by-16_ddr_2012-11-02
TRANSCRIPT
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Well Name:
Chevron Bangladesh Drilling Morning Report
Report Printed : 11/3/2012
Date: 11/2/2012
Slot:
SBU Drilling Well Category : Drlg Well Category 3
Rig: WDI 801 End Date:
Days Since Last DAFW / RI Case : 689 / 36
Total Time: 60.00
Time from Spud: 53.02
Rpt No: 60
Hours: 24.00
Depth End (MD) (mKB): 4,183 TVD End (mKB): 3,465.19
Field Name
BibiyanaOriginal Spud Date
9/10/2012Country
BangladeshWater Depth (m) Original KB to Mud Line (m)
Actual Start Date
9/4/2012 00:00Actual End Date Target Depth (MD) (mKB)
4,450Target Depth (TVD) (mKB)
AFE/WBS Number
100630Total AFE Amount (Cost)
19,433,001Safety/Inspections
Date Safety Check Tour Des
11/2/2012 00:00 Pre-Job Meeting Night Gen. Crane lifting
11/2/2012 00:00 Pre-Job Meeting Night Gen Hot work (PTW)
11/2/2012 00:00 Pre-Job Meeting Night Clean Mud Tank (PTW)
11/2/2012 00:00 Pre-Job Meeting Night Gen. Forklift ops
11/2/2012 01:30 Safety Procedures Night T-card Audit
11/2/2012 06:00 Pre-Job Meeting Day Hot Work - Rain Shed (PTW)
11/2/2012 06:00 Pre-Job Meeting Day Gen. Forklift ops
11/2/2012 06:30 Pre-Job Meeting Day Service TD (PTW)
11/2/2012 06:30 Safety Meeting Day Permit Meeting- BBS, Tnt# 2
11/2/2012 06:30 Pre-Tour Safety Meeting Day w/Akota, BBS, Tnt# 2
11/2/2012 07:00 Pre-Tour Safety Meeting Day w/Drivers, BBS, Tnt# 2
11/2/2012 07:00 Pre-Job Meeting Day General maintenance (BJ)
11/2/2012 08:00 Pre-Job Meeting Day Slip & Cut Drill Line (PTW)
11/2/2012 08:00 Pre-Job Meeting Day Refueling equipments (PTW)
11/2/2012 08:00 Pre-Job Meeting Day Painting with brush
11/2/2012 08:28 Trip Drill Day Trip Drill/40sec
11/2/2012 09:30 PTW Audit Day General hotwork, TRA audited
11/2/2012 10:45 Pre-Job Meeting Day Collecting waste materials from Location
11/2/2012 11:30 Pre-Tour Safety Meeting Day RADAR Cards, Ops, Tnt#2
11/2/2012 12:00 Pre-Job Meeting Day Gen Hot work (PTW)
11/2/2012 12:00 Pre-Job Meeting Day Gen. Crane lifting
11/2/2012 13:30 Safety Procedures Day T-card Audit
11/2/2012 14:00 Pre-Job Meeting Day Service Geberator (PTW)
11/2/2012 14:10 PTW Audit Day Fixing sunshade on roof, TRA audited
11/2/2012 16:00 PTW Audit Day Transfer & refueling diesel, TRA audited
11/2/2012 17:00 Safety Meeting Day Permit Meeting- BBS, Tnt#2
11/2/2012 18:00 Pre-Job Meeting Night Gen. Forklift ops
11/2/2012 18:30 Pre-Job Meeting Night Refueling equipments (PTW)
11/2/2012 18:30 Pre-Tour Safety Meeting Night w/Akota, BBS, Tnt# 2
11/2/2012 22:00 Pre-Job Meeting Night Working at Height (PTW)
Safety / Environmental IncidentsIncident Cat. Incident Desc
No safety or environmental incident.
BY-16
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Well Name:
Chevron Bangladesh Drilling Morning Report
Report Printed : 11/3/2012
Date: 11/2/2012
Slot:
SBU Drilling Well Category : Drlg Well Category 3
Rig: WDI 801 End Date:
Days Since Last DAFW / RI Case : 689 / 36
Total Time: 60.00
Time from Spud: 53.02
Rpt No: 60
Hours: 24.00
Daily OperationsReport Start Date
11/2/2012 00:00Report End Date
11/3/2012 00:00Daily Field Est Total (Cost)
198,330Cum Field Est To Date (Cost)
13,253,170Daily Mud Field Est (Cost)
7,394Cum Mud Cost to Date (Cost)
438,545Drilling Hours (hr)
4.50Cum Rotating Hrs on Casing
185.5Operations Summary
Ops for past 24 hrs: Trouble shoot LWD. TIH to 3022m. Slip & cut drill line. Cont TIH to 3840m. Ream & wash to 4137m. Drill 8-1/2" hole f/ 4137m to 4183m.
Projected ops for next 24 hrs: Work on pipe handler & C/O saver sub. Cont drilling 8-1/2" hole section.Comments
00:00-05:00 Ops:
00:00-00:30 Rig Service
00:30-02:00 Change Grabber dies on pipe handler. Monitor on the trip Tank
02:00-02:30 Circulate Gas 15%
02:30-04:30 Pull one stand and Change out Saver Sub. Monitor on the trip Tank
04:30-05:00 Continue drilling 8 1/2" hole section F/4183 T/4189mMax Drill Gas
6.10Avg Background Gas
4.16Head Count
129.0Required Matls next day
Hawk jaw: WDI 100-10 torque wrench on site. Lamprell performed engineering survey for installation. Awaiting installation.Hydraulic torque wrench waiting on parts.Leaking main seal on ODS hydraulic cathead. Recieved spare seals. Will install while performing open hole logging.Multiple leaking or inoperable 6" valves in mud tanks. Spares on location. Will repair during rig move.93 joints of Chevron 5" drillpipe being utilized by WDI.#15 Seal leaking & shaft misaligned causing vibration on Reserve pit #1, no spare parts.Diesel centrifuge not working waiting on seals.Safety Observation Cards
Observation Typ # Rpts Com
CVX-9, WDI-15, Other-40 64 During lifting gear oil barrel by crane I observed a person on the rig floor came in between the air winch and the load when they were putting it down. I immediately stopped the crane operator and moved the person to safety and explained the hazard that he could have been caught in between. Tenet # 2 - OMAR FARUQUE - FLOORMAN - WDI
Daily ContactsContact
Tracy Love
Stephen Joubert
Jay Darder
Musharref Hossain
Latifur Rahman
Peter Jennings
Time Log
Start Time End Time Phase Activity Dur (hr)Unsched Event?
UE Time (hr)
UE Ref No. Com
00:00 01:30 PRODCSG, DRILL BHATST 1.50 Yes 1.00 38 Trouble shooting LWD. Suspected problem with Radio Active Source.
01:30 08:30 PRODCSG, DRILL TIH 7.00 TIH to 3022m.
08:30 10:30 PRODCSG, DRILL DRLLNSC 2.00 HPJSM. Slip & cut 88' of drill line.
10:30 11:00 PRODCSG, DRILL UNITMAIN 0.50 Rig service - Change out TDS gear lube.
11:00 14:00 PRODCSG, DRILL TIH 3.00 Cont TIH f/ 3022m. Set down @ 3840m w/ up to 30K and unable to work through.
14:00 15:00 PRODCSG, DRILL REAM 1.00 Yes 1.00 39 MU TDS. Ream & wash down f/ 3840m to 3855m and stall out TDS. Work string. Unable to rotate. Cont circ & work string. Gas increase to 40%. Flowcheck (static). Cont work pipe & circ until gas decreased. Set down 70K & cock jars. PU 70K overpull, hold, & fire jars. Pipe free. Cont PU & start rotation. Back ream to 3834m & ream down to 3863m. Backream & ream down stand.
15:00 15:30 PRODCSG, DRILL REAM 0.50 Ream & wash f/ 3863m to 3900m.
BY-16
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Well Name:
Chevron Bangladesh Drilling Morning Report
Report Printed : 11/3/2012
Date: 11/2/2012
Slot:
SBU Drilling Well Category : Drlg Well Category 3
Rig: WDI 801 End Date:
Days Since Last DAFW / RI Case : 689 / 36
Total Time: 60.00
Time from Spud: 53.02
Rpt No: 60
Hours: 24.00
Time Log
Start Time End Time Phase Activity Dur (hr)Unsched Event?
UE Time (hr)
UE Ref No. Com
15:30 19:30 PRODCSG, DRILL REAM 4.00 Log down @ 100 m/hr while ream & wash f/ 3900 m to 4137m.
Note: LWD neutron porosity not working.
19:30 00:00 PRODCSG, DRILL DRLROT 4.50 Drill 8-1/2" hole F/4137m T/4183m
Today: Drilled 46m. AROP w/ connection 10.2 m/hr.
4.80 bbls/hr losses, .31 bbls/hr downhole losses.
Lithology (4237.0-4183.0m) - sandstone (15-30%), claystone(Tr-10%) silt stone (60-80%).
Recovered 36 grams metal filings off ditch magnet. Total recovery 516 grams.
PersonnelCompany Total Headcount SSE
Chevron 12
Weatherford 11 Rig Expat
Weatherford 43 Rig National
Weatherford 23 Shamolima Catering
Aker-Kvaerner 1 Wellhead Eng
Weatherford 2 LWD/MWD
BJ Services 3 Cementing
Weatherford 2 DD
MI Swaco 3 Solids control
Weatherford 0 Gyrodata
Weatherford 5 TRS
Brandt NOV 11 Solids
Weatherford 7 Wireline
Weatherford 5 SLS
Weatherford 0 Ayun ent
Chevron 1 PetroBangla
Smith International 0 Inspection
Schlumberger 0 Slickline
Weatherford 0 Completion hands
Weatherford 0 Shafiq Brothers
Chevron 0 WWT
Weatherford 0 BanglaCat
Weatherford 0 Bangla Industrial
Mud ChecksDate
11/2/2012 22:00Depth (MD) (mKB) Depth (TVD) (mKB) Mud/Brine Type
NAFSample Source
Active PitChecked By
Flow Line Temperature (°C) Fluid Density (lb/gal)
11.00Gel 10 sec (lbf/100ft²)
16.0Gel 10 min (lbf/100ft²)
32.0Gel 30 min (lbf/100ft²)
36.0YP Calc (lbf/100ft²)
16Vis 3rpm
7Vis 6rpm
8Vis 300rpm
42Vis 600rpm
68Funnel Viscosity (s/qt)
61PV Calc (Pa•s)
0pH Chlorides (mg/L)
51,500CaCl2 (mg/L)
335,000.00Electric Stability (V)
780.0Water Phase Salinity (mg/L)
283,786ROC (Wet) (% by wt) (lb/lb)
Filtration Sz (µm) High Gravity Solids (lb/bbl)
170.80Corrected Solids (%)
16.80Retort Solids (% by Volume) (%)
19.00Retort Water by Volume (%)
16.00Retort NAF by Volume (%)
65.00NAF/Water Ratio
80.2/19.8NaCl (mg/L) API Filtrate (cc/30min) API Filter Cake (1/32") HTHP Filtrate (cc/30min)
3.4HTHP Filter Cake (1/32")
1Weather Conditions
Wave Ht (m) Swell Ht (m) Wave Dir (°) Wind Spd (knots) Wind Dir P Bar (mmHg) T High (°C) T Low (°C) Visibility (km)
BY-16
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Well Name:
Chevron Bangladesh Drilling Morning Report
Report Printed : 11/3/2012
Date: 11/2/2012
Slot:
SBU Drilling Well Category : Drlg Well Category 3
Rig: WDI 801 End Date:
Days Since Last DAFW / RI Case : 689 / 36
Total Time: 60.00
Time from Spud: 53.02
Rpt No: 60
Hours: 24.00
Support VesselsVessel Name Vessel Type Arrival Date Depart Date Note
Unscheduled EventsReference No. Start Date End Date Event Type Unsch Maj Cat Unsch Detail Description Accountable Party Contractor
38 11/2/2012 11/2/2012 NPT EQP LWD LWD tool problems. Operator's Other Contractors
Weatherford, Directional Drlg-MWD
39 11/2/2012 11/2/2012 NPT WP TIGHT HOLE Hang up @ 3855m. Work & jar free. Back ream & ream down stand.
Operator Chevron, Asset Team
Mud Additive AmountsDes Date Rec Consumed On Loc
Barite 11/2/2012 6.0 148.0
Cacl2 / Nacl 11/2/2012 40.0 200.0
Lime 11/2/2012 13.0 127.0
Nova Plus 11/2/2012 1.0 18.0
Nova Plus 11/2/2012 2.0 34.0
Versatrol M 11/2/2012 17.0 113.0
VG Plus 11/2/2012 6.0 162.0
VG-69 11/2/2012 4.0 146.0
Job Supply AmountsSupply Item Des Date Received Consumed Cum On Loc
Diesel 11/2/2012 0.0 14,315.0 42,960.0
Drill String/BHA
BHA #9, Adjustable Gauge StabilizerBit Run
1Drill Bit
8 1/2in, MDSi516, JG2045
Length (m)
0.25IADC Bit Dull
-------Bit Total Fluid Area (nozzles) (in²)
0.91BHA ROP (m/hr)
10.2
Nozzles (1/32")
15/15/15/16/16String Length (m)
261.61Max Nominal OD (in)
6.750String Components
Smith Bits MDSi516, Stabilizer - Near Bit, Float Sub, Adjustable Gauge Stabilizer, MFR, IDS, NDT, HEL, Stabilizer, 5" HWDP, JARS, 5" HWDPComment
String/BHA ComponentsItem Des Len (m) Mass/Len (lb/ft)
5" HWDP 160.42 49.30
JARS 9.67 0.00
5" HWDP 56.91 49.30
Stabilizer 1.80
HEL 5.42
NDT 8.57
IDS 3.72
MFR 8.98
Adjustable Gauge Stabilizer 3.15
Float Sub 0.81
Stabilizer - Near Bit 1.91
Drilling ParametersWellbore
Original HoleDepth Start (MD) (mKB)
4,137TVD Start (mKB)
3,437.60Depth End (MD) (mKB)
4,183TVD End (mKB)
3,465.19Drill Time (hr)
4.50On Bottom Drill Time (hr)
2.95Interval ROP (m/hr)
10.2Cum Depth Drilled (mKB)
46Cum Drilling Time (hr)
4.50Flow Rate (gpm)
500Weight on Bit (1000lbf)
20RPM (rpm)
180Stand Pipe Pressure (psi)
3,100.0Drill Str Wt (1000lbf)
270Pick-Up String Weight (1000lbf)
365Drilling Torque
20.0Weight of String in Air (1000lbf)
35Slack-Off String Weight (1000lbf)
220Casing StringsCasing Description
Intermediate Casing 2Set Depth (MD) (mKB)
3,032Set Depth (TVD) (mKB)
2,753.79Run Date
10/11/2012Comment
BY-16
Page 5/5
Well Name:
Chevron Bangladesh Drilling Morning Report
Report Printed : 11/3/2012
Date: 11/2/2012
Slot:
SBU Drilling Well Category : Drlg Well Category 3
Rig: WDI 801 End Date:
Days Since Last DAFW / RI Case : 689 / 36
Total Time: 60.00
Time from Spud: 53.02
Rpt No: 60
Hours: 24.00
Casing ComponentsTop Depth (MD) (mKB) Btm Depth (MD) (mKB) Len (m) Jts Item Des OD (in) ID (in)
Tubing StringsTubing Description Set Depth (mKB) Run Date
Comment
Tubing ComponentsTop Depth (mKB) Bottom Depth (mKB) Length (m) Joints Item Description OD Nominal (in) ID (in)
BOP TestDate Com
11/1/2012 Press test 13 5/8'' 10k BOPE - annular - 200/3500psi. Upr & lwr pipe rams, VBR's, BSR's, choke/ kill HCR & manual valves, check valve, TIW, kelly cock, IBOP, standpipe & manifold, kelly hose, MP manifold, choke & kill lines, choke manifold- 200/5000 psi. Perfrom koomey drawdown test - IP - 2900 psi, FP - 1800 psi, Recharge - 2min 41 sec.
WellboresWellbore Name
Original HoleKick Off Depth (mKB)
Directional SurveysDescription
Planned survey BY-16Survey Data
Date MD (mKB) Incl (°) Azm (°) TVD (mKB) VS (m) NS (m) EW (m) DLS (°/30m)
Description
Actual Survey BY-16Survey Data
Date MD (mKB) Incl (°) Azm (°) TVD (mKB) VS (m) NS (m) EW (m) DLS (°/30m)
11/2/2012 4,137.04 52.36 244.20 3,437.62 1,257.79 -1,148.38 -548.91 0.51
11/2/2012 4,166.50 53.51 244.11 3,455.38 1,278.19 -1,158.63 -570.06 1.17
11/2/2012 4,183.00 53.51 244.11 3,465.19 1,289.71 -1,164.42 -582.00 0.00
BY-16