath: BeCu
• From D. G. Crabb, UVA
• Weakly magnetized SS
• Tosca simulation by Tim, ASU
Faraday cage
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Wire connection for temperature sensors
• Thermometer leads: twisted pair , Phosphor bronze– Suggested by S. Williamson
• Noninductive winding scheme– Minimizing induced voltage due magnetic flux
change• Voltage wires and current wires thermal
anchor separately• Wire lengths for thermal anchoring (300K
to 4K)– 1.1cm for #32 AWG – 3.8cm for #24 AWG Heat
sinkpost
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Summary
Design work is almost done, ready for fabrication and assembling. Injection test will be ready in
the end of July
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Thanks!