11th north-west qualtech awards for excellence in quality · wastages and improve efficiency of...
TRANSCRIPT
11thNorth-West QualTech Awards Page 1
11th North-West QualTech AwardsFor Excellence in Quality
Project Title : To improve productivity of CEPS assembly line
Organization : ,
Executive summary
Since Lean Manufacturing System (LMS) was introduced in the Indian industries, peoplehave been looking for an effective “tool kit” to lead this program in own business andorganization. Many of the organizations started applying the principle of Lean to eliminatewastages and improve efficiency of manufacturing organization. Though the concept ofMUDA, MURI, MURA, 7QC tools , Design of Experiments & QC problem solving approach isknown to Indian manufacturing industries, but use of these strong tools & techniques forimproving production system has not yet gained popularity. With the introduction of LMS,XXXXXXXXXX has also introduced Lean Production as XXXXXXXXXXXXXX in its all plants.As we know that customer wish to pays only for value added activities and rest are thewastages. With this philosophy, business will be depend only on the value creation for thecustomer. LMS provide such tool which help organization to eliminate wastages and create“Lean Enterprises.” To remain in the business and be competitive in future everyorganization has to follow this proven philosophy of “Lean”.Our team worked on this philosophy as were facing a situation of “how to meet customerdemand without making investment on buying new machines & without investment for spacerequirement within short span of time” as volumes increased suddenly.Team worked very sincerely under the guidance & facilitation of expert seniors who havewide experience of lean manufacturing. With the cooperation & help of the otherdepartments like Kaizen shop, Maintenance deptt. Manufacturing Engineering deptt. etc.team succeeded to increases the production rate from XX no/hr to XX no/hr andstandardized it. By achieving this we were meet the customer demand without failure. Teammembers used extensive use of tools like- Videos, Time and motion study, XXX chart,Kaizens etc.
Team Leader
Author 1
Name : XXXXXXXXXX
Designation : JM-3
Tel : 0000000000
Email : [email protected]
11thNorth-West QualTech Awards Page 2
Team Members
Member 1
Name : XXXXXX XXXXXX
Designation : JM-2
Member 2
Name : XXXXXX XXXXXX
Designation : JM-1
Member 3
Name : XXXXXX XXXXXX
Designation : Associate
Member 4
Name : XXXXXX XXXXXX
Designation : Associate
Member 5
Name : XXXXXX XXXXXX
Designation : Associate
Member 6
Name : XXXXXX XXXXXX
Designation : Associate
Instructions:
Please fill only your text responses within the gray box provided under eachheading.
Do not paste tables, pictures or graphs in the response area. Please attach allsuch items as annexure with proper numbering system and attach the same inthe email along with the main project report.
We recommend that you avoid responding with only bullet points for every sub-head. Your input should be more like a narration.
You can use bullets where you need to list points.
The gray boxes are flexible can be resized to fit text.
Please do not change the formatting within the gray boxes. (The standard font isAerial with single spacing and the font size is 11pt)
Please ensure that all paragraphs should be left aligned (not justified)
Please ensure all annexures are cross referenced in the project report.
For each response, please mention the process and the tools used, whereverapplicable.
Please ensure that the total number of pages for the project report, inclusive ofannexure does not exceed 25 pages.
Besides soft copy on CD, three hard copies should be submitted on A4 size paperwith a 1 inch margin on all four sides. Soft copy should be compatible with MSWord-2010
All sections are not mandatory; sections marked # are optional.
11thNorth-West QualTech Awards Page 3
Organization’s Profile
Response: Response:(Approx. 100 words.)
OVERVIEW OF THE PROJECT
Response:1) Need of the Project: - We are the single source supplier of XXXX assembly to XXX for
one of their top selling model (XXX). Currently the demand is being cater through 2 shiftsper day with 90% of our capacity. Due to sudden increase in demand and increased futureprojections since April 2015 we have to run production in 3 shifts. This is increasing ourmanufacturing cost (power Cost + Manpower cost).
2) The Solution: - In order to avoid increasing of manufacturing cost & new investment, weare left with only solution to increase line capacity by reducing Neck Machine Cycle Time(NMCT).
3) Expected Results:- By reducing NMCT up to 11%, we expect to improve our line capacityby 9% to fulfill increase demand of customer in only 2 shifts.
1. IDENTIFYING THE PROJECT (Annexure-1,2,3,4,5,6,7)
1.1 Identifying the problem
a. What was the process used to identify and prioritize this problem?(Internal Rejection analysis, Audit reports, customer feedback, management reviews,
Business plans, Benchmarking with competition)
11thNorth-West QualTech Awards Page 4
Response:In F15, XXX assy. line capacity @ XX% efficiency on 2 shift basis was XXXXXX/year andactual customer demand was XXXXXX. But in F16 there was a sudden increase in customerdemand & future projections of F17 also increased further. In F16 customer demand jumpedto XXXXXXX/year & projections of F17 reflected as XXXXXXX/year which are more than theproduction capacity of XXX assy. line. So to meet the customer demand since April XX wewere running extra 3rd shift which was increasing power cost & manpower cost and affectingour manufacturing cost. (Annexure -1)
b. Why is it important to solve the problem now?
Response: Due to running 3rd shift, our manufacturing cost was increasing beyond targetwhich affecting our top line.(Annexure – 2)
c. How does the problem align with strategic goals of the organization?
Response: In our Business Strategy Increase Productivity is a key factor to Achieve HighProfitability (Annexure-3). As per our company and plant level KMI (Key ManagementIndices) growth in EBIDTA (Earnings Before Interest Tax Depreciation and Amortization) is animportant parameter which is directly affected by Power cost & Employee cost (Annexure-4).As per our policy 3rd shift is always kept spare to meet fluctuation in customer demand but inour case we were running continuously with the spare shift which was directly a factor toimposing a negative impact on the growth of EBITDA. Hence this problem is directly alignedwith strategic goals of the organization.
d. Problem/Opportunity Statement
Response:Our XXX assy. line customer demand increased suddenly which is more than our lineproduction capacity. Due to this we need to run line in 3rd shift which is against our plantstandard of running lines in 2 shifts. (Annexure-5)
e. Goal Statement
Response:To reduce line bottleneck cycle time (NMCT) from XX sec. to XX sec. to meet the customerrequirement in two shifts till XXth Nov-XX.(Annexure-6a, 6b)
f. High Level Process Flow Diagram
Response: Process flow diagram of XXX assembly is shown as attached in Annexure -7.
2. Data Collection (Annexure-1,8,6a,9,10,11,12,13,14,15,16)
2.1. Description of the data collection system used to measure current performance
Data collection plan
11thNorth-West QualTech Awards Page 5
Response: Following data were collected & analyzed.1. Customer Demand (Annexure-1)2. Line Layout (Annexure-8)3. Line cycle time at current efficiency. (Annexure -6(a))4. Line Organization Efficiency (LOE) (Annexure-9)5. Out of Balance Index (OBI) (Annexure -9)6. Processes step by step cycle time. (Annexure-10,11,12,13,14)7. NVA –Non value added activities8. VA -Value added activities
2.2. Data Analysis (Graphs, Pareto Chart, Histogram etc)
Response:1. Brainstorming2. Group discussion3. YAMAZUMI chart- Related to Manual cycle time balancing study. (Annexure-15)4.Time study (Annexure-10,11,12,13,14)5. Motion study (Annexure-16)
2.3. Quantification of baseline performance (Metrics depending upon project type (quality, Cost,delivery): Percentage, PPM, Defects per unit, Process Capability etc. Metrics for projectsrelated to delivery/cycle time; Process Map, Cycle time study, Value Stream Mapping,Overall equipment effectiveness)
Response:1. Current NMCT – XXsec.2. Current Production per Hour (PPH) – XXNOS.3. Line organization efficiency (LOE) – XX%4. Out of balance index (OBI) - XX%5. Line efficiency-XX%
3. DIAGNOSING THE CAUSES (Annexure-15,10,11,12,13,14,16)
3.1. Process for identification and prioritization of high level causes
a. Potential Causes: Fishbone diagram
Response: In our case we used the following tools to identify the potential causes.1. YAMAZUMI CHART (Annexure-15 )2. Process Sequence & Cycle time study of operators. (Annexure-10, 11, 12, 13, 14)3. Group Discussion.4. Motion Study. (Annexure-16)
b. Prioritization: Cause and effect matrix, or FMEA, or any other prioritization tool
Response: With the help of YAMAZUMI chart we could visualized & prioritized the work whichwere out of Balance Index. (Annexure-15)
11thNorth-West QualTech Awards Page 6
3.2. Root cause analysis methodology (Why-Why analysis, concentration charts, or any othermethod/s)
Response:1. Time study of manual work.2. Group discussion to identified the activities which can eliminate, reduce and overlap with
other activities. (Annexure-10,11,12,13,14)
3.3. Process for testing of theories/verification of root causes (GembaInvestigations/Observations, Hypothesis testing such as t- test, Chi-Square, ANOVA,regression or any other experimentation method/s)
Response:1. Gemba investigation and observations.2. Data collection
4. REMEDYING THE CAUSES (Annexure-17,18,19,20a,20b,21,10,11,12,13,14)
4.1. Process for identification and prioritization of possible solutions (Brainstorming, or creativitytools, Design of Experiment, Benchmarking or any other method/s)
Response:1. Identify & eliminating / reducing the Non value added activities through Kaizens
implementations. (Annexure-17,18,19,20a, 20b,21)
4.2. Process for choosing the best solution/s (Cost benefit analysis, evaluation matrix, or anyother method/s)
Response:1. Group discussion2. Matrix has made for judgment that which activity can eliminate, reduce or overlap with
other activities. (Annexure -10,11,12,13,14)
4.3. Process for validating that the solutions work
Response:Whatever the activities identified through judgment matrix , we did the actual demo & validatethat activities on Assy. Line.
5. IMPLEMENTING THE SOLUTION (Annexure-22)
5.1. Process for implementing the finalized solutions (Implementation plan, Project Managementtechniques or any other method)
Response:1. Activity Plan, (Annexure-22)2. Gemba kaizen done by CFT to achieve cycle time lower than takt time.3. Program in PLC modified to incorporate process sequence.
11thNorth-West QualTech Awards Page 7
5.2. How did you tackle resistance to change (Confidence building workshops,awareness/training or any other method)
Response:1. Line associates were involved in the improvement journey.2. They were given Group Kaizen Activity Trainings & 7 QC tools training.3. Trainings were given about YAMAZUMI chart & basics of ergonomics.4. Regular meetings of team members with facilitator.5. Full cooperation from other department like Maintenance & Kaizen departments.6. Equal hand holdings by management during the whole improvement journey.7. Associates made all handmade chart, pictures, sketches etc by themselves.8. Appreciation & awards to line associates & team after completion of project.
6. BENEFITS (Annexure-23)
6.1. Tangible
Response:1. Bottle Neck Machine Cycle Time (NMCT) is reduce from XXsec. to XXsec.2. Production per hour (PPH) increase from XX to XX nos.3. Eliminate the X shift.4. Cost is saved X% (X lac/annum).Annexure-23
6.2. Running expenses/investment, if any (#)
Response:These all improvements were done by the in-house facilities (Kaizen Department). Investmentis done less than approx. Rs. XXXXX (XXXXX Thousands only).
6.3. Intangible
Response:1. Understanding the concept & application of various tools.2. Strengthen team work.3. Confidence increase among people.4. Encouragement to other teams.
7. HOLDING AND SUSTAINING THE IMPROVEMENTS (Annexure-24)
7.1. Processes to ensure that the gains from the implemented improvements are sustainable(Control Plans, Control Charts, SOPs, Audits, or any other method)
Response:1. Standardized the work by updating Work standard quality control sheet (WSQC).2. Standardized the work element sheet (WES).3. Update the XX check sheet.4. Update the XXX XXXX check sheet.(Annexure -24)
11thNorth-West QualTech Awards Page 8
7.2. Plans for replicating gains in similar processes across other locations throughout theorganization
Response:Next project taken on XXX line to balance the manual work as attached. ( Annexure -25)
8. ANNEXURE LIST
Response:Annexure 1 :- Customer demand Yearly projectionAnnexure 2 :- Manufacturing costAnnexure 3 :- Business StrategyAnnexure 4 :- Plant XXXAnnexure 5 :- Demand vs. CapacityAnnexure 6a,6b :- Setting the target (6a),(6b)Annexure 7 :- High level of process flow diagram of CEPS Assy.Annexure 8 :- Line LayoutAnnexure 9:- Line Organization Efficiency, Out of Balance IndexAnnexure10 :- Step by step cycle timeAnnexure11 :- Step by step cycle timeAnnexure12:- Step by XXXXX timeAnnexure13:- Step by step cycle timeAnnexure14:- Step by step cycle timeAnnexure15:- Yamazumi chartAnnexure16:- Motion studyAnnexure17:- Implementing the solutionAnnexure18:- Implementing the solutionAnnexure19:- Implementing the solutionAnnexure20a,20b:- Implementing the solution(20a),(20b)Annexure21:- Implementing the solutionAnnexure22:- Activity planAnnexure23:- BenefitsAnnexure24:- Holding & sustaining the improvementsAnnexure25:- Future plan
11thNorth-West QualTech Awards Page 9
Annexure-1 : Customer Demand Yearly projection
Customer Demand Yearly ProjectionsNumbers
908070605040302010
CapacityXXXXX @XXX%
XXX
F-15 (ActualDemand)
XX % increasefrom F15 to F17.
XXX
F-16 (ProjectedDemand)
XXX
F-17 (ProjectedDemand)
Annexure-2 : Manufacturing Cost
Rupees Manufacturing Cost1101009080706050403020
10
XXXXX
Saving XXXX(XXX%).
XXXXXX
F-15 F-16 (After Project completion)
11thNorth-West QualTech Awards Page10
Annexure-3: Business Strategy
Achieving highprofitability.
An organization ofenergized & involvedemployees.
BusinessStrategy
Supplying to majorAutomotive OEMs inIndia.
Overseas export ofthis plant products.
An organization ofenergized &involved employees.
Develop futureleaders throughtrainings & skills.
Achieving highprofitability.
Reduce/Eliminate Losses.
Supplying to majorAutomotive OEMsin India.
CompetitivePrice.
Overseas export ofthis plant
BrandingProducts.
Drive passion byengaging themin theimprovement
Boost motivationby recognition &rewards.
IncreaseProductivity
Develop newproduct lines.
Win customertrust &confidence.
Cutting edgetechnology.
Associatedpartnership withOEMs.
Concurrentdevelopment ofsuppliers.
Internationallycompetitiveinnovation.
Identify NicheMarkets.
DevelopingChannelPartners.
11thNorth-West QualTech Awards Page11
Annexure-4 : Plant XXX
Annexure-5: Demand Vs. Capacity
11thNorth-West QualTech Awards Page12
Annexure-6: Setting the Target (6a)
Cycle Time Requirement at XX% EfficiencySeconds46
XX45
44
43XX
42XX
41
40F-15 (At present) F-16 (Requirement @
2 shifts)F-17 (Requirement @
2 shifts)
Annexure-6: Setting the Target (6b)
Seconds Target Setting of NMCT at XX% efficiency46
XX45
44
43
42
41XX
40
39
38
37Current NMCT
XXXXTarget NMCT15th XXX
11thNorth-West QualTech Awards Page13
Annexure-7: High Level Process Flow Diagram of CEPS AssemblyConveyor
Annexure-8: Line LayoutCEPS Inspection. Line-1
Matl.OUT
FGTrolley
final ASSY Fitmentinsp. &motornoise
HandTapping
Noisechecking
FeelingInspection
Rotationaltorqueinsp.
ColumnNoise
checking
Over Allinspection
ImpactTesting
Deburring &Crimping
Balancingmachine
Bottle neck operationCycle time-XXXX. Bottle neck operation
Cycle time-XXXX.
Matl.IN
NeedleBearingPressing
CoilAssy
C Ringpressing
Soldering andPCB cover
Inner jkt.pressing
Ball Brg.Pressing
Capsulefitment
Outer jacketpressing
GeneralAssembly
Motorattachment
Detection ringpressing
Common CEPS assembly line
CEPS Inspection Line-2
Matl.OUT
Final Assy Motor Noise &FitmentInspection
HandTapping
FitmentInspection
FeelingInspection
Column NoiseInspection & PCB Cap
Attachment
OverallInspection
ImpactInspection
Deburring &Crimping
Balancing M/c
Bottle neck operationCycle time-XXXX.
11thNorth-West QualTech Awards Page14
Annexure-9: Line Organization Efficiency (LOE), Out of Balance Index (OBI)
Line organization efficiency (LOE)=Total no. ofoperators
∑CT
× Bottle NeckCycle time
× 100
XXX=
XX × XX× 100
= XXX%
LOE should be >XX% (As per XXXXX standard)
Out of balance Index (OBI) =
Bottle NeckCycle time ×
∑CT
Total no. ofoperators ∑CT
× 100
XX x XX=
XXX
XXX
× 100
= XXX%
OBI should be <XX% (As per XXXXX standard)
Annexure-10 : Step by Step Cycle Time
50Net Cycle Net Cycle XX XX
XX XX
40 time-XX
30XX XX
time-XXXX
XXXX
XX XX XX Manual CT
20XX XX
10
0
Auto CT
0 0
OPT-1 OPT-2 OPT-3 OPT-4 OPT-5 OPT-6 OPT-7 OPT-8
11thNorth-West QualTech Awards Page15
Annexure-11 : Step by Step Cycle TimeActivity
No.Machine
No.Descriptions
Time(sec.)
B-17
1
B-17
Start the cycle X
XX
2Pick the 'O' Ring & Rocket , put on motor shaft &insert the ring through Rocket
X
3Pick the motor & put on XXXX. By adjusting both GearTeeth
X
4 Connect the motor connector in female connector X
5Pick two bolts from bolt dispenser & tight manuallytwo to three thread
X
6 Tight the bolt by Torque Wrench X
7Marking two tight bolts by black marker forconfirmation of tightening
X
8 Keep the components X
Total Cycle time of operator XX
Annexure-12 : Step by Step Cycle TimeActivity
No.Machine
No.Descriptions Time
(sec.)Total Cycle
time1
B-16
Cut the packing of worm housing by cutter & removefrom packing
X
XX
2 Put the worm XXX. on fixture & check the torque X
3Pick the detection ring & check crimping condition,put on fixture
X
4 Put the worm XXXX. on fixture X
5 Press cycle start X
6 Walking for motor greasing X
7 Pick the motor from bin & put on stand X
8Pick the greasing stick & take grease from greasecontainer by stick
X
9Apply the grease on motor serration by rotating themotor
X
10 Return the Station X
Total cycle time of operator XX
11thNorth-West QualTech Awards Page16
Annexure-13 : Step by Step Cycle TimeActivity
No.Machine
N0. DescriptionsTime(sec.)
Total Cycletime
1
B-16
Pick the Worm XXXX. & put on XXXXX stand X
XX
2 Pick the greased worm XXXX. & put on XXXXX pad X
3 Press both clamping pad X
4 pick the middle shaft X
5 Check the middle shaft under magnifying glass, X
6 Put lower bracket X
7 Pick two bolts X
8 Fasten bolts manually & tight by Torque Wrench X
9Mark two tight bolts by black marker forconfirmation of tightening
X
10 Keep comp. on stand X
Total Cycle time of operator XX
Annexure-14 : Step by Step Cycle TimeActivity
No.Machine
No.Descriptions Time
(sec.)TotalCylcle
1 Pick the capsule & put on Fixture X
2 Pick the Outer Jacket & put on Fixture X
3 A-14 Pick the horn earth and Retainer & put on Fixture X XX
4 Press both Cycle Start X
5 Check & mark the Capsule & retainer pressing parts X
6Walk & pick the inner jacket sub assy from conveyor
X& back to outer jacket pressing machine
7 Apply oil on inner jacket sub assy. X
8 Put the comp. on lower Fixture X
9 A-16 Put the Outer Jkt on Upper locator X XX
10 Press both Cycle Start X
11 Mark the pressed component X
12 Pick retainer & insert inside the tube & return XTotal Cycle time of operator X
11thNorth-West QualTech Awards Page17
Annexure-15 : XXXXX ChartXXXXX chart (Only Manual time) of common CEPS assembly line
50 Sec.
45
TARGET LINE – XXX.
XX XXXX XX
OPT-5 to OPT-8 havemore manual work
40XX
35XX
30 XX XX
25
20
M\C No.15 B-12
M\C No.B-03
M\C No.A-35
M\C No.A-12
M\C No.A-16
M\C No.B-16
M\C No.B-17
M\C No.A-17
MANUAL TIME
NMCT
10
M\C No.5 C-85
M\C No.A-15
M\C No.A-14
0OPT-1 OPT-2 OPT-3 OPT-4 OPT-5 OPT-6 OPT-7 OPT-8
Manual Cycle time of Operator 1 to 8
11thNorth-West QualTech Awards Page18
Annexure-20a : Implementing the solutionAnnexure-18 : Implementing the solution
XXXXXXXXXXXXXXX KAIZEN IDEA SHEET
Line / Area : CEPS Assy. M/C No./ ProcessName :
B-17Motor attachment
Date ofidentification XX.10.XXXX
Name of Suggestor:
XXXXXXXXXXXXX
Location : CEPS Assy line-1Date ofimplementation XX.10.XXXXX
Before After
Before situation:
Need to bend the wire harness of motor during connection infemale connector.
After situation:XXXXXXXXXXXXXXXXXXXXXX
Benefits: 1. Cycle time is reduced XXX seconds to XXX seconds.2. Operator XXXX is reduced.
11thNorth-West QualTech Awards Page19
Annexure-20a : Implementing the solution
CEPS line-1
General Assy station.B-16
Bottle neckmachine of line
Moulding machineC-72
Middle shaft line
Straighteningmachine(B-67)
Cycle time- XXXsec.
1
Cycle time-XXXsec.
Middle shaft inspection ongeneral assy. station.
2
Cycle time- XX sec.
Torsion bar pressingmachine
B-25
Activity :-Check the middle shaft under the magnifying glass.
Annexure-20b : Implementing the solution
Sona Koyo Steering Systems Ltd.KAIZEN IDEA SHEET
Line / Area : CEPS M/C No./ ProcessName :
General Assy.B-16
Date ofidentification XX-10-20XX
Name of Suggestor:
Mahesh,Sunil, ManeshSurender, Ajay,Priyanka,Sanjeev
Location : Front SideDate ofimplementation XX-10-20XX
Before After
Before situation:
Middle shaft inspection with XXXXXXX done atgeneral assy. station
After situation:
XXXXXXXXXXX
Benefits :This activity cycle time eliminate XX second to XXX.
11thNorth-West QualTech Awards Page20
Annexure-21 : Implementing the solution
XXXXXXXXX. KAIZEN IDEA SHEET
Line / Area : CEPS Assy. M/C No./ ProcessName :
A-16Outer Jacket
Date ofidentification XX.10.20XX
Name of Suggestor:
XXXXXXLocation : CEPS Assy line-1
Date ofimplementation XX.10.20XX
Before After
Before situation:
Operator movement XX feet to pick theinner jacket sub assy.
After situation:XXXXXXXX
Benefits : Cycle time reduced XX seconds to XX seconds.
Annexure-22 : Activity Plan
S.No. Activities Sept.XXPeriodOct.XX Nov.XX
WK-3 WK-4 WK-1 WK-2 WK-3 WK-4 WK-1 WK-2
1 Select Topic
2 Understand The situation P
3 Set Target
4 Analyze causesD
5 Consider and implement Countermeasures
6 Check Results C
7 Standardize and astablish Control A
11thNorth-West QualTech Awards Page21
2. JH check sheet updated.
4. Work element sheet updated.
Productivity XX
XX
92
Annexure-23 : BenefitsNos./Hrs.
Sec.46
44
42
40
38
36
XX NMCT 90888684
XX 8280787674
Before After Before After
No. of Shift.76543210
C Shift Eliminate
XX
XX
0000
0000
0000
0000
0000
0000
0
Rs..Cost Saving
XXXXTotal Cost Saving= XXXX Rupees/Year.
XXXX
Before After Manpower Cost Energy Cost
Annexure-24 : Holding and Sustaining the Improvements1. Line SWC updated.
3. Poke yoke map updated.
11thNorth-West QualTech Awards Page22
Annexure-25 : Future Plan
Sec.45
Line balancing tobe improve byJune-XX
CYCLE TIME
XXXX
40
XX XX
35XX
NMCT TARGET
XX
30 XXXX
25
20OPT-1 OPT-2 OPT-3 OPT-4 OPT-5 OPT-6 OPT-7 OPT-8
Manual work is not balance of operator XX to XX. So next project is taken to balance themanual work of these stations.