1 vva-based combustion control strategies for efficiency · 2021. 5. 5. · 18 combustion control...

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VVA-based combustion control strategies for efficiency 1 improvement and emissions control in a heavy-duty diesel engine 2 3 Wei Guan 1 , Vinícius B. Pedrozo 1 , Hua Zhao 1 , 4 1 Brunel University London, UK; 5 Zhibo Ban 2 , Tiejian Lin 2 6 2 Guangxi Yuchai Machinery Company, China 7 8 Abstract 9 10 High nitrogen oxide (NOx) levels of the conventional diesel engine combustion often requires 11 the introduction of exhaust gas recirculation (EGR) at high engine loads. This can adversely 12 affect the smoke emissions and fuel conversion efficiency associated with a reduction of the 13 in-cylinder air-fuel ratio (lambda). In addition, low exhaust gas temperatures (EGT) at low 14 engine loads reduce the effectiveness of aftertreatment systems (ATS) necessary to meet 15 stringent emissions regulations. These are some of the main issues encountered by current 16 heady-duty (HD) diesel engines. In this work, variable valve actuation (VVA)-based advanced 17 combustion control strategies have been researched as means of improving upon the engine 18 exhaust temperature, emissions, and efficiency. Experimental analysis was carried out on a 19 single-cylinder HD diesel engine equipped with a high pressure common rail fuel injection 20 system, a high-pressure loop cooled EGR, and a VVA system. The VVA system enables a late 21 intake valve closing (LIVC) and a second intake valve opening (2IVO) during the exhaust 22 stroke. 23 The results showed that Miller cycle was an effective technology for exhaust temperature 24 management of low engine load operations, increasing the EGT by 40and 75when 25 running engine at 2.2 and 6 bar net indicated mean effective pressure (IMEP), respectively. 26 However, Miller cycle adversely effected carbon monoxide (CO) and unburned hydrocarbon 27 (HC) emissions at a light load of 2.2 bar IMEP. This could be overcome when combing Miller 28 cycle with a 2IVO strategy due to the formation of a relatively hotter in-cylinder charge induced 29

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Page 1: 1 VVA-based combustion control strategies for efficiency · 2021. 5. 5. · 18 combustion control strategies have been researched as means improving upon the of engine 19 exhaust

VVA-based combustion control strategies for efficiency 1

improvement and emissions control in a heavy-duty diesel engine 2

3

Wei Guan1, Vinícius B. Pedrozo1, Hua Zhao1, 4

1Brunel University London, UK; 5

Zhibo Ban2, Tiejian Lin2 6

2Guangxi Yuchai Machinery Company, China 7

8

Abstract 9 10

High nitrogen oxide (NOx) levels of the conventional diesel engine combustion often requires 11

the introduction of exhaust gas recirculation (EGR) at high engine loads. This can adversely 12

affect the smoke emissions and fuel conversion efficiency associated with a reduction of the 13

in-cylinder air-fuel ratio (lambda). In addition, low exhaust gas temperatures (EGT) at low 14

engine loads reduce the effectiveness of aftertreatment systems (ATS) necessary to meet 15

stringent emissions regulations. These are some of the main issues encountered by current 16

heady-duty (HD) diesel engines. In this work, variable valve actuation (VVA)-based advanced 17

combustion control strategies have been researched as means of improving upon the engine 18

exhaust temperature, emissions, and efficiency. Experimental analysis was carried out on a 19

single-cylinder HD diesel engine equipped with a high pressure common rail fuel injection 20

system, a high-pressure loop cooled EGR, and a VVA system. The VVA system enables a late 21

intake valve closing (LIVC) and a second intake valve opening (2IVO) during the exhaust 22

stroke. 23

The results showed that Miller cycle was an effective technology for exhaust temperature 24

management of low engine load operations, increasing the EGT by 40℃ and 75℃ when 25

running engine at 2.2 and 6 bar net indicated mean effective pressure (IMEP), respectively. 26

However, Miller cycle adversely effected carbon monoxide (CO) and unburned hydrocarbon 27

(HC) emissions at a light load of 2.2 bar IMEP. This could be overcome when combing Miller 28

cycle with a 2IVO strategy due to the formation of a relatively hotter in-cylinder charge induced 29

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by the presence of internal EGR (iEGR). This strategy also led to a significant reduction in soot 30

emissions by 82% when compared to the baseline engine operation. Alternatively, the use of 31

external EGR and post injection on a Miller cycle operation decreased NOx emissions by 67% 32

at a part load of 6 bar IMEP. This contributed to a reduction of 2.2% in the total fluid 33

consumption, which takes into account the urea consumption in ATS. At a high engine load of 34

17 bar IMEP, a highly boosted Miller cycle strategy with EGR increased the fuel conversion 35

efficiency by 1.5% while reducing the total fluid consumption by 5.4%. The overall results 36

demonstrated that advanced VVA-based combustion control strategies can control the EGT 37

and engine-out emissions at low engine loads as well as improve upon the fuel conversion 38

efficiency and total fluid consumption at high engine loads, potentially reducing the engine 39

operational costs. 40

Keywords 41

Heavy-duty diesel engine, VVA, Miller cycle, EGR, post injection, total fluid consumption, 42

exhaust gas temperature 43

44

45

46

47

48

49

50

51

52

53

54

55

56

57

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1. Introduction 58

Over the last two decades, the research and development of heavy-duty diesel engines have 59

been focused on the reduction of the NOx and particulate matter (PM) emissions. Their 60

formation is due to the fact that conventional diesel engine combustion is characterised by a 61

wide range of local in-cylinder gas temperatures and equivalence ratios as a result of the non-62

premixed diffusion-controlled combustion [1]. More recently, the demand for the reduction of 63

fuel consumption and carbon dioxide (CO2) coupled with the customer’s requirements to 64

reduce the vehicle operational cost also impose stringent requirements on the development of 65

HD diesel engines [2,3]. To address these issues, in-cylinder combustion control technologies 66

combined with emission control ATS is required [4,5]. 67

Low temperature combustion (LTC) modes, such as Homogeneous Charge Compression 68

Ignition (HCCI), Premixed Charge Compression Ignition (PCCI), and Partially Premixed 69

Charge Compression Ignition (PPCI), have shown their potential to achieve simultaneous low 70

NOx and soot emissions. However, these combustion modes suffer from high unburned HC 71

and CO emissions, lack of combustion phasing control and limited load range [6–8]. Moreover, 72

these LTC strategies result in significantly lower exhaust gas temperature, which creates great 73

challenges for the effective operation of the ATS including selective catalytic reduction (SCR), 74

diesel particulate filter (DPF), and diesel oxidation catalyst (DOC) at the low engine loads and 75

cold-start [9]. These ATS are strongly dependent on the exhaust gas temperature (EGT) and a 76

minimum EGT of approximately 200°C is required for catalyst light-off and to initiate the 77

emissions control [10]. When the EGT is above 300°C, the unburned HC and CO emissions 78

can be effectively removed from the exhaust gases in the DOC [11]. Additionally, the active 79

regeneration of the DPF can be realised when the inlet gas temperature reaches 500°C [12]. 80

Advanced combustion technologies such as multiple fuel injection strategy, higher fuel 81

injection pressure, and higher boost pressure have been employed to improve upon fuel 82

conversion efficiency, however, these technologies are typically accompanied with a lower 83

EGT [13]. 84

Alternatively, the application of VVA-based technology such as Miller cycle and iEGR to 85

diesel engines has been shown as an effective technology for exhaust emissions and EGT 86

control. This is due to the fact that Miller cycle achieved via early or late intake valve closing 87

(IVC) timings reduces the peak in-cylinder combustion temperature and air-fuel ratio. The 88

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iEGR realised via a 2IVO during exhaust stroke and/or exhaust valve re-opening (2EVO) 89

during intake stroke allows for the control of the in-cylinder hot residual gas fraction [14,15]. 90

Gonca et al. [16] evaluated the effect of Miller cycle operation on engine performance and 91

exhaust emissions by means of experimental and simulation analysis. The lower effective 92

compression ratio (ECR) led to a reduction of 30% in NOx emissions at the expense of lower 93

torque and fuel conversion efficiency. Rinaldini et al. [17] also carried out experimental and 94

numerical studies to analyse the influence of Miller cycle. The results showed that Miller cycle 95

operation reduced NOx and soot emissions by 25% and 60% respectively, which was attained 96

with a fuel efficiency penalty of 2% in a light-duty diesel vehicle in the European Driving 97

Cycle. Experimental investigation by Garg et al. [18] showed that the cylinder throttling via 98

early (EIVC) and late (LIVC) IVC reduced the volumetric efficiency. This resulted in a lower 99

in-cylinder mass, leading to an increase in EGT. The use of iEGR can retain hot residuals from 100

the previous cycle, which allows for the improvement in exhaust thermal management and 101

reduction in unburned HC and CO emissions at low engine loads [19–21]. 102

Other effective means for reducing NOx emissions is the introduction of cooled EGR to the 103

Miller cycle operation, as reported in our previous works [15,22]. Moreover, Kim et al. [23] 104

experimentally studied the combined use of Miller cycle with EGR in a single cylinder diesel 105

engine operating at low engine loads. The NOx emissions were reduced from 10 g/kWh to 106

approximately 1 g/kWh. Verschaeren et al. [24] revealed NOx reduction levels of more than 107

70% when using Miller cycle and EGR in a HD diesel engine. Experimental and simulation 108

studies by Benajes et al. [25,26] showed that EIVC and EGR can decrease the combustion 109

temperatures and create leaner local equivalence ratios, effectively curbing NOx and soot 110

formation. 111

However, the lower in-cylinder air-fuel ratio resulted from the combined use of Miller cycle 112

and EGR at high engine loads can deteriorate the combustion process, yielding poor fuel 113

conversion efficiency and high levels of soot and CO emissions [27–30]. Therefore, higher 114

intake air boost is necessary in order to increase or maintain the in-cylinder air-fuel ratio when 115

both Miller cycle and EGR strategies are applied at high engine loads. Kovács et al. [29] studied 116

the effect of boost pressure on Miller cycle operation with EGR in the upper load range of a 117

HD diesel engine. A significant improvement in soot and CO emissions was achieved as well 118

as a reasonable trade-off with NOx. Further investigations by Kovács et al. [31] demonstrated 119

that a very high turbocharger efficiency is needed to minimise the fuel consumption of the 120

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Miller cycle operation. Many other works have also shown that a higher boost pressure is the 121

key enabler for Miller cycle operation with EGR to achieve simultaneous high fuel conversion 122

efficiency and low exhaust emissions [32–34]. 123

To address the challenges encountered by current HD diesel engines, research and development 124

work is required in order to further optimise the combustion process. This study aims to 125

investigate advanced VVA-based combustion control strategies as means to improve upon 126

exhaust temperatures and reduce the emissions at low load operation as well as to increase fuel 127

conversion efficiency and reduce total fluid consumption at high load operation. 128

In particular, the current work is the first attempt to experimentally study and analyse the 129

potential of VVA-based technology at low and high engine load conditions. Advanced 130

combustion control strategies including the combinations of Miller cycle, internal and external 131

EGR, post injection, and highly boosted operation for emissions and EGT control and 132

efficiency improvement were demonstrated accordingly. In the last section, an overall 133

efficiency and emissions analysis based on the Euro VI NOx limit was carried out to determine 134

the effectiveness of VVA-based strategies for lowering the total fluid consumption of a HD 135

diesel engine. 136

The experimental study was carried out on a single-cylinder HD diesel engine equipped with a 137

VVA system. A one-dimensional (1D) engine simulation model was used to calculate the mean 138

in-cylinder gas temperatures (𝑇𝑇𝑚𝑚). The effectiveness of Miller cycle with iEGR was examined 139

at a light engine load of 2.2 bar IMEP (e.g. test point 1). The application of Miller cycle 140

operation combined with cooled EGR and post injection was investigated at a part engine load 141

of 6 bar IMEP (e.g. test point 2). Moreover, the potential of Miller cycle operating with EGR 142

and a higher boost pressure was explored at a high engine load of 17 bar IMEP (e.g. test point 143

3). The overall engine efficiency and cost-benefit of the optimum VVA-based combustion 144

control strategies were analysed and compared to those of the baseline diesel combustion 145

operation. 146

2. Experimental setup 147

2.1 Engine specifications and experimental facilities 148

Figure 1 shows the schematic diagram of the single cylinder heavy-duty diesel engine. A 149

Froude Hofmann AG150 eddy current dynamometer was coupled to absorb the engine power 150

output. Table 1 outlines the base hardware specifications of the test engine. The combustion 151

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system was designed based on the Yuchai YC6K 6-cylinder diesel engine, which consisted of 152

a 4-valve swirl-oriented cylinder head and a stepped-lip piston bowl design with a geometric 153

compression ratio of 16.8. The bottom end/short block was AVL-designed with two counter-154

rotating balance shafts. 155

156 Figure 1. Layout of the engine experimental setup. 157

Table 1. Specifications of the test engine. 158

Displaced Volume 2026 cm3

Stroke 155 mm

Bore 129 mm

Connecting Rod Length 256 mm

Geometric Compression Ratio 16.8

Number of Valves 4

Piston Type Stepped-lip bowl

Diesel Injection System Bosch common rail

Nozzle design 8 holes, 0.176 mm hole diameter,

included spray angle of 150°

Maximum fuel injection pressure 2200 bar

Maximum in-cylinder pressure 180 bar

159 The compressed air was supplied by an AVL 515 sliding vanes supercharger with closed loop 160

control. Two surge tanks were installed to damp out the strong pressure fluctuations in intake 161

and exhaust manifolds. The intake manifold pressure was finely controlled by a throttle valve 162

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located upstream of the intake surge tank. An Endress+Hauser Proline t-mass 65F thermal mass 163

flow meter was used to measure the fresh air mass flow rate. An electronically controlled 164

butterfly valve located downstream of the exhaust surge tank was used to independently control 165

the exhaust back pressure. High-pressure loop cooled external EGR was introduced to the 166

engine intake manifold located between the intake surge tank and throttle by using a pulse 167

width modulation-controlled EGR valve and the pressure differential between the intake and 168

exhaust manifolds. Coolant and oil pumps were driven by separate electric motors. Water 169

cooled heat exchangers were used to control the temperatures of the boosted intake air and 170

external EGR as well as engine coolant and lubricating oil. The coolant and oil temperatures 171

were kept within 356 ± 2 K. The oil pressure was maintained within 4.0 ± 0.1 bar throughout 172

the experiments. 173

The fuel injection parameters such as the injection pressure, start of injection (SOI), and the 174

number of injections (up to three injections per cycle) were controlled by a dedicated electronic 175

control unit (ECU). During the experiments, the diesel fuel was injected into the engine by a 176

high-pressure solenoid injector through a high pressure pump and a common rail with a 177

maximum fuel pressure of 2200 bar. The fuel consumption was determined by measuring the 178

total fuel supplied to and from the high pressure pump and diesel injector via two Coriolis flow 179

meters. The specifications of the measurement equipment can be found in Appendix A. 180

2.2 Variable valve actuation system 181

The engine was equipped with a prototype hydraulic lost-motion VVA system, which 182

incorporated a hydraulic collapsing tappet on the intake valve side of the rocker arm. The VVA 183

system allowed for the adjustment of the IVC timing and thus enable Miller cycle operation. 184

The intake valve opening (IVO) and closing (IVC) of the baseline case were set at 367 and -185

174 crank angle degrees (CAD) after top dead centre (ATDC), respectively. All valve events 186

were considered at 1 mm valve lift and the maximum intake valve lift event was set to 14 mm. 187

In addition, this system enables a 2IVO event during the exhaust stroke in order to trap iEGR 188

and increase the residual gas fraction. The earliest opening timing and the latest closing timing 189

of the 2IVO strategy were set at 160 CAD ATDC and 230 CAD ATDC, respectively. The 190

maximum valve lift of this configuration was 2 mm. Figure 2 shows the intake and exhaust 191

valve profiles for the baseline engine operation as well as for the LIVC and 2IVO cases. The 192

effective compression ratio, ECR, was calculated as 193

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𝐸𝐸𝐸𝐸𝐸𝐸 = 𝑉𝑉𝑖𝑖𝑖𝑖𝑖𝑖_𝑒𝑒𝑒𝑒𝑒𝑒

𝑉𝑉𝑡𝑡𝑡𝑡𝑖𝑖 (1) 194

where 𝑉𝑉𝑡𝑡𝑡𝑡𝑖𝑖 is the cylinder volume at top dead centre (TDC) position, and 𝑉𝑉𝑖𝑖𝑖𝑖𝑖𝑖_𝑒𝑒𝑒𝑒𝑒𝑒 is the 195

effective cylinder volume where the in-cylinder compressed air pressure is extrapolated to be 196

identical to the intake manifold pressure [35,36]. 197

198

Figure 2. Fixed exhaust and variable intake valve lift profiles. 199

2.3 Exhaust emissions measurement 200

A Horiba MEXA-7170 DEGR emission analyser was used to measure the exhaust gases such 201

as NOx, HC, CO, and CO2 in the exhaust pipe before the exhaust back pressure valve. In this 202

analyser system, gases including CO and CO2 were measured through a non-dispersive infrared 203

absorption (NDIR) analyser, HC was measured by a flame ionization detector (FID), and NOx 204

was measured by a chemiluminescence detector (CLD). To allow for the measurement at 205

elevated back pressure, a high pressure sampling module was used between the exhaust 206

sampling point and the emission analyser. A heated line was deployed to maintain the exhaust 207

gas sample temperature of approximately 192℃ to avoid condensation. The smoke number 208

was measured downstream of the exhaust back pressure valve using an AVL 415SE Smoke 209

Meter. The measurement was taken in filter smoke number (FSN) basis and thereafter was 210

converted to mg/m3 [37]. All the exhaust gas components were converted to net indicated 211

specific gas emissions (in g/kWh) according to [38]. In this study, the EGR rate was defined 212

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as the ratio of the measured CO2 concentration in the intake surge tank ((𝐸𝐸𝐶𝐶2%)𝑖𝑖𝑖𝑖𝑡𝑡𝑖𝑖𝑖𝑖𝑒𝑒) to the 213

CO2 concentration in the exhaust manifold ((𝐸𝐸𝐶𝐶2%)𝑒𝑒𝑒𝑒ℎ𝑖𝑖𝑎𝑎𝑎𝑎𝑡𝑡) as 214

𝐸𝐸𝐸𝐸𝐸𝐸 rate = (𝐶𝐶𝐶𝐶2%)𝑖𝑖𝑖𝑖𝑖𝑖𝑖𝑖𝑖𝑖𝑖𝑖(𝐶𝐶𝐶𝐶2%)𝑖𝑖𝑒𝑒ℎ𝑖𝑖𝑎𝑎𝑎𝑎𝑖𝑖

× 100% (2) 215

2.4 Data acquisition and analysis 216

The instantaneous in-cylinder pressure was measured by a Kistler 6125C piezo-electric 217

pressure transducer with a sampling resolution of 0.25 CAD. The high speed and low speed 218

National Instruments data acquisition (DAQ) cards were used to acquire the high and low 219

frequency signals from the measurement devices. The captured data from the DAQ as well as 220

the resulting engine parameters were displayed in real-time by an in-house developed transient 221

combustion analysis software. 222

The crank angle based in-cylinder pressure traces were recorded through an AVL FI Piezo 223

charge amplifier, averaged over 200 consecutive engine cycles, and used to calculate the IMEP 224

and apparent heat release rate (HRR). According to [1], the apparent HRR was calculated as 225

𝐻𝐻𝐸𝐸𝐸𝐸 =𝛾𝛾

(𝛾𝛾 − 1) 𝑝𝑝 𝑑𝑑𝑉𝑉𝑑𝑑𝑑𝑑

+ 1

(𝛾𝛾 − 1) 𝑉𝑉

𝑑𝑑𝑝𝑝𝑑𝑑𝑑𝑑

(3) 226

where 𝛾𝛾 is defined as the ratio of specific heats, which was assumed constant at 1.33 throughout 227

the engine cycle [39]; 𝑉𝑉 and 𝑝𝑝 are the in-cylinder volume and pressure, respectively; and 𝑑𝑑 is 228

the crank angle degree. 229

In this study, the mass fraction burned (MFB) was defined by the ratio of the integral of the 230

HRR and the maximum cumulative heat release. Combustion phasing (CA50) was determined 231

by the crank angle of 50% MFB. Combustion duration was represented by the period of time 232

between the crank angles of 10% (CA10) and 90% (CA90) MFB. Ignition delay was defined 233

as the period of time between the main SOI and the start of combustion (SOC), denoted as 0.3% 234

MFB point of the average cycle. The in-cylinder combustion stability was monitored by the 235

coefficient of variation of the IMEP (COV_IMEP) over the sampled cycles. 236

3. Methodology 237

3.1 Estimation of the total fluid consumption 238

An increase in engine-out NOx emissions can lead to a higher consumption of aqueous urea 239

solution in the aftertreatment system of an SCR equipped HD diesel engine. This can adversely 240

affect the total engine fluid consumption and thus the engine operational cost. Therefore, the 241

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total fluid consumption is estimated in this study in order to take into account both the measured 242

diesel flow rate (ṁ𝑡𝑡𝑖𝑖𝑒𝑒𝑎𝑎𝑒𝑒𝑑𝑑) and the estimated urea consumption in the SCR system (ṁ𝑎𝑎𝑢𝑢𝑒𝑒𝑖𝑖). As 243

the relative prices between diesel fuel and urea are different in different countries and regions, 244

the price and property of urea is simulated to be the same as diesel fuel in this study [40,41]. 245

According to [40,42], the required aqueous urea solution to meet the Euro VI NOx limit of 0.4 246

g/kWh can be estimated as 1% of the diesel equivalent fuel flow per g/kWh of NOx reduction. 247

�̇�𝑚𝑎𝑎𝑢𝑢𝑒𝑒𝑖𝑖 = 0.01�𝑁𝑁𝐶𝐶𝑁𝑁𝑒𝑒𝑖𝑖𝑒𝑒𝑖𝑖𝑖𝑖𝑒𝑒−𝑜𝑜𝑎𝑎𝑡𝑡 − 𝑁𝑁𝐶𝐶𝑁𝑁𝐸𝐸𝑎𝑎𝑢𝑢𝑜𝑜 𝑉𝑉𝑉𝑉��̇�𝑚𝑡𝑡𝑖𝑖𝑒𝑒𝑎𝑎𝑒𝑒𝑑𝑑 (5) 248

By adding the measured diesel flow rate to the estimated urea flow rate allowed for the 249

calculation of total fluid consumption, which was defined as 250

�̇�𝑚𝑡𝑡𝑜𝑜𝑡𝑡𝑖𝑖𝑑𝑑 = �̇�𝑚𝑡𝑡𝑖𝑖𝑒𝑒𝑎𝑎𝑒𝑒𝑑𝑑 + �̇�𝑚𝑎𝑎𝑢𝑢𝑒𝑒𝑖𝑖 (6) 251

3.2 Calculation of the mean in-cylinder gas temperature 252

In order to better analyse the influence of different combustion control strategies on in-cylinder 253

combustion process, a 1D engine simulation has been carried out using Ricardo Wave software 254

to estimate the mean in-cylinder gas temperatures. As demonstrated in our previous works 255

[22,43], the combustion process was simulated by using the experimentally derived HRR 256

profile based on the measured in-cylinder pressure, the heat transfer was calculated by the 257

Woschni heat transfer model, and the thermodynamic state of the in-cylinder gas was estimated 258

by using a two-zone model. In all cases, the intake air mass flow rate, IMEP, in-cylinder 259

pressure, intake and exhaust manifold pressures were calibrated against the experimental data 260

in order to validate the 1D engine model. Finally, the validated 1D engine model was used to 261

calculate the mean in-cylinder gas temperatures. 262

3.3 Test conditions 263

In this study, the experimental work was carried out at a speed of 1150 rpm and a light engine 264

load of 2.2 bar IMEP, as well as at a constant speed of 1250 rpm and the engine loads of 6 bar 265

and 17 bar IMEP. These conditions were denoted as test point 1, 2, and 3, respectively. Figure 266

3 shows the location of the World Harmonized Stationary Cycle (WHSC) test points over a 267

heavy-duty diesel engine operation map. The WHSC is a legislated test cycle adopted in the 268

Euro VI emission standard [44]. The size of the circle represents the weighting factor. A larger 269

circle indicates a higher relative weight of the engine operation condition over the WHSC. 270

Figure 3 also shows the three test points, which are located within the area of the WHSC test 271

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cycle. In particular, the test point 1 represents a typical engine operating condition of a transient 272

HD drive cycle and is typically characterised by an exhaust gas temperature below 200℃. 273

Eng

ine

load

(bar

IMEP

)

0

5

10

15

20

25

30

Engine speed (rpm)600 800 1000 1200 1400 1600 1800

Engine Operation Map WHSC Test Points

Test point 1

Test point 2

Test point 3

274 Figure 3. Experimental test points and WHSC operating conditions over an estimated HD 275

diesel engine speed-load map. 276

Table 2 summarises the engine test conditions for the different engine combustion control 277

strategies used at the three test points. The intake pressure set points of the baseline engine 278

operation were taken from a corresponding 6-cylinder HD diesel engine, which complies with 279

the Euro V emissions legislation. The IVC in the Miller cycle mode was set at -100 and -105 280

CAD ATDC at the low engine loads of 2.2 bar IMEP (test point 1) and 6 bar IMEP (test point 281

2), respectively. These settings have been determined in our previous studies [15,43]. At the 282

high load of 17 bar IMEP (test point 3), the IVC was advanced to -115 CAD ATDC. Such 283

settings were necessary in order to avoid combustion instability, excessive smoke emissions, 284

as well as to minimise the demand on the boosting system when operating the engine with 285

Miller cycle and EGR. 286

At the test point 1, the optimum operation mode was determined when the EGT achieved more 287

than 200℃ necessary to initiate the emissions control operation while achieving comparable 288

emissions and efficiency to the baseline operation. This was fulfilled by the addition of iEGR 289

via 2IVO event to a Miller cycle mode with an IVC at -100 CAD ATDC. The diesel injection 290

timing and the fuel injection pressure were held constant at -5.7 CAD ATDC and 500 bar, 291

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respectively. The exhaust back pressure was kept similar to the intake pressure for all three 292

operating modes at this test point. 293

At the test point 2, the optimum operating condition employed an external EGR of 15% 294

combined with a Miller cycle operation (LIVC at -105 CAD ATDC). In addition, a 12 mm3 295

post injection at 18 CAD ATDC was applied. This post injection strategy was found to give 296

the best trade-off between exhaust emissions and fuel conversion efficiency in our previous 297

study [43]. Furthermore, a small pilot injection of 3 mm3 with a constant dwell time of 1 ms 298

prior to the main injection timing was employed in order to keep the maximum pressure rise 299

rate (PRR) below 20 bar/CAD. 300

At the test point 3, the optimum operation mode used an EGR rate of 15% and a higher intake 301

pressure of 2.62 bar. The exhaust back pressure was adjusted to maintain a constant pressure 302

differential of 0.10 bar above the intake pressure, simulating the real engine operation with a 303

turbocharger and achieving the required EGR rate. The fuel injection timings of three operating 304

modes were optimised between -2.5 and -12 CAD ATDC in order to achieve the minimum 305

total fluid consumption. 306

Diesel injection pressures were increased at higher engine loads in order to control the levels 307

of smoke but held constant at a given load as shown in Table 2. The maximum in-cylinder 308

pressure was limited to 180 bar. Stable engine operation was determined by controlling the 309

COV_IMEP below 3%. 310

Table 2 Engine testing conditions for baseline, Miller cycle, and optimum engine operations. 311

312

Test point

Engine speed

Engine load

Operating mode

Main SOI

Injection pressure

Intake pressure

Exhaust pressure IVC iEGR eEGR Pre-

inj. Post-inj.

- rpm bar IMEP - CAD

ATDC bar bar bar CAD ATDC - % - -

1 1150 2.2

Baseline

-5.7 500 1.16 1.20

-178 No

0 No No Miller cycle -100 No

Optimum -100 Yes

2 1250 6.0

Baseline

-4 1150 1.44 1.54

-178

No

0

Yes

No

Miller cycle -105 0 No

Optimum -105 15 Yes

3 1250 17.0

Baseline -6

1450

2.32 2.42 -178

No

0

No No Miller cycle -7.5 2.32 2.42 -115 0

Optimum -8 2.62 2.72 -115 15

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4. Results and discussions 313

4.1 Analysis of the in-cylinder pressure and heat release rate 314

Figures 4, 5, and 6 show a comparison of the in-cylinder pressure and heat release rate (HRR) 315

for the baseline, Miller cycle, and optimum engine operations at the three test points. At the 316

test point 1 shown in Figure 4, the Miller cycle and the optimum cases were characterised by 317

significantly lower in-cylinder gas pressure than that of the baseline operation. This was 318

attributed to a later initiation of the compression process resulted from the LIVC (e.g. lower 319

ECR), which lowered the in-cylinder gas pressure and temperature [45]. Consequently, the 320

combustion process was shifted far away from TDC. Despite the recirculation of residual gases 321

back to the cylinder could lead to a higher specific heat capacity, the introduction of iEGR on 322

the optimum engine operating condition enhanced the combustion process via a higher in-323

cylinder gas temperature resulted from the trapped hot residual gas [15]. This was a reason for 324

a relatively more advanced SOC and higher peak HRR than the Miller cycle operation, which 325

can potentially improve the combustion efficiency and fuel conversion efficiency. 326

At the test point 2, the optimised main SOI of the three different operating modes was obtained 327

at -4 CAD ATDC, as depicted in Figure 5. The application of an LIVC in the Miller cycle and 328

optimum operation modes reduced the in-cylinder pressure during the compression stroke as a 329

result of a lower ECR. In the optimum engine operation mode, the combined use of a post 330

injection and EGR lowered the peak HRR and further decreased the maximum in-cylinder gas 331

pressure. This was attributed to a decrease in the amount of fuel injected during the main 332

injection combined with the dilution and specific heat capacity effects of the EGR that slow 333

down the reaction rates [46]. A second heat release peak was generated by the combustion of 334

the post injected fuel, which can help to minimise soot emissions by enhancing fuel-air mixing 335

and increasing the combustion temperature of late combustion process, according to the 336

findings of [47,48]. 337

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In-c

ylin

der p

ress

ure

[bar

]

0

20

40

60

HRR

[J/C

AD]

0

100

200

300

400Test point 11150 rpm, 2.2 bar [email protected] CAD ATDC

Baseline Miller cycle Optimum

Inje

ctor

cur

rent

sig

nal

[A/1

0]

0

2

4

CAD ATDC-10 0 10 20 30

338 Figure 4. In-cylinder pressure, HRR, and diesel injector signal for different engine 339

combustion control strategies at test point 1. 340

In-c

ylin

der p

ress

ure

[bar

]

0

30

60

90HR

R [J

/CAD

]

0

100

200

300

400Test point 21250 rpm, 6 bar IMEPMain SOI@-4 CAD ATDC

Baseline Miller cycle Optimum

Inje

ctor

cur

rent

sig

nal

[A/1

0]

0

2

4

CAD ATDC-15 -5 5 15 25 35

341 Figure 5. In-cylinder pressure, HRR, and diesel injector signal for different engine 342

combustion control strategies at test point 2. 343

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As the engine load was increased to 17 bar IMEP, the diesel injection timing was optimised to 344

achieve the minimum total fluid consumption. The Miller cycle operation allowed for a more 345

advanced SOI than the baseline engine operation, as shown in Figure 6. However, the level of 346

NOx reduction achieved with a Miller cycle strategy was limited primarily due to the small 347

impact on the in-cylinder flame temperature, as reported by Benajes et al. [49]. 348 In

-cyl

inde

r pre

ssur

e [b

ar]

0

40

80

120

160

HRR

[J/C

AD]

0

150

300

450Test point 31250 rpm, 17 bar IMEPOptimised SOI

Baseline Miller cycle Optimum

Inje

ctor

cur

rent

sig

nal

[A/1

0]

0

2

4

CAD ATDC-20 0 20 40

349 Figure 6. In-cylinder pressure, HRR, and diesel injector signal for different engine 350

combustion control strategies at test point 3. 351

The use of EGR can effectively curb NOx emissions but the fuel conversion efficiency could 352

be compromised when introducing EGR to Miller cycle operation at high engine loads. This is 353

because of a decrease in the charging efficiency and a reduction of the lambda when using the 354

LIVC strategy, according to the findings of [17]. In order to overcome such shortcomings, 355

higher boost pressure was adopted in the optimum engine operation mode to improve the in-356

cylinder air-fuel ratio. This helped to increase the compression pressure while maintaining the 357

potential benefit of a more advanced combustion process for maximum fuel conversion 358

efficiency and minimum NOx emissions. 359

It should be noted that a conventional turbocharging system is likely not able to deliver the 360

required air flow rate when operating the engine with Miller cycle and EGR [50]. For this 361

reason, a more sophisticated boosting system such as a two-stage variable geometry 362

turbocharger configuration would be needed to deliver the desired boost pressures and 363

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overcome this limitation of a Miller cycle engine operation [31,51,52]. However, a high-364

performance turbocharging system would require additional cost, thus increasing the total 365

engine operational cost [2,52,53]. 366

Figure 7 shows the calculated mean in-cylinder gas temperatures of different engine 367

combustion control strategies at the three test points. The use of Miller cycle strategy via an 368

LIVC decreased the gas temperatures during the compression stroke, especially at the test point 369

1 due to the use of a relatively later IVC timing than that employed in the other two test points. 370

The reduced compressed gas temperatures were attributed to a decrease in the ECR. However, 371

the peak mean in-cylinder gas temperature was increased when compared to the baseline engine 372

operation. This happened because of a reduction in the intake air mass flow rate, which 373

decreased the in-cylinder heat capacity during the combustion event [25]. 374

Mea

n in

-cyl

inde

r gas

tem

pera

ture

[K]

600

1000

1400

1800 Baseline Miller cycle Optimum

Test point 1SOI=-5.7 CAD ATDC

Mea

n in

-cyl

inde

r gas

tem

pera

ture

[K]

800

1100

1400

1700

Test point 2SOI=-11.5 CAD ATDC

Mea

n in

-cyl

inde

r gas

tem

pera

ture

[K]

900

1300

1700

2100

CAD-20 0 20 40

Test point 3Optimised SOI

375 Figure 7. Calculated mean in-cylinder gas temperatures for baseline, Miller cycle, and 376

optimum engine operations at the three test points. 377

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The addition of iEGR to the Miller cycle operation at the test point 1 increased the compressed 378

gas temperature owing to the presence of hot residual gas, despite the higher heat capacity of 379

the in-cylinder charge. This resulted in a higher peak 𝑇𝑇𝑚𝑚 than the Miller cycle case as well as 380

higher temperatures during the expansion stroke. At the test point 2, the introduction of EGR 381

in the optimum operation mode had little impact on the compressed gas temperature. The post 382

injection, however, led to a reduction in the peak combustion temperature and an increase in 383

the mean in-cylinder gas temperatures during the late stages of the combustion process, which 384

can help to raise the EGT and improve the SCR operation. At the test point 3, the optimum 385

mode with the use of a higher intake pressure and EGR increased the 𝑇𝑇𝑚𝑚 during the combustion 386

process compared to the baseline engine operation, despite a reduction in the 𝑇𝑇𝑚𝑚 during the 387

compression stroke. This was a result of the more advanced SOI, which led to earlier and faster 388

heat release than that of the baseline operation. 389

4.2 Combustion characteristics 390

Figure 8 shows the resulting heat release characteristics for the different engine combustion 391

control strategies at the three test points. At the test point 1, the use of an LIVC had a significant 392

impact on the ignition delay, increasing the ignition delay by approximately 4 CAD compared 393

to the baseline operation. This was a result of the reduced ECR, which delayed the SOC. This 394

was also the reason for the delayed combustion phasing (CA50). However, a higher degree of 395

premixed combustion accelerated the combustion rate of the late combustion phase as 396

represented by a shorter period of CA50-CA90. As a result, a shorter combustion duration was 397

obtained than that of the baseline operation. At the test points 2 and 3, however, the Miller 398

cycle operation had less impact on the ignition delay compared to that of the test point 1. This 399

could be explained by the use of a relatively earlier IVC timing and a better ignition condition 400

when operating at a relatively higher engine load. The later ignition and longer combustion 401

process for the Miller cycle cases lengthened the late combustion phase as shown by the longer 402

CA50-CA90 period. These effects contributed to a longer combustion duration (CA10-CA90). 403

In comparison to the Miller cycle operation, the use of iEGR on the optimum operation mode 404

advanced the SOC and thus decreased the ignition delay at test point 1. This combustion 405

strategy also advanced the CA50 and led to a shorter combustion duration despite the slightly 406

longer period of CA50-CA90. At the test point 2, the addition of a post injection delayed the 407

CA50 as more diesel fuel was burned during a relatively later combustion phase. In addition, 408

the introduction of EGR in the optimum operation mode contributed to the resulting later CA50 409

as the lower oxygen concentration decreased the combustion rate. As a result, the period of 410

Page 18: 1 VVA-based combustion control strategies for efficiency · 2021. 5. 5. · 18 combustion control strategies have been researched as means improving upon the of engine 19 exhaust

CA50-CA90 was longer for the optimum engine operation with post injection and EGR. These 411

effects resulted in an increase in the combustion duration by up to 5.5 CAD when compared to 412

the Miller cycle operation. At the test point 3, the Miller cycle mode allowed for a more 413

advanced SOI to achieve the minimum total fluid consumption, resulting in a slightly earlier 414

CA50 than the baseline engine operation. In the optimum engine operation, the use of EGR 415

and a higher boost pressure resulted in similar heat release characteristics to that of the Miller 416

cycle operation. 417

Com

bust

ion

dura

tion

[CAD

]

8

16

24

32

Test point 1 Test point 2 Test point 3

CA50

[CAD

ATD

C]

6

10

14

18

Test point 1 Test point 2 Test point 3

Baseline Miller cycle Optimum

CA50

-CA9

0 [C

AD]

4

10

16

22

Igni

tion

dela

y [C

AD]

4

8

12

16

418 Figure 8. Heat release characteristics for baseline, Miller cycle, and optimum engine 419

combustion control strategies at the three different test points. 420

4.3 Engine-out emissions 421

Figure 9 depicts the engine-out emissions for the baseline, Miller cycle, and optimum engine 422

operations at the three different test points. At the test point 1, the engine-out NOx emissions 423

were reduced slightly in the Miller cycle operation due to the decreased mass of air and the 424

lower burned gas temperature caused by the LIVC strategy [43]. However, the NOx emissions 425

were increased slightly by the addition of iEGR. This was attributed to the introduction of hot 426

residual gas, which shortened the combustion duration and increased the combustion 427

temperature. Nevertheless, the use of an LIVC, with and without adding iEGR, significantly 428

decreased soot emissions from approximately 0.05 g/kWh in the baseline operation to less than 429

0.01 g/kWh in the Miller cycle operation. This can be explained by the higher degree of 430

premixed combustion resulted from the longer ignition delay, which improved the air-fuel 431

mixing and consequently the combustion process. In addition, the resulting higher combustion 432

temperature helped to improve the oxidation of smoke, which contributed to the reduction in 433

soot emissions. The longer ignition delay and the later combustion process, however, resulted 434

Page 19: 1 VVA-based combustion control strategies for efficiency · 2021. 5. 5. · 18 combustion control strategies have been researched as means improving upon the of engine 19 exhaust

in higher levels of unburned HC and CO emissions. Nevertheless, the introduction of iEGR 435

helped to curb the formation of HC and CO as the trapped hot residual gas shortened the 436

ignition delay, increased the combustion temperature, and consequently improved the 437

combustion process. 438

ISH

C [g

/KW

h]

0

2

4

6

ISso

ot [g

/KW

h]

0.00

0.02

0.04

0.06

Test point 1 Test point 2 Test point 3

ISC

O [g

/KW

h]

0

6

12

18

Test point 1 Test point 2 Test point 3

ISN

Ox

[g/K

Wh]

0

5

10

15

Baseline Miller cycle Optimum

439

Figure 9. Exhaust emissions for baseline, Miller cycle, and optimum engine combustion 440 control strategies at the three different test points. 441

For both test points 2 and 3, the Miller cycle operation achieved slightly lower engine-out NOx 442

emissions than the baseline cases. A significant reduction in NOx emissions was obtained via 443

the addition of EGR owing to the lower combustion temperature and lower in-cylinder oxygen 444

concentration. However, the in-cylinder oxygen availability of the combined use of Miller 445

cycle and EGR can be decreased noticeably, resulting in excessive smoke and CO emissions, 446

as demonstrated by Verschaeren et al. [24]. Therefore, an advanced combustion control 447

strategy was employed to help address these issues. As showed in Figure 9, the use of a post 448

injection at the test point 2 and a highly boosted strategy at the test point 3 helped to curb the 449

levels of soot emissions to approximately 0.01 g/kWh. All engine combustion control strategies 450

at the test points 2 and 3 yielded significantly lower levels of CO and unburned HC than those 451

of the test point 1. This was primarily because of the higher gas temperatures during the 452

expansion and exhaust strokes as the engine load increased. 453

4.4 Engine performance 454

Figure 10 depicts the engine performance parameters for the baseline, Miller cycle, and 455

optimum engine operations at the three different test points. The LIVC strategy in the Miller 456

cycle operation reduced the lambda due to a reduction of the in-cylinder mass trapped when 457

Page 20: 1 VVA-based combustion control strategies for efficiency · 2021. 5. 5. · 18 combustion control strategies have been researched as means improving upon the of engine 19 exhaust

compared to the baseline cases. This was the primary reason for an increase in EGT from 163℃ 458

in the baseline operation to 203℃ in the optimum operation, which is extremely important for 459

achieving efficient exhaust aftertreatment operation at low engine loads. The delayed 460

combustion process and longer combustion duration for the Miller cycle operation adversely 461

affected the fuel conversion efficiency. In particular, the lower combustion efficiency of 96.1% 462

at the test point 1 contributed to a decrease in the fuel conversion efficiency of 5% to 38.9%. 463

This was a result of an increase in unburned HC and CO emissions caused by the lower 464

combustion temperatures. 465

Compared to the Miller cycle case, the addition of iEGR increased the combustion efficiency 466

from 96.1% to 98.6% and the fuel conversion efficiency from 38.9% to 40.4% while operating 467

the engine at the test point 1. This was attributed to the presence of hot residual gas, which 468

helped improve the combustion process and resulted in a higher lambda value. At the test point 469

2, the optimum engine operation with post injection and EGR decreased the lambda further, 470

yielding a higher EGT. These effects combined with a longer combustion duration resulted in 471

a reduction in fuel conversion efficiency when comparing to both baseline and Miller cycle 472

operations. However, the lambda of the optimum engine operation at test point 3 was 473

maintained the same to the Miller cycle operation via a higher intake pressure. The highly 474

boosted strategy together with a more advanced combustion phasing in the optimum engine 475

operation led to an increase in the fuel conversion efficiency of 3.3% to 46.5% compared to 476

the Miller cycle mode. This was more than the fuel conversion efficiency produced by baseline 477

case. 478 Co

mbu

stio

n ef

ficie

ncy

[%]

94

96

98

100

EGT

[deg

C]

150

300

450

600

Test point 1 Test point 2 Test point 3

200 deg C

Fuel

con

vers

ion

effic

ienc

y [%

]

38

41

44

47

Test point 1 Test point 2 Test point 3

Lam

bda

[-]

1.0

2.5

4.0

5.5 Baseline Miller cycle Optimum

479 Figure 10. Engine performance for baseline, Miller cycle, and optimum engine combustion 480

control strategies at the three different test points. 481

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4.5 Overall engine efficiency and potential benefit analysis 482

In this section, the overall engine efficiency of different engine combustion control strategies 483

was analysed by taking into account the consumption of aqueous urea solution in the SCR 484

system. Additionally, the potential benefit of advanced VVA-based combustion control 485

strategies was demonstrated by comparing the results of the optimum cases to those of the 486

baseline engine operation. 487

The estimated urea flow rate in the aftertreatment system and the resulting total fluid 488

consumption are depicted in Figure 11. As the urea consumption depends mainly on engine-489

out NOx emissions, reductions in the levels of engine-out NOx can help minimise the use of 490

urea in the SCR system. The Miller cycle and the optimum engine operations decreased the 491

urea consumption via lower engine-out NOx emissions. This helped to minimise the total fluid 492

consumption, particularly at high engine load (e.g. test point 3) where the total fluid 493

consumption was reduced from 7.35 kg/h in the baseline case to 6.95 kg/h in the optimum 494

engine operation mode. At the test point 1, however, the Miller cycle and optimum engine 495

operations led to a slight increase in total fluid consumption when compared to the baseline 496

operation. This was attributed to the lower fuel conversion efficiency and similar level of 497

engine-out NOx emissions. 498 Es

timat

ed u

rea

cons

umpt

ion

[kg/

h]

0.0

0.3

0.6

0.9

Baseline Miller cycle Optimum

Tota

l flu

id c

onsu

mpt

ion

[kg/

h]

0

3

6

9

Test point 1 Test point 2 Test point 3 499

Figure 11. Overall engine efficiency analysis for baseline, Miller cycle, and optimum engine 500 operation at the three different test points. 501

Figure 12 provides an overall assessment of the potential benefit of the VVA-based optimum 502

engine operation in terms of exhaust emissions, engine performance, and total fluid 503

consumption at the three test points investigated. Positive results achieved in the optimum 504

Page 22: 1 VVA-based combustion control strategies for efficiency · 2021. 5. 5. · 18 combustion control strategies have been researched as means improving upon the of engine 19 exhaust

engine operation are denoted with a green circle while the negative results are highlighted with 505

a red circle. 506

The results of the optimum engine operations were compared to the baseline cases. The analysis 507

revealed that the Miller cycle operation with iEGR increased EGT by 40℃ and minimised soot 508

emissions by 82% at the test point 1. These improvements were attained at the expense of little 509

variation in NOx emissions and a reduction of 1.5% on the fuel conversion efficiency, resulting 510

in an increase in the total fluid consumption of 0.2%. 511

Varia

tion

in IS

NOx

[%]

-90

-60

-30

0

30

-67% -68%

+0.2%

Varia

tion

in E

GT

[deg

C]

0

20

40

60

80

+40

+75

+24+40Va

riatio

n in

fuel

conv

ersi

on e

ffici

ency

[%]

-4

-2

0

2

4

-3.0%

+1.5%

Varia

tion

in IS

soot

[%]

-1500150300450600

-82%

+45%

-1.5%

+545%

-1.5%

less than0.01g/kWh

+0.2%

Varia

tion

in to

tal f

luid

cons

umpt

ion

[%]

-7

-5

-3

-1

1

VVA-based optimum engine operations

-2.2%

-5.4%

Test point 1 Test point 2 Test point 3

512 Figure 12. Overall evaluation of the potential benefit for the optimum engine operations at 513

the three different test points. The variations in engine performance and emissions are relative 514 to those for the baseline cases. 515

The combined use of Miller cycle with EGR and post injection increased the EGT by 75℃ 516

while reducing the NOx emissions by 67% at the test point 2. As a result, this strategy decreased 517

the total fluid consumption by 2.2% despite the lower fuel conversion efficiency. At the test 518

Page 23: 1 VVA-based combustion control strategies for efficiency · 2021. 5. 5. · 18 combustion control strategies have been researched as means improving upon the of engine 19 exhaust

point 3, the combination of a Miller cycle strategy with EGR and a higher boost pressure 519

increased the fuel conversion efficiency by 1.5% while reducing the NOx emissions by 68%. 520

These improvements yield a reduction of 5.4% in the total fluid consumption. Overall, the 521

results demonstrated that an advanced VVA-based combustion control strategy enables exhaust 522

thermal management and exhaust emissions control of a HD diesel engine operating at low 523

engine loads (e.g. test points 1 and 2). The findings also indicated that an alternative 524

combustion control strategy with Miller cycle can attain higher fuel conversion efficiency and 525

lower total fluid consumption than those typically found on a conventional HD diesel engine 526

operating at high engine loads (e.g. test point 3). 527

5. Conclusions 528

In this study, experiments were performed on a HD diesel engine operating at a typical light 529

engine load of 2.2 bar IMEP with low EGT and two other engine loads of 6 and 17 bar IMEP 530

located within WHSC test cycle. The aim of the research was to investigate advanced VVA-531

based combustion control strategies as means to overcome the challenges encountered by 532

current HD diesel engines. At 2.2 and 6 bar IMEP, the study was focused on increasing exhaust 533

gas temperature for optimum exhaust emissions control. At 17 bar IMEP, the investigation 534

aimed at increasing the fuel conversion efficiency and reducing the total fluid consumption. 535

Both Miller cycle and iEGR operations were realised by means of a VVA system. Cooled 536

external EGR and multiple injections were achieved via a high pressure loop EGR and a 537

common rail fuel injection system, respectively. The primary findings can be summarised as 538

follows: 539

1. Optimised VVA-based combustion control strategies were effective means of managing 540

the exhaust gas temperature at low engine loads, increasing EGT by 40℃ at 2.2 bar IMEP 541

and by 75℃ at 6 bar IMEP. In particular, the resulting EGT was higher than 200℃ at 2.2 542

bar IMEP, which is more than the minimum necessary to initiate the exhaust emissions 543

control. These improvements were attained at the expense of a slightly lower fuel 544

conversion efficiency. 545

2. At a light engine load of 2.2 bar IMEP (test point 1), the Miller cycle strategy decreased 546

soot emissions by 82% compared to the baseline engine operation. The addition of iEGR 547

helped to improve the combustion efficiency via lower unburned HC and CO emissions. 548

3. At the part load of 6 bar IMEP (test point 2), the combination of Miller cycle with EGR 549

and a post injection of 12 mm3 at 18 CAD ATDC allowed for a reduction of 67% in NOx 550

Page 24: 1 VVA-based combustion control strategies for efficiency · 2021. 5. 5. · 18 combustion control strategies have been researched as means improving upon the of engine 19 exhaust

emissions. Furthermore, the total fluid consumption was reduced by 2.2% despite a 551

reduction in fuel conversion efficiency of 3.0%. 552

4. At the high load condition of 17 bar IMEP (test point 3), the optimum engine operation 553

employed Miller cycle, EGR, and a higher boost pressure. This enabled an increase of 1.5% 554

in fuel conversion efficiency and a reduction of 68% in NOx emissions. These 555

improvements contributed to a reduction in total fluid consumption of 5.4%. 556

5. Overall, an advanced VVA-based combustion control strategy enabled exhaust emissions 557

and EGT control at low engine loads, as well as helped to increase the fuel conversion 558

efficiency for lower total fluid consumption at high engine loads. These improvements can 559

minimise the total engine operational cost of future HD diesel engines. 560

Contact information 561

Wei Guan 562 [email protected] 563 [email protected] 564 Centre for Advanced Powertrain and Fuels Research 565 College of Engineering, Design and Physical Sciences 566 Brunel University London 567 Kingston Lane 568 Uxbridge 569 Middlesex UB8 3PH 570 United Kingdom 571

Acknowledgments 572

The first author, Mr W Guan, would like to acknowledge the Guangxi Yuchai Machinery 573 Company for supporting his PhD study supervised by Prof. Zhao at Brunel University London. 574

Declaration of conflicting interests 575

The author(s) declared no potential conflicts of interest with respect to the research, authorship, 576

and/or publication of this article. 577

Funding 578

The author(s) disclosed receipt of the following financial support for the research, authorship, 579

and/or publication of this article: Funding for this project was provided by Guangxi Yuchai 580

Machinery Company. 581

Definitions/Abbreviations 582

ATS Aftertreatment System.

Page 25: 1 VVA-based combustion control strategies for efficiency · 2021. 5. 5. · 18 combustion control strategies have been researched as means improving upon the of engine 19 exhaust

ATDC

CA90

CA50

CA10

CAD

CLD

CO

After Firing Top Dead Center.

Crank Angle of 90% Cumulative Heat Release.

Crank Angle of 50% Cumulative Heat Release.

Crank Angle of 10% Cumulative Heat Release.

Crank Angle Degree.

Chemiluminescence Detector.

Carbon Monoxide.

CO2

COV_IMEP

(CO2%)intake

(CO2%)exhaust

DAQ

DOC

ECR

ECU

EGR

EGT

EVO

EVC

EIVC

FID

FSN

HCCI

HRR

HC

HD

iEGR

IMEP

IVO

IVC

ISsoot

ISNOx

ISCO

Carbon Dioxide.

Coefficient of Variation of IMEP.

CO2 concentration in the intake manifold.

CO2 concentration in the exhaust manifold.

Data Acquisition.

Diesel Oxidation Catalyst.

Effective Compression Ratio.

Electronic Control Unit.

Exhaust Gas Recirculation.

Exhaust Gas Temperature.

Exhaust Valve Opening.

Exhaust Valve Closing.

Early Intake Valve Closing.

Flame Ionization Detector.

Filter Smoke Number.

Homogenous Charge Compression Ignition.

Heat Release Rate.

Hydrocarbons.

Heavy Duty.

Internal Exhaust Gas Recirculation.

Indicated Mean Effective Pressure.

Intake Valve Opening.

Intake Valve Closing.

Net Indicated Specific Emissions of Soot.

Net Indicated Specific Emissions of NOx.

Net Indicated Specific Emissions of CO.

Page 26: 1 VVA-based combustion control strategies for efficiency · 2021. 5. 5. · 18 combustion control strategies have been researched as means improving upon the of engine 19 exhaust

ISHC

LIVC

LTC

MFB

ṁurea

ṁdiesel

ṁtotal

NDIR

NOx

PM

PCCI

PPCI

PRR

SCR

SOI

SOC

TDC

Tm

VVA

WHSC

Net Indicated Specific Emissions of Unburned HC.

Late Intake Valve Closing.

Low Temperature Combustion.

Mass Fraction Burned.

Aqueous Urea Solution Consumption.

Diesel Flow Rate.

Total Fluid Consumption.

Non-Dispersive Infrared Absorption.

Nitrogen Oxides.

Particulate Matter

Premixed Charge Compression Ignition.

Partially Premixed Charge Compression Ignition.

Pressure Rise Rate.

Selective Catalytic Reduction.

Start of Injection.

Start of Combustion.

Firing Top Dead Centre.

Mean in-cylinder gas temperature.

Variable Valve Actuation.

World Harmonized Stationary Cycle.

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Appendix A. Test cell measurement devices 741

Variable Device Manufacturer Measurement range Linearity/Accuracy

Speed AG 150 Dynamometer Froude Hofmann 0-8000 rpm ± 1 rpm

Torque AG 150 Dynamometer Froude Hofmann 0-500 Nm ± 0.25% of FS

Diesel flow rate (supply)

Proline promass 83A DN01 Endress+Hauser 0-20 kg/h ± 0.10% of reading

Diesel flow rate (return)

Proline promass 83A DN02 Endress+Hauser 0-100 kg/h ± 0.10% of reading

Intake air mass flow rate

Proline t-mass 65F Endress+Hauser 0-910 kg/h ± 1.5% of reading

In-cylinder pressure

Piezoelectric pressure sensor

Type 6125C Kistler 0-300 bar ≤ ± 0.4% of FS

Intake and exhaust pressures

Piezoresistive pressure sensor

Type 4049A Kistler 0-10 bar ≤ ± 0.5% of FS

Oil pressure Pressure

transducer UNIK 5000

GE 0-10 bar < ± 0.2% FS

Temperature Thermocouple K Type RS 233-1473K ≤ ± 2.5 K

Intake valve lift S-DVRT-24

Displacement Sensor

LORD MicroStrain 0-24 mm ± 1.0% of reading

using straight line

Smoke number 415SE AVL 0-10 FSN - Fuel injector current signal

Current Probe PR30 LEM 0-20A ± 2 mA

742

743

744

745

746

747

748

749

750

751

752

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Paper Correction 753 754

Dear Organizers and Reviewers, 755

Thank you for your kind comments and suggestions to the revised manuscript. We have 756

modified the manuscript accordingly, and detailed corrections are listed below point by point. 757

The paragraphs in black are the reviewers’ comments, while our responses are listed in blue. 758

All the modifications in the manuscript are highlighted in red. 759

We look forward to hearing from you. 760

Sincerely, 761

Wei Guan 762

Brunel University London 763

Reviewer(s)' Comments to Author: 764

765

Reviewer: 2 766

Comments to the Author 767

After reading carefully the new version of the paper I appreciate the effort carried out by the 768

authors to provide suitable answers to my questions and, on the light of the new information 769

added to the manuscript, I consider this version as complete and correct. Then, the quality of 770

the manuscript fits now the high standards of IJER and my recommendation is publishing it in 771

its current status. 772

773

Reviewer: 1 774

Comments to the Author 775

Although most of the issues from the first review have been addressed accordingly, I would at 776

least strongly recommend the following minor revisions before publication (- the numbers refer 777

to my original review): 778

Page 34: 1 VVA-based combustion control strategies for efficiency · 2021. 5. 5. · 18 combustion control strategies have been researched as means improving upon the of engine 19 exhaust

(1) Concerning the novelty of your work, I understand and accept that you are attributing this 779

to the combination of both low-load and high-load application of the measures studied. 780

However, I still wonder if it is really necessary to explicitly stress the "originality and novelty" 781

in the introduction, as this might provoke expectations by some readers which the paper might 782

not be able to satisfy. My suggestion would be to simply erase the sentence "Therefore, this 783

work includes a good novelty and originality." and leave it up to the reader to decide... 784

Thanks. We are agree with it and the sentence “Therefore, this work includes a good novelty 785

and originality” has been removed from the Introduction. 786

(2) With respect to the influence of specific heat capacity, I agree with the statement added on 787

page 17 ("...despite the higher heat capacity of the in-cylinder charge."); however, I am quite 788

confused by the contradictory statement added on page 13 ("Despite the recirculation of 789

residual gases back to the cylinder could lead to a >>lower<< specific heat..."), as the specific 790

heat capacity of exhaust gas is higher than that of air (as correctly stated on page 17). The only 791

factor which might contribute to a lower absolute heat capacity of the in-cylinder charge might 792

be a reduction of the overall in-cylinder mass due to higher temperature and consequently lower 793

density. However, the entire sentence on page 13 would make much more sense in my eyes if 794

it started: "Despite the recirculation of residual gases back to the cylinder could lead to a higher 795

specific heat..." [which would reduce the temperature increase obtained from compression]. 796

Please check this, maybe this is just a misunderstanding. 797

Thanks. This sentence has been corrected on Page 13 accordingly. 798

(7) Concerning the references to literature in combination with statements or interpretations of 799

your own investigation results, I fear you got me wrong. My point was simply to add (e.g.) ", 800

according to the findings of [47,48]" or something similar, just in order to distinguish between 801

your own findings and the publications you are referring to in order to substantiate your 802

interpretation of the results. I did not mean you have to change the references you cited in the 803

original version of the paper (so you could of course work with the previous references in case 804

you prefer these). 805

Thanks for the kind suggestion. Relevant modifications have been added to distinguish between 806

our own findings and the publications we are referring to. 807