75 kw microturbine chpbare

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Combined Heat and Power Application of a 75-kW Microturbine at a Toronto Laboratory: Monitoring Results Brian Boyd Technology Directorate of PWGSC 2001

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Page 1: 75 KW Microturbine CHPbare

Combined Heatand Power Application of a

75-kW Microturbineat a Toronto Laboratory:

Monitoring Results

Brian BoydTechnology Directorate of PWGSC

2001

Page 2: 75 KW Microturbine CHPbare

Outline of presentation

• Project Description

• Equipment

• Funding Partners

• Site Description

• Reason for Doing the Project

• Project Chronology

• Summary Figures

• Conclusions

Page 3: 75 KW Microturbine CHPbare

2301 Midland Avenue, Scarborough has the first Canadian installation of a micro-turbine supplying electricity and waste heat to a building. The gas-fired unit was intended to operate continuously, providing 75 kW electric and 155 kW thermal heat. Natural gas consumption by the building’s boilers has been reduced by the application of recovered heat to space heating systems in winter and humidity control systems in summer.

Project Description75 kW Microturbine CHP Application

Page 4: 75 KW Microturbine CHPbare

2301 Midland Avenue, Scarborough

Project Description

Page 5: 75 KW Microturbine CHPbare

Parallon 75

Equipment

Honeywell International Inc.

Page 6: 75 KW Microturbine CHPbare

Parallon75

Page 7: 75 KW Microturbine CHPbare

Parallon 75

Honeywell International Inc.

Page 8: 75 KW Microturbine CHPbare

Parallon 75Honeywell Power Systems

Canadian Distributor:Mercury Electric Calgary, AB

Features:

• 75-kW gas-fired microturbine• No gearbox• A recuperator• Low NOx emissions in exhaust

Local support was provided by the local Honeywell group.

Equipment

Page 9: 75 KW Microturbine CHPbare

MicoGenHeat Recovery System

Unifin International, London, ON

This Canadian designed and fabricated heat recovery system increases the system’s overall efficiency by recovering the heat in the turbine’s exhaust and using it to heat hot water for space heating in the winter and humidity control in the summer. The heat supplied reduces the natural gas used in the building’s boilers.

Equipment

Page 10: 75 KW Microturbine CHPbare

The MicoGen combined heat & power system reduces the need for design engineering, leaving only application and installation considerations. The heat supplied reduces the natural gas used in the building's boilers.

Further information on the equipment is available at the Unifin web site.http://www.unifin.com/micogen.htm

Equipment

Page 11: 75 KW Microturbine CHPbare

The building computer recorded the net outputs while various other parameters were logged by a computer connected to the turbine.

The average measured electrical output of the turbine after it’s internal power needs are subtracted (such as fans and compressors) came to 68.4 kW during the half year of its operation.

Due to design problems the heat recovery system used only 62.4 kW of waste heat on average.

Output During Operation:

Honeywell International Inc.

Page 12: 75 KW Microturbine CHPbare

75 kW Microturbine CHP Application

Funding PartnersThe costs of the installation were shared among:• PWGSC CAN$ 143 K• NRCan CAN$ 66 K • Enbridge Consumers Gas CAN$ 50 K• Kinectrics CAN$ 30 K( formerly Ontario Hydro Technologies )

CAN$ 104 K of which went to the contractor, VESTAR.

CAN$ 77 K was the price of the turbine.

Page 13: 75 KW Microturbine CHPbare

Item ActualCost (C$)

100%Hindsight

50th

InstallationSpecificCost $/kW

Turbine 70,900 70,900 70,900 945

CHP unit 13,065 15,800 11060

Mechanical 19,425 19,330 17,330 378

Electrical 4,755 4,755 4,255

Civil 11,377 7,940 5,540 131

Metering 9,820 9,820 6,820 91

ConsultingEngineering

21,751 12,000 8,448

ProjectMangement

42,542 24,336 8,884 232

TOTAL 193,635 164,882 133,287

$/kW 2581 2198 1777 1777

Cost Breakdown Source: NRCan

Page 14: 75 KW Microturbine CHPbare

Cost Breakdown Source: NRCan

TurbineHeat RecoveryCivil/ElectricalMetering

Assuming 110 kW heat recovery, this investment has less than a 1 year payback

This is where the maincost reduction has to come

Page 15: 75 KW Microturbine CHPbare

Funding Partners

The Technology Directorate of PWGSC originally obtained funding from the Program for Energy Research and Development (PERD) and later through the Technology Development & Transfer (TD&T) Program.

The installation was done by VESTAR as a design-build through a contract with PWGSC, Technology (E. Morofsky, Project Manager).

Page 16: 75 KW Microturbine CHPbare

Site Description

Site selection:The building requirements were to be such as to continuously have a need for at least 155 kW heat and 75 kW electricity. The installation was to be monitored and evaluated for 18 months.

Page 17: 75 KW Microturbine CHPbare

2301 Midland Avenue, Scarborough

Site Description

Page 18: 75 KW Microturbine CHPbare

Site Description

Building Host:Health Canada Laboratory Building@ 2301 Midland Avenue3-story buildingapproximate altitude of 600 ft.

The building has also recently undergone a FBI (Federal Buildings Initiative) project that reduces its energy consumption by 50% through more efficient lighting, controls and a conversion of the constant volume ventilation to a variable volume system. (Retrofit done by Vestar, an energy services company supplying third party financing.)

Page 19: 75 KW Microturbine CHPbare

Site Description

The Building Operator:PWGSC - Ontario RegionRick SchveighardtFacility ManagerHealth Protection Branch - Health Canada2301 Midland Avenue, Scarborough, ONM1P 4R7CanadaTel: (416) 512-5667E-mail: [email protected]

Page 20: 75 KW Microturbine CHPbare

Site Description

Enclosure

Concrete Pad

Fuel Transformer

Heat Rec. Unit

Turbine

H2O

Gas Meter

Sloped lines on water loop

Page 21: 75 KW Microturbine CHPbare

Site Description

Enclosure

Concrete Pad

FuelPower

Page 22: 75 KW Microturbine CHPbare

Reasons for doing the projectBenefits of CHP (CombinedHeat and Power) microturbines:

- Reduction of greenhouse gas production

- Potential energy cost savings

- Versatility and stand-alone capability

- Possibility of selling power back to grid

75 kW Microturbine CHP Application

Page 23: 75 KW Microturbine CHPbare

Reasons for doing the project

Microturbines are used successfully in oilfields and it was suggested that they might be useful for providing supplementary or back-up power to buildings. The partners decided they wanted to gain experience in the field of turbine co-generation while exploring the feasibility of the suggested application. The Midland Rd. site is ideal since it is a lab and has a high power demand year-round, including a use for heated water.

Page 24: 75 KW Microturbine CHPbare

Net Present Value of Microturbine Savings (Office Building)

($600,000)

($500,000)

($400,000)

($300,000)

($200,000)

($100,000)

$0

$100,000

$200,000

$300,000

$400,000

$500,000

$600,000

$700,000

$800,000

$900,000

15 17 19 21 23 25 27 29 31 33 35 37 39 41 43 45

Average Natural Gas Cost (¢/m 3)

Ne

t P

res

en

t V

alu

e o

f S

av

ing

s (

$)

4 5 6 7 8 9 10 11 12

Average Natural Gas Cost ($/GJ)

15 cents/kWh

14 cents/kWh

13 cents/kWh

12 cents/kWh

11 cents/kWh

10 cents/kWh

9 cents/kWh

8 cents/kWh

7 cents/kWh

6 cents/kWh

5 cents/kWh

4 cents/kWh

3 cents/kWh

Generation Efficiency: 30%Location: OttawaDiscount Rate: 7%

Av

era

ge

Ele

ctr

icit

y C

os

t- I

nc

lud

ing

De

ma

nd

Reasons for doing the project

Source: PWGSC study All values in Canadian Funds

Page 25: 75 KW Microturbine CHPbare

To obtain performance and operating experience with a Microturbine Combined Heat and Power system at the Health Canada Laboratory at 2301 Midland Road at high efficiency and low exhaust emissions compared to other fossil fuel generation power plants.

Project ObjectiveCETC DISTRIBUTED GENERATION PROGRAM

Page 26: 75 KW Microturbine CHPbare

• April 12, 2000 – Equipment Delivery (originally planned for September 30, 1999)

• June 9, 2000 – Commissioned (originally planned for October 30, 1999)

• November 7, 2000 – Unit shut down pending ETS Field Certification

• June 9, 2000 - November 7, 2000 – Availability: 60%

• Gas compressor and core replaced after 2000 hours of operation

• January, 2001 – Monitoring Underway (originally planned for November 30, 1999)

• January 4 – Emissions Testing

• January 26 – A minor gas leak was detected by Enbridge and repaired by Honeywell.

• February 5 – Versatech (mechanical contractor) replaced the bottom flange of gas meter and installed a flexible connector to the cogeneration unit.

• February 6 – Vestar restarted the co-gen unit at 10:30 a.m. Logging was restarted at 12:00 noon (after 2614 hours of operation).

• February 8 – Turbine stopped at 2 p.m.

Project chronology: 2000 - 2001

Page 27: 75 KW Microturbine CHPbare

• February 9 – Enbridge found the unit had been off for an unknown amount of time with the fault light lit. The key was turned from the normal position to the off position.

• February 15 – Honeywell checked the unit and started it up at 1 p.m.

• March 7 – Kinectrics turned the microturbine off briefly to install a power quality meter for a test. The power level was measured at 75kW.

• March 14 – Honeywell performed a retrofit on the plenum sealing and fan hub upgrade.

• March 27 – Honeywell fixed a leak on the outlet of the flex line to the ASCO solenoid and added 500ml of oil to the gas compressor, then got the unit up and running but it stopped at 4 p.m.

• March 29 - Turbine restarted at 12 p.m.

• April 6 – The computer was found off; the data may not be good.

• April 6 – The computer was found off; the data may not be good.

• April 23 – Honeywell attempted an efficiency test but the unit shut itself down after 8:30 a.m. and the test was delayed.

Project chronology: 2001

Page 28: 75 KW Microturbine CHPbare

• April 24 – Honeywell suspects the shut-down is due to an ignitor which will be replaced.

• May 9 – Honeywell installed the new ignitor and a new inlet air filter. The cooling module oil was found to be leaking and the unit was shut back down.

• June 7 – Honeywell replaced the cooling module and the unit was running again by 4:00 p.m.

• June 15 – Enbridge found the fault light flashing on the unit but it was left running until it switched off on its own at 8 a.m.

• June 25 – Honeywell added 350ml of oil, checked for faults then switched the unit back on at 12 p.m.

• June 28 – The fault light was flashing.

• June 30 – At approximately 11 p.m. the gas meter’s first erratic reading is recorded.

• July 6 – The fault light had switched off by itself.

• July 11 – At approximately 11 p.m. the increasingly erratic gas meter stops reading gas flow altogether.

Project chronology: 2001

Page 29: 75 KW Microturbine CHPbare

Project chronology: 2001• July 18 – The unit switched of at 5 a.m.

• July 20 – The unit was found off with the fault light on, and the unit would not restart.

• July 24 – The unit is still off, the oil was topped up and the filters drained before restarting at 12 p.m.

• July 27 – The Unit was running O.K.

• August 9 – At start up, there was a flashing red light but no obvious fault. 500ml of oil was added. The filters were cleaned. Unit seemed to be running fine. The reclaimer damper linkage was disconnected and wired open.

• August 15 – The unit switched itself off at 5 a.m.

• August 17 – The unit was found off with the fault light steadily lit.

• August 24 – The unit was still off and waiting to be serviced.

• August 31 – The unit was checked but left off.

• September 7 – The unit was still off.

• Honeywell has since recalled all its microturbine units.

Page 30: 75 KW Microturbine CHPbare

2001 Performance Summary

• The microturbine logged 2939 hours in 2001 for a total of 5553 hours of operation at final shut down.

• From the February power up until the August shut down the unit had an overall availability of 64.55 %

• Typical values under steady running conditions :– natural gas consumption 1000 std.cubic feet / hour or 269.6

kW (LHV)

– 26 % turbine efficiency @ ~70 kW power output

– 30 % heat efficiency @ ~80 kW heat output

• Overall averages:– power output: 68.4 kW– heat output: 62.4 kW

• Inverter, transformer, and parasitic losses: 5 kW

Page 31: 75 KW Microturbine CHPbare

2001 Performance Summary

• Estimated Parasitic Losses: 1.4 -1.6 kW (fans, fuel compressor)

• Thermal Performance:– Large thermal losses due to enclosure cooling air blowing

over and through silencer system.– Good heat balance obtained around Unifin heat recovery

system. The problem is the approach temperature is not the 250° C expected but 191 ° C

– Likely fix will involve insulating duct from recuperator discharge; need to avoid restricting enclosure cooling flow which is significant

• Average gas properties over test period: – HHV 1012.6 Btu/CuFt (0.2965 kWh/CuFt)– LHV 920.55 Btu/CuFt (0.2696 kWh/CuFt)

Page 32: 75 KW Microturbine CHPbare

Febru

ary

Mar

chApr

il

June

July

Augus

t

Septe

mbe

r

May

-20

-10

0

10

20

30

40

0.5 1 1.5 2 2.5 3 3.5 4 4.5 5 5.5 6 6.5 7 7.5 8

Month

Tem

per

atu

re i

n D

eg.

Cel

ciu

s

Max. Temp. deg. CAvg. Temp. deg. CMin. Temp. deg. C

Temperature

Page 33: 75 KW Microturbine CHPbare

February

March

April

June

July

August

SeptemberMay0

10

20

30

40

50

60

70

80

90

100

0.5 1 1.5 2 2.5 3 3.5 4 4.5 5 5.5 6 6.5 7 7.5 8

Month

Per

cen

t A

vail

abil

ity

Availability

Page 34: 75 KW Microturbine CHPbare

Meter Output

0

200

400

600

800

1000

1200

15-Feb 17-Feb 19-Feb 21-Feb 23-Feb 25-Feb 27-Feb 1-Mar

Cu

bic

Fe

et

Na

tura

l G

as

0

100

200

300

400

Kil

ow

att

s

STD CuFt/HrFuel Rate in kWBtu Meter (kW)Power Out (kW)

Page 35: 75 KW Microturbine CHPbare

Performance and Temperature

0.00

5.00

10.00

15.00

20.00

25.00

30.00

35.00

40.00

15-Feb17-Feb

19-Feb21-Feb

23-Feb25-Feb

27-Feb1-M

ar

Per

cen

t E

ffic

ien

cy

-20

-10

0

10

20

30

40

Ou

tdo

or

Tem

per

atu

re (

deg

. C

)

Heat Efficiency (%)Turbine Efficiency (%)Outside Temp. (deg C)

Page 36: 75 KW Microturbine CHPbare

Hourly Net Heat Rate Btu / kWh (HHV)(based on hourly power and heat rates)

0

1000

2000

3000

4000

5000

6000

7000

8000

9000

10000

15-Feb 17-Feb 19-Feb 21-Feb 23-Feb 25-Feb 27-Feb 1-Mar

Btu

/ k

Wh

(H

HV

)

Page 37: 75 KW Microturbine CHPbare

75

271

84

GAS

HEAT

37

POWER

191 CLOSSES

STACKLOSSESto ambienttemperature

Heat Balance 4th January0°C Ambient ( all data in kW)

75

91C

70

Page 38: 75 KW Microturbine CHPbare

Emission Testing January 4th

Page 39: 75 KW Microturbine CHPbare

Performance Summary

Preliminary Emission Results (g/kWh)

75 kW 50 kW 25 kW

NOx 1.704 1.2168 1.296

CO 2.352 23.904 85.392

THC 0.0384 2.916 5.5152

Source: NRCan

Page 40: 75 KW Microturbine CHPbare

Performance Summary

Emission Data (dry ppm)

75 kW 50 kW 25 kW

NOx 28.4 15.1 8.8

CO 63.9 488 952

THC 1.9 104.1 107.5

Source: NRCan

Page 41: 75 KW Microturbine CHPbare

• The heat recovery was lower than expected (62.4 vs 155 kW) due to thermal losses on uninsulated parts of the recuperator and a reduced thermal output in winter.• The heating circuit design was a success using water instead of glycol in an outside freezing environment.• The noise issue, which had originally concerned the building operator, proved not to be a problem.• The emission data was found to be within specifications.

Conclusions

75 kW Microturbine CHP Application

Page 42: 75 KW Microturbine CHPbare

Conclusions

The gas compressor caused problems because it was not registered with the local fuel safety organization and was noisy and unreliable.

Is the installation economic and how many buildings are suitable for microturbine application?

Many aspects of the installation at Midland Avenue would be done differently if we had a second chance. Most of these were due to inexperience with installing and operating a microturbine at a building site. We will be analyzing these issues and recommending standard installation procedures.

Page 43: 75 KW Microturbine CHPbare

The Health Canada Laboratory is not a typical building but other building types where clients require highly reliable power or dependable standby power with strict dehumidification requirements are potential applications. This would include laboratories, museums, computer facilities and 24/7 operations, and office buildings with alternate cooling needs.

Conclusions