best practices in energy efficiency in fertilizer sector€¦ · energy saving scheme ng fuel...
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Rashtriya Chemicals and Fertilizers Limited
(A Government of India Undertaking)
Ammonia Plant Rastriya Chemicals & Fertilizers Ltd.1
BEST PRACTICES IN
ENERGY EFFICIENCY IN
FERTILIZER SECTOR
Rastriya Chemicals & Fertilizers Ltd.22
Incorporated in 1978 with the re-organisation of erstwhile FCI
This Organization is a JEWEL called “MINIRATNA”
Consistently PROFIT making
Two UNITS- TROMBAY & THAL
THAL -Capacity to produce 20.00 Lakh MT of UREA
Rashtriya Chemicals and Fertilizers Ltd.
Rastriya Chemicals & Fertilizers Ltd.3
Urea
(20 LMT)
Methyl Amine
(0.11 LMT)
Ammonia
(11.55 LMT)
DMF
(0.025 LMT)
Argon(0.14 LMT)
Thal Unit
DMAc(0.05 LMT)
Formic Acid (0.1 LMT)
RCF, THAL
R.C.F.Thal Unit
FEATURES
1. FIRST of it’s kind “MEGA FERTILIZER UNIT” in INDIA using NATURAL GAS from Mumbai Offshore as Raw Material.
2. When it was established this was the LARGEST producer of UREA FERTILIZER from single location in ASIA (More than 1.5 Million MT in a Year)
3. FIRST FERTILIZER UNIT with DCS in INDIA.
4. ADVANCED CONTROL UNIT and PLC for Electrical Load Management.
5. Strong emphasis on Environmental management.
6. In-Built Pollution Control and Safety features.
Our Achievements: 2014-15
• Highest
• Ammonia Production
13,39,430 MT
• Lowest
• Energy
8.24 Gcal/MT
Our Achievements: 2014-15
• Highest
• Urea Production
21,78,010 MT
• Lowest
• Energy
5.869 Gcal/MT
1000000
1100000
1200000
1300000
1400000
YEAR
1205350 1199070
1339430
Ammonia Production MT
2012-13 . 2013-14 2014-15
Rastriya Chemicals & Fertilizers Ltd.9
AMMONIA PRODUCTION
6
6.5
7
7.5
8
8.5
9
YEAR
8.85 8.594 8.24
Energy in Gcal /MT
2012-13 . 2013-142 2014-15
Rastriya Chemicals & Fertilizers Ltd.10
AMMONIA ENERGY
1500000
1600000
1700000
1800000
1900000
2000000
2100000
2200000
YEAR
1951200
1993800
2178010
Urea Production MT
2012-13 . 2013-14 2014-15
Rastriya Chemicals & Fertilizers Ltd.11
UREA PRODUCTION
5
5.5
6
6.5
7
YEAR
6.22 6.098
5.869
Urea SP.Energy Gcal/MT
2012-13 . 2013-14 2014-15
Rastriya Chemicals & Fertilizers Ltd.12
UREA SP. ENERGY CONS.
1984-85 : Initial set up
Ammonia Plants : 2 x 1350 MTPD
Urea Plants : 3 x 1500 MTPD
Initial Ammonia energy- 9.5 GCal/MT
Initial Urea energy - 7.5 Gcal/MT.
Improvement Schemes at RCF-Thal Unit
1
2011-12 : Ammonia Revamp scheme
Increased Ammonia production capacity to
2 x 1750 =3500 MTPD
Increased Urea production to 6060 MTPD.
Reduction in Ammonia Energy by 0.6 Gcal/MT.
Improvement schemes at RCF-Thal Unit
1
RCF Thal Ammonia & Urea performance
during Commissioning Time and Present
1
Unit Before Present
Ammonia
Production
MTPD 2700 3500
Ammonia Energy Gcal/MT 9.5 8.15
Urea Production MTPD 4500 6060
Urea Energy Gcal/MT 7.5 5.8
ENERGY SAVING SCHEME
Replacement of combustion air pre heater in waste heat section of Primary
Reformer
Before After Gain
Fin type exchanger
Plate type exchanger
Flue gas outlet
temperature 175°C.
Flue gas outlet
temperature 140OC.
Energy savings:
0.05GKcal/MT
16
Modification of NG coil E204A/B in waste heat section of Primary Reformer
S.No Before After Gain
Modification of NG CoilE204A/B(4 inlets)
Modification ofNG Coil
E204A/B(8 inlets)
1 Inlet Pressure 39.8 Kg/cm2
Inlet Pressure 39.8 Kg/cm2
2 Outlet Pressure 37.9
Kg/cm2
Outlet Pressure 39.2 Kg/cm2
3 Diff. press.1.9Kg/cm2
Diff. press. 0.5 Kg/cm2
1.4Kg/cm2
Steam saving 2.52 MT/hr per stream in Synthesis Gas Compressor
17
ENERGY SAVING SCHEME
Energy saving is
0.13 Gcal/MT.
S-50 CONVERTER INSTALLATION FOR L1 &L2
• Increase in ammonia concentration exit the new converter.
• Decrease in loop pressure due to lower circulation rate (from 195-200 kg/cm2 g to 178-180 kg/cm2 g)
• Savings in steam to synthesis gas compressor & refrigeration compressors.
• Additional HP Steam production from loop resulting in lower of energy consumption.
ENERGY SAVING SCHEME
ENERGY SAVING SCHEME
.
Energy Saving
is 0.16
Gcal/MT.
MP Condensate Stripper
Revamp of single stage Benfield CO2 removalsystem to 2 stage GV system in Ammonia - I
Before After Gain
HP Regenerator (single stage)
2 stage GV system HP &
LP regenerator
Steam consumption
32 MT/Hr.
Steam consumption
20 MT/Hr.
LP Steam saving of 12 MT/hr.
To be utilized for
BFW/CT turbines. Energy
savings: 0.15
MKcal/ MT
20
ENERGY SAVING SCHEME
REPLACEMENT OF MP TURBINES WITH LP TURBINES FOR COOLING TOWER AND BFW PUMPS
Energy saving is
0.12 Gcal/MT.
Total MP Steam consumption of 25 MT/hr was saved.
ENERGY SAVING SCHEME
S – 200 BASKET REPLACED WITH S-300 BASKET
SAVING : 0.02
MKCAL/MT
ENERGY SAVING SCHEME
E-1504 water cooler CS tubes replaced with Duplex SS tubes
to improve performance
Energy
saving is
0.03
Gcal/MT.
ENERGY SAVING SCHEME
ENERGY SAVING SCHEME
NG FUEL PREHEATING
Heating of Fuel gas from 300C to 900 C by
MP Stripper outlet condensate which is at
at 1200 C in new Exchanger E 216.
Saving of 0.005 MKcal/MT. of NH3.
Ammonia Plant Rastriya Chemicals & Fertilizers Ltd.24
ENERGY SAVING SCHEME
NG FUEL PREHEATING
Ammonia Plant Rastriya Chemicals & Fertilizers Ltd.25
ENERGY SAVING SCHEME
Methanator Heating
Ammonia Plant Rastriya Chemicals & Fertilizers Ltd.26
Methanator Heating to the required temp.takes
About 6 to 8 hrs.
If Methanator is made ready in advance,process
gas can be lined up directly to the the synthesis
after CO2 Removal section is ready thereby
saving startup time.
ENERGY SAVING SCHEME
Methanator Heating
Ammonia Plant Rastriya Chemicals & Fertilizers Ltd.27
ENERGY SAVING SCHEME
Provision of CV in NG line to GV absorber for
energy improvement during start up.
Ammonia Plant Rastriya Chemicals & Fertilizers Ltd.28
Running of small seal water
pump instead of 3.3KV motor
pump during GV startup
Ammonia Plant Rastriya Chemicals & Fertilizers Ltd.
29
ENERGY SAVING SCHEME
Seal water grid modification
Seal water grid modification
Ammonia Plant Rastriya Chemicals & Fertilizers Ltd.
30
ENERGY SAVING SCHEME
APC- Advanced process controller for process
Optimization.
• Regular Monitoring of Primary Reformer tube
skin temp. and furnace temp adjustments.
• Flare header/PSV checking with temp. gun.
• Steam traps monitoring.
Ammonia Plant Rastriya Chemicals & Fertilizers Ltd.
31
ENERGY SAVING SCHEME
Present Energy reduction plan for Thal
plants
Replacing existing Steam Turbo Generators by
Gas Turbo Generators with HRSG for power &
Steam Production.
• Ammonia Energy will reduce from 8.12 Gcal / MT to 7.7
Gcal / MT.
• Urea Energy will reduce from 5.8 to 5.45 G Cal/MT.
• Total estimated Gas saving - 0.25 MMSCMD
• Total estimated raw water saving – 6400 M3/Day
3
Ammonia Plant Rastriya Chemicals & Fertilizers Ltd.33
Present Energy reduction plan for Thal
plants
Replacing existing
Steam Turbo
Generators by Gas
Turbo Generators
with HRSG for
power & Steam
Production.
Total estimated Gas
saving-0.25
MMSCMD
Rastriya Chemicals & Fertilizers Ltd.34