acidising case study – kawerau injection wells · yoong wei lim 1, malcolm grant2, kevin brown3,...

6
PROCEEDINGS, Thirty-Sixth Workshop on Geothermal Reservoir Engineering Stanford University, Stanford, California, January 31 - February 2, 2011 SGP-TR-191 ACIDISING CASE STUDY – KAWERAU INJECTION WELLS Yoong Wei Lim 1 , Malcolm Grant 2 , Kevin Brown 3 , Christine Siega 1 and Farrell Siega 1 1 Mighty River Power, 283 Vaughan Road, Rotorua, New Zealand 2 MAGAK, 208D Runciman Road, RD2 Pukekohe 2677 New Zealand 3 GEOKEM, P.O. Box 30-125, St Martins, Christchurch, New Zealand e-mail: 1 [email protected]; ABSTRACT Brine at the Kawerau Geothermal Limited (KGL) plant was injected into three injection wells (KA43, KA44 and PK4A). Since plant commissioning, the capacity of the wells declined to the point where well intervention was necessary to avoid loss of generation. Investigative work was initiated with multi-rate injection tests which found that the injection index of the wells had declined significantly to approximately half of pre-utilisation levels. Further geochemistry analysis identified that the most likely source of injectivity decline was scaling due to colloidal silica forming in the formation. KA44 and PK4A were acidised using a standard 10% hydrochloric acid pre-flush followed by a 10%:5% HF:HCL mud acid solution. A 2” coil tubing unit with a 5 hole 45º nozzle bottom hole assembly was used giving a maximum pump rate of 3.5 - 4.0 barrels per minute. Feedzones were acidised one at a time starting with the deeper zones. Post well injection tests identified that the acidising had recovered the injectivity of the deeper feedzones but the shallower feedzones remain blocked with scale. The injectivity index at PK4A improved from 50 t/h.b to 84 t/h.b while KA44’s gross injectivity index increased from 25 t/h.b to 50 t/h.b. Camera runs carried out before and after acidising revealed excellent scale removal from the perforated liners. Pre and post acidising High Temperature Casing Corrosion (HTCC) logs also showed that the acid had not caused any measurable corrosion in the casings. INTRODUCTION Three injection wells (KA43, KA44 and PK4A) were used to inject brine from the Kawerau Geothermal Limited (KGL) plant (Figure 1) since plant commissioning in August 2008. Figure 1: Location of the Kawerau Geothermal Field Silica precipitation at Kawerau has been a concern since the design phase as the silica saturation index (SSI) is approximately 1.9 at injection temperature. To prevent deposition, an acid inhibition system (or pH modification) was installed at Kawerau (Horie 2009). Since plant commissioning, routine monitoring of the wells identified declines in the well capacity. Subsequent investigative work was initiated to confirm declines and identify the root cause. INVESTIGATIVE WORK As an initial step in the investigation, multi-rate injection tests were carried out on all three wells and identified that the injectivity indices had declined to

Upload: buiduong

Post on 22-Aug-2019

215 views

Category:

Documents


0 download

TRANSCRIPT

Page 1: Acidising Case Study – Kawerau Injection Wells · Yoong Wei Lim 1, Malcolm Grant2, Kevin Brown3, Christine Siega and Farrell Siega1 1 Mighty River Power, 283 Vaughan Road, Rotorua,

PROCEEDINGS, Thirty-Sixth Workshop on Geothermal Reservoir Engineering Stanford University, Stanford, California, January 31 - February 2, 2011 SGP-TR-191

ACIDISING CASE STUDY – KAWERAU INJECTION WELLS

Yoong Wei Lim1, Malcolm Grant2, Kevin Brown3, Christine Siega1 and Farrell Siega1 1 Mighty River Power, 283 Vaughan Road, Rotorua, New Zealand

2 MAGAK, 208D Runciman Road, RD2 Pukekohe 2677 New Zealand 3 GEOKEM, P.O. Box 30-125, St Martins, Christchurch, New Zealand

e-mail: 1 [email protected];

ABSTRACT

Brine at the Kawerau Geothermal Limited (KGL) plant was injected into three injection wells (KA43, KA44 and PK4A). Since plant commissioning, the capacity of the wells declined to the point where well intervention was necessary to avoid loss of generation. Investigative work was initiated with multi-rate injection tests which found that the injection index of the wells had declined significantly to approximately half of pre-utilisation levels. Further geochemistry analysis identified that the most likely source of injectivity decline was scaling due to colloidal silica forming in the formation. KA44 and PK4A were acidised using a standard 10% hydrochloric acid pre-flush followed by a 10%:5% HF:HCL mud acid solution. A 2” coil tubing unit with a 5 hole 45º nozzle bottom hole assembly was used giving a maximum pump rate of 3.5 - 4.0 barrels per minute. Feedzones were acidised one at a time starting with the deeper zones. Post well injection tests identified that the acidising had recovered the injectivity of the deeper feedzones but the shallower feedzones remain blocked with scale. The injectivity index at PK4A improved from 50 t/h.b to 84 t/h.b while KA44’s gross injectivity index increased from 25 t/h.b to 50 t/h.b. Camera runs carried out before and after acidising revealed excellent scale removal from the perforated liners. Pre and post acidising High Temperature Casing Corrosion (HTCC) logs also showed that the acid had not caused any measurable corrosion in the casings.

INTRODUCTION

Three injection wells (KA43, KA44 and PK4A) were used to inject brine from the Kawerau Geothermal Limited (KGL) plant (Figure 1) since plant commissioning in August 2008.

Figure 1: Location of the Kawerau Geothermal Field Silica precipitation at Kawerau has been a concern since the design phase as the silica saturation index (SSI) is approximately 1.9 at injection temperature. To prevent deposition, an acid inhibition system (or pH modification) was installed at Kawerau (Horie 2009). Since plant commissioning, routine monitoring of the wells identified declines in the well capacity. Subsequent investigative work was initiated to confirm declines and identify the root cause.

INVESTIGATIVE WORK

As an initial step in the investigation, multi-rate injection tests were carried out on all three wells and identified that the injectivity indices had declined to

Page 2: Acidising Case Study – Kawerau Injection Wells · Yoong Wei Lim 1, Malcolm Grant2, Kevin Brown3, Christine Siega and Farrell Siega1 1 Mighty River Power, 283 Vaughan Road, Rotorua,

approximaNon- lineatests sugge Table 1:

Well OII

KA43 KA44 PK4A The declinperformancproblems, square roo2. The injesame timeinjection w

Figure 2stimulationwaste wate Not only dof increasdeclined. Brine wasstainless stwellhead. microscopeprecipitatesmall amosilica. Thelarger amcompositio

ately half of prear injectivity westing restrictio

Comparisonperformance a

Original I (t/h/b) II a

45 97 100

ne in injectivce elsewhere. injectivity shou

ot of the time iectivity is highe injecting, a

whereas the wa

: Injectivty n with cold waer.

did the Kaweraing injectivity

s also filtered teel filter at th

An environe (E-SEM) was. The LP sep

ount of debris e injection welmount of ons similar to th

e-utilisation lewas also obseon at the well fa

n between oand July 2009 II as of July 2

at low rate 13 45 42

vity is in coIn the absenceuld increase ronjecting, as sh

her under stimuas cold waterste water is ho

history of Rter and under

au wells not foy with time,

through a Swhe LP separatornmental scannas then used to arator filter (Fwhich mainly

lhead filter (Fmaterial dephe LP filter.

evels (Table 1)erved from theface.

original wellperformance.009 (t/h/b) II at high rate

25 60 75

ontrast to thee of depositionoughly with thehown in Figureulation, for ther is used fortter.

RK21 duringoperation with

ollow the trendbut injectivity

wagelok 2 µmr and injectionning electroninvestigate the

Figure 3) had ay consisted ofigure 4) had aposited with

. e

l

e n e e e r

g h

d y

m n n e a f a h

Figu

Figu

Interpthat collocamewellbrestri UnfoKA4subseplansprepaPK4A

re 3: Low masteel filt

re 4: Low masteel filt

preting the resthe most lik

oidal silica sera runs donebores were reliction was occu

ortunately, both43 also identifiequent sleevins to acidise aration work A.

agnification ofter from LP bri

agnification ofter from injecti

sults of this tekely cause of scaling. Sube in all wells latively clean urring at the w

h the spinner ed a shallow c

ng job was noKA43 wer

focused on a

f the 2µm staine.

f the 2µm staion wellhead b

est, it was postf scaling is dbsequent dow

identified thconfirming th

well face.

and camera rucasing break anot successful. re abandonedacidising KA4

ainless

ainless rine.

tulated due to wnhole hat the hat the

uns in nd the Thus,

d and 4 and

Page 3: Acidising Case Study – Kawerau Injection Wells · Yoong Wei Lim 1, Malcolm Grant2, Kevin Brown3, Christine Siega and Farrell Siega1 1 Mighty River Power, 283 Vaughan Road, Rotorua,

WELL ACIDISING

BJ Services were contracted to design and carry out the acidising. A 2” coil tubing unit with a 5 hole 45º nozzle bottom hole assembly was used giving a maximum pump rate of 3.5 - 4.0 barrels per minute. The use of a CTU was hoped to provide better acid placement as it can be moved to each zone prior to pumping acid. A traditional 10% hydrochloric (HCL) to 5% hydrofluoric (HF) mud acid was used for this project along with corrosion inhibitors, iron chelating agents and gelling agents. The standard 10% HCL preflush was also used to dissolve carbonate minerals in the formation (Kalfayan, 2008, p70). Both wells were quenched prior to the acidisation and a multi-rate injection test along with downhole camera and High Temperature Casing Corrosion (HTCC) runs was carried out to identify the pre-acidising conditions. The pre-flush was then carried out followed by the mud-acid mixture. Permeable zones were divided into groups and acidised using a “bottom-up” approach. This approach was used as there were concerns that a “top-down” approach would open shallow zones and introduce hot inflows which will reduce the effectiveness of the corrosion inhibitors. After each zone was acidised, a water overflush was carried out to displace the mud-acid mixture away from the wellbore (Kalfayan, 2008, p73). It should be noted that while pumping acid into the well approximately 2 barrels per minute of water was pumped into the well from the side valves to keep the well cool and to prevent acid upflows. Information on the acidised zones and mixture amounts are shown in Figure 5 and Figure 6.

Figure 5: Wellbore schematic of KA44 showing

permeable zones (red) and amounts of acid introduced to each zone (green).

Figure 6: Wellbore schematic of PK4A showing

permeable zones (red) and amounts of acid introduced to each zone (green).

kick-off point398.4m

Top of 10-3/4" liner (ID=0.253m)1438.4 mMD/ 1382.4 mVD 13-3/8" (ID=0.315m) Production Casing Shoe

1468.04 mMD/ 1411.3 mVD

Bottom of 10-3/4" liner2582.4 mMD/ 2448.4 mVD

Total Depth = 2582.4 mMD/ 2448.4 mVD

KA44 (Big Hole)

RT-CHF = 9.6m

All depths are referred to the Casing Head Flange

20" Casing (ID=0.486m) 394.4m

Tie Back = 345.4m

30" Casing 12.4m

1450 - 1480m

1590 - 1615m1680 - 1710m

1860 - 1900m

2010 - 2035m2052 - 2084m

2500 - 2560m

Zone 1240 bbls HCL350 bbls HCL:HF

Zone 2270 bbls HCL420 bbls HCL:HF

Zone 3120 bbls HCL180 bbls HCL:HF

Zone 4220 bbls HCL320 bbls HCL:HF

Zone 5140 bbls HCL

200 bbls HCL:HF

kick-off point394.3m

Top of 7" liner (ID=0.16m)1317.2 mMD/ 1235.4 mVD

9-5/8" (ID=0.22m) Production Casing Shoe1340.6 mMD/ 1256.45 mVD

Bottom of 7" liner1915.2 mMD/ 1710.3 mVD

Total Depth = 1922 mMD/ 1715.4 mVD

PK4A

13-3/8" Casing (ID=0.32m) 387.8m

RT-CHF = 5.4m

All depths are referred to the Casing Head Flange

18-5/8" Casing (ID=0.45m) 119.6m

Tie Back = 348.5m

24" Casing (ID=0.59m) 23.6m

1404 - 1450m

1550 - 1700m

1870 - 1880m

Stage 140 bbls HCL60 bbls HCL:HF

Stage 2586 bbls HCL879 bbls HCL:HF

Stage 3176 bbls HCL264 bbls HCL:HF

Page 4: Acidising Case Study – Kawerau Injection Wells · Yoong Wei Lim 1, Malcolm Grant2, Kevin Brown3, Christine Siega and Farrell Siega1 1 Mighty River Power, 283 Vaughan Road, Rotorua,

RESULTS

Given that multi-rate injection tests along with downhole cameras and HTCCs were carried out before and after the acidising, the well improvements can be measured reasonably accurately. Spinner runs into KA44 (Figure 7) showed that prior to acidising, the bottom zones were almost fully blocked and the majority of fluid was exiting at 2090-2135mMD. Gross Injectivity index (i.e. without compensating for inflows) at this point had decreased to 25 t/h/b. Post-acidising, the spinner profiles were similar to original well conditions suggesting the bottom zones had recovered most of its original performance. Gross injectivity index post-acidising had doubled to 50 t/h/b.

Figure 7: KA44 PTS profiles comparing original

performance to pre and post acidising performance.

At PK4A (Figure 8), the spinner runs for the post-acidising run had a large bias with velocities at the casing showing much higher values compared to the pump rate. Applying a correction factor solves this, but a bias still exists from 1700mMD onwards. However, even with this issue it is still clear that the main zone at 1570-1595mMD is partially blocked prior to acidising. Injectivity index at this point had decreased to 50 t/h/b. Post-acidising, the main zone has completely recovered its original permeability increasing the injectivity index to 84 t/h/b.

Figure 8: PK4A PTS profiles comparing original

performance to pre and post acid performance

In order to further analyse the improvements due to acidising, a zone by zone injectivity index (Table 2 and Table 3) was calculated. This was done using the spinner response and unfortunately a few zones had a different sign due to changes that are too small for the spinner to measure. Regardless of this, the results are still useful as a qualitative tool to compare the effectiveness of the project. At KA44, the deeper zones achieved the greatest improvement with acidising, particularly the zone at 2295-2335mMD. The shallower zones showed very little improvements. PK4A’s calculation showed a similar result with deeper zones achieving the greatest improvements with minimal effect on the shallow zones. However, it should be noted that the spinner bias seen at PK4A’s post-acidising run may have affected the calculations. Table 2: Zone by zone injectivity index for KA44 to

two significant figures. Figures with * signifies inaccurate values.

Zone Type Original II (t/h/b)

Pre-acid II (t/h/b)

Post-acid II (t/h/b)

1450 In -8.3 -0.30 2.1* 1680 In -21 -0.030 1.5* 2075-2135

Out 42 17 23

2295-2335

Out 27 1.5 16

2500 Out 2.2 -0.60* 2.0

-10

10

30

50

70

90

110

130

150

0

0.2

0.4

0.6

0.8

1

1.2

1.4

1400 1600 1800 2000 2200 2400 2600

Tem

pera

ture

[C]

Flui

d Ve

loci

ty [m

/s]

Depth [m MD]

Orig vel - 118t/h Post Acid Vel - 105 t/h Pre Acid vel - 105 t/h

Orig T - 118 t/h Post Acid T - 105 t/h Pre Acid T - 105t/h

20

40

60

80

100

120

140

160

180

200

0

0.2

0.4

0.6

0.8

1

1.2

1.4

1.6

1.8

2

1200 1300 1400 1500 1600 1700 1800 1900 2000

Tem

pera

ture

[C]

Flui

d Ve

loci

ty [m

/s]

Depth [m]

Orig Vel - 90t/h Pre-acid Vel - 116t/h Post-acid Vel - 116t/h

Orig T - 90t/h Pre-acid T - 116 t/h Post-acid T - 116t/h

Page 5: Acidising Case Study – Kawerau Injection Wells · Yoong Wei Lim 1, Malcolm Grant2, Kevin Brown3, Christine Siega and Farrell Siega1 1 Mighty River Power, 283 Vaughan Road, Rotorua,

Table 3: Zone by zone injectivity index for PK4A to two significant figures. Figures with * signifies inaccurate values.

Zone Type Original II (t/h/b)

Pre-acid II (t/h/b)

Post-acid II (t/h/b)

1404 In -4.6 -3.6 -1.9 1570-1595

Out 62 53 67

1870-1880

Out -6.4* -0.60* 8.0

Downhole camera runs at KA44 (Figure 9) showed little change in well condition as the wellbore was very clean in the first instance. Several parts of the liner showed some minor scaling which was not evident post-acidising. Given that most of the scaling occurred at the wellface behind the perforated liner, camera runs are not ideal as a measure of success for the project.

Figure 9: (a) Pre-acidising downhole camera run at

KA44 showing slight scaling in the liner. (b) Post-acidising downhole camera run at KA44 showing cleaned liner.

However, the camera runs and HTCC at KA44 did identify that there was no change in casing thickness confirming that the corrosion inhibitors used were

effective. Another interesting observation is that there was no evidence of acid in the 13-3/8” production casing which suggested no upflows of acid. The downhole camera run at PK4A (Figure 10) showed that the perforations were scaled up prior to acidisation. The blockages were particularly worse near the main feedzone where injected fluids exited the well. Introduction of acid managed to fully dissolve all scale in the perforations. Again, due to the scaling occurring mainly at the wellface, this result should not be used as a measure of success.

Figure 10: (a) Pre-acidising downhole camera run at

PK4A showing scaled perforations. (b) Post-acidising downhole camera run at PK4A showing unblocked perforations.

Similar to KA44, both the camera and HTCC runs showed no noticeable corrosion due to acid. As expected, the 9-5/8” casing also showed no evidence of contact with acid.

DISCUSSION

From the pre and post acidising multi-rate injection test, it is clear that the acid had a preferential flow path to the deeper zones even with placement with the CTU. This phenomena isn’t too surprising as it is common for the deeper zone to be the largest exit point as hydrostatic gradient provides a greater

(a)

(b)

(a)

(b)

Page 6: Acidising Case Study – Kawerau Injection Wells · Yoong Wei Lim 1, Malcolm Grant2, Kevin Brown3, Christine Siega and Farrell Siega1 1 Mighty River Power, 283 Vaughan Road, Rotorua,

driving force. Moreover, the deeper zones at KA44 and PK4A are the most permeable. The “bottom-up” approach also reduced the chance of placement as once the deeper zones are unblocked it opens a preferential pathway for the acid to exit the well. A “top-down” approach may have allowed for better acid placement as the bottom zones would have remained blocked as the top zones are acidised. Plus, the hydrostatic pressure and additional water introduced during the acid stages will reduce any upflows of acid allowing the deeper zones to be sequentially acidised. Concerns with the shallow zones inflowing causing the corrosion inhibitors to lose effectiveness using the “top-down” approach could possibly be mitigated by a few methods. The most obvious would be to use inhibitors with higher temperature limitations or by introducing a large quantity of cold water to quench the top zone. Both methods will unfortunately increase the overall cost of the project. Increasing a higher concentration of HF acid (say 9%) and lower amounts of HCL acid should theoretically provide a more effective mud acid mixture (P Rae 2010, pers. comm.. 29 April). There are also several proprietary mud acid mixtures available that contains higher amounts of HF which are safer to handle.

CONCLUSIONS

Since plant commissioning in August 2008, all three KGL injection wells (KA43, KA44 and PK4A) have declined due to silica scaling in spite of pH modification inhibition. Downhole camera runs identified very little scaling in the wellbore, confirming that the decline in injectivity is due to silica scaling at the wellface.

PK4A and KA44 were acidised with a CTU using a standard 10%:5% HCL:HF mud acid with a 10% HCL preflush. Multi-rate injection tests carried out before and after acidising showed that the deeper zones improved post acidification but the shallow zones did not. Injectivity index of both wells did improve substantially post acidising, but did not fully recover its original capacity. Downhole camera and HTCC runs confirmed that the corrosion inhibitors were effective in preventing acid attack on the casing and liner. The results also confirmed that acid placement was unsuccessful as once the main bottom zones are unblocked, a preferential pathway opens for acid to exit the well. A “top-down” approach may be more successful with acid placement compared with a “bottom-up” as it allows for the bottom zones to remain blocked as the shallow zones are acidised. Increasing the HF concentration may also increase the effectiveness of the mud acid.

ACKNOWLEDGEMENTS

The authors wish to thank the management of Mighty River Power for the review and permission to publish this paper and all staff who have been involved with this project. Also, the authors would like to thank Phil Rae (InTuition Energy Associates), David Addison (Thermal Chemistry) and Julius Dacanay (SKM) for their help and support during this project. Lastly, thank you to BJ Services New Zealand for services rendered.

REFERENCES

Kalfayan, L., (2008), “Production Enhancement with Acid Stimulation,” PennWell, Oklahoma.

Horie, T., (2009), “Kawerau and Nga Awa Purua Geothermal Power Station Projects, New Zealand”, Fuji Electric Review, 55-3, 80-86.