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AD-A022 207 MARINE FOULING OF TITANIUM HEAT EXCHANGERS Wayne L. Adamson David W. Taylor Naval Ship Research and Development Center- Annapolis, Maryland March 1976 DISTRIBUTED BY: National Technical Information Service U, S. DEPARTMENT OF COMMERCE

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AD-A022 207

MARINE FOULING OF TITANIUM HEAT EXCHANGERS

Wayne L. Adamson

David W. Taylor Naval Ship Research and Development Center- Annapolis, Maryland

March 1976

DISTRIBUTED BY:

National Technical Information Service U, S. DEPARTMENT OF COMMERCE

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THIS DOCUMENT IS BEST QUALITY AVAILABLE. THE COPY

FURNISHED TO DTIC CONTAINED

A SIGNIFICANT NUMBER OF

PAGES WHICH DO NOT

REPRODUCE LEGIBLYo

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DAVID W. TAYLOR NAVAL SHIP RESEARCH AND DEVELOPMENT CENTER

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Beth«sdo, Md. 20034

MARINE FOULING OF TITANIUM HEAT EXCHANGERS

by Wayne L. Adamson

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Approved for public release; distribution unlimited.

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PROPULSION AND AUXILIARY SYSTEMS DEPARTMENT

Annapolis

RESEARCH AND DEVELOPMENT REPORT

March 1976 REPRODUCED BY NATIOKÄL TECHNICAL Report PAS-75-29 INFORMATION SERVICE J

Tne Naval Ship Rrtrarch and De.*lopweru Center n a I; 5. N«v> enter lor launratory il effort directed at achieving • mproved tea and air vehirlee. it *ea formed in March 1967 by merfins *• David Taylor Model B&ain at Carderork, Mary lend with the Marine Engineering Laboratory at Annapolia, Maryland

Nevai Ship Rfoeerrh ar,d Development Center

Bethetde. Md. 200.14

MAJOR NSROC ORGANIZATIONAL COMPONENTS

REPORT ORIGINATOR

NSRDC

COMMANDER ^ 00

TECHNICAL DIRECTOR

OFFICER-IN- CHARGE CARDEROCK

05

OFFICER-IN-CMARCE ANNAPOLIS

04

SYSTEMS DEVELOPMENT DEPARTMENT

SHIP PERFORMANCE DEPARTMENT

AVIATION AND SURFACE EFFECTS

DEPARTMENT 16

STRUCTURES DEPARTMENT

!7

COMPUTATION AND MATHEMATICS

DEPARTMENT

SHIP ACOUSTICS DEPARTMENT

19

PROPULSION AND * AUXILIARY SYSTEMS

DEPARTMENT 27

/

MATERIALS ncBiBTuryr

CENTRAL INSTRUMENTATION

21 DEPARTMENT ) 29

ü UNCLASSIFIED SECURITY CLASSIFICATION OF THIS PAGE (Whon Oat« Entmtod)

REPORT DOCUMENTATION PAGE 1. REPORT NUMBER

PAS-75-29

[2. COVT ACCESSION NOJ

4. TITLE (md Subtitt*)

MARINE FOULING OF TITANIUM HEAT EXCHANGERS

7. AUTHORft;

Wuyne L. Adamson

9. PERFORMING ORGANIZATION NAME AND ADDRESS

David W. Taylor Naval Ship R&D Center Annapolis, Maryland 21402

11. CONTROLLING OFFICE NAME AND ADDRESS

David W. Taylor Naval Ship R&D Center Bethesda, Maryland 20084

Tt MONITORING AGENCY NAME * ADORESSfJ/ dUUrmnt from Controlling Ofitcm)

READ INSTRUCTIONS BEFORE COMPLETING FORM

3. RECIPIENT'S CATALOG NUMBER

5. TYPE OF REPORT » PERIOD COVERED

Research & Development •■ PERFORMING ORG. REPORT NUMBER

I CONTRACT OP GRANT NUMBER^

10. PROGRAM ELEMENT. PROJECT, TASK AREA • WORK UNIT NUMBERS

Element 63513N, TA SSL 30002, Task 15941 Work Unit 2761-108 12. REPORT DATE

March 1976 IS. NUMBER OF PAGC5

28 IS. SECURITY CLASS, (of thi» tmport)

Unclassified is«, DECLASSIFICATION/OOWNGRADING

SCHEDULE

16. DISTRIBUTION STATEMENT (ot thit Report)

Approved for public release; distribution unlimited.

17. DISTRIBUTION STATEMENT (of tho •beutet ontmrmd in Block 20, II dllloront from Ropott)

II. SUPPLEMENTARY NOTES

19. KEY WOR0S (Cot.ttnif on rovmff «'etc It n»c««««ry mnd Idmntlty by block nunibtf)

Marine fouling Titanium heat exchangers Seawater Chlorination

Shipboard operation

»mry mnd Idmn Ity by block number) 20. ABSTRACT (Continue on rovmrmo mldm tl i

A series of marine foaling experiments was conducted at Freeport, Texas, on two single-pass titanium heat exchangers. The exchangers, which were constructed with commercially pure titanium tubes (5/8-inch (1.59-centimeter) outside diameter by 30-inch (76.3-centimeter length) and 6A1-4V alloy tube sheets and headers, were operated on natural seawater. One of the

(over)

DO ,: FORM AN 71 1473 EDITION OF I NOV 6S IS OBSOLETE

S/N 0102-014 5601 ' UNCLASSIFIED

SECURITY CLASSIFICATION OF THIS PAGE (Whim Dim Mntmrmd)

UNCLASSIFIED -i_i„UH»TY CLASSIFICATION OF THIS PAGEfFh*» Dmtm Bntmrmd)

20. Abstract (cont)

exchangers was fed electrolytically chlorinated seawater, while the other was run with untreated seawater feed. Velocity and chlorination levels were varied to determine the effect of these two variables on fouling of the titanium surfaces. Operating conditions similar to those that might be expected in shipboard heat exchanger/condenser usage were modeled. The tests revealed that fouling of titanium heat exchanger surfaces can occur at velocities less than 4 feet per second (1.2 meters per second) unless preventive techniques such as chlorination are applied. Intermittent chlorination for as short as 4 hours per day at concentrations of 1 part per million total chlorine was sufficient to prevent barnacle attachment. High velocity watsr (9 feet per second (2.7 meters per second) killed small (1- to 2-millimeter) barnacles in a previously established colony but had no apparent effect on larger ones. It is recommended that titanium heat exchangers intended for shipboard operation at seawater tube velocities less than 4 feet per second (1.2 meters per second) be provided with chlorinated seawate-. Chlorination of heat exchangers operating at higher velocities may be warranted, depending upon their other operating conditions.

(Author)

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UNCLASSIFIED SKCUNITV CLASSIFICATION OF THIS PAGEfVh«n Dmtm Bntmrmd)

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u ADMINISTRATIVE INFORMATION

U This investigation was carried out under Element 635J-3N, Task Area SSL 30002, Task 15941, Work Unit 2761-108. The program manager was NAVSEA (SEA 0331F), Dr. F. Ventriglio.

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ACKNOWLEDGMENTS

The author wishes to acknowledge the contribution of Mr. M. W. Titus, who assisted in the design, fabrication, and shakedown of the test apparatus used in this investigation. Also, the contribution of Dr. D. C. Msngum of Dow Chemical Company, who conducted the actual fouling tests and the sub- sequent biological analyses, is acknowledged.

LIST OF ABBREVIATIONS

a-c - alternating-current cm - centimeters d-c - direct-current ft/sec - feet per second gpm - gallor.s per minute g/sec - grams per second lb/hr - pounds per hour mA - milliamperes mm - millimeters m/sec - meters per second mq/l - milligrams per liter o.d. - outside diameter ppm - parts per million ppt - parts per thousand PVC - polyvinyl chloride vdc - volts direct current

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ADMINISTRATIVE INFORMATION ACKNOWLEDGMENTS LIST OF ABBREVIATIONS INTRODUCTION BACKGROUND INVESTIGATION

Fouling Control Techniques Description of Fouling Test Apparatus Method of Test

RESULTS Initial Low Velocity Tests High Velocity Tests Extended Shutdown Intermittent Chlorination Tests Intermediate Velocity Test

CONCLUSIONS AND RECOMMENDATIONS TECHNICAL REFERENCES LIST OF FIGURES

Figure 1 - Photograph; Overall View of Fouling Test System

Figure 2 - Drawing; Piping Layout for Fouling Test Figure 3 - Photograph; Titanium Heat Exchanger Figure 4 - Titanium Heat Exchanjer Detail Drawings Figure 5 " Photograph; Electrolytic Chlorinator Figure 6 - Curves; Heat Exchanger Operating Schedule Figure 7 - Photograph; Barnacle Fouling of Titanium

Heat Exchanger after 2 Weeks at 1 ft/sec (0.3 m/sec) Seawater Velocity

Figure 8 - Photograph; Close-up of Barnacle Fouling in Titanium Tubes after 2 Weeks at 1 ft/sec (0.3 m/sec) Seawater Velocity

Figure 9 ~ Photograph; Typical Unfouled Tube and Tube-sheet Surfaces Experienced wich Chlorinated Seawater

Figare 10 - Photograph; Barnacle Growth on Heat Exchanger Plastic Insert

Figure 11 - Photograph; Barnacle Growth Inside PVC Piping at 1 ft/sec (0.3 m/sec) Seawater Velocity

INITIAL DISTRIBUTION

i 1 1 2 2 4 4 6 6 9 ll ll 12 12 14

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INTRODUCTION

The David W. Taylor Naval Ship Research and Development Center, as authorized by the Naval Sea Systems Command, is investigating the use of titanium for condenser and heat exchanger applications aboard Navy ships. The purpose of this investigation has been to develop the technology necessary for succesr :ul fabrication, installation, and maintenance of shipboard titanium condensers and heat exchangers, to provide improved reliability, maintainability, and performance of these systems as compared to existing copper-nickel systems. A previous DTNSRBC study identified several areas where further investigations were required prior to application of titanium condensers aboard ship. Among tuese were: marine fouling of titanium, galvanic

| corrosion between titanium and other metals in a seawater *"J environment, and fabrication of titanium tubes in a double

tube-sheet heat exchanger or condenser. This report presents the findings on marine fouling of titanium heat exchangers.

Li BACKGROUND

The detrimental effects of marine fouling on ship per- formance have long been recognized by the Navy. These effects range from ship speed reduction due to the increased resistance on the hull to actual plugging of pipes, condensers, and other related equipment used to distribute seawater aboard ship. Under peacetime conditions, these effects are greatly increased because naval vessels spend a larger part of their time in port where fouling is most severe.

For purposes of this report, marine fouling refers to the growth of plant and animal organisms in a seawater environment and attachment of these organisms on submerged surfaces. Universally in the oceans, marine fouling increases in intensity as a ship approaches land masses or enters the warmer waters of the Tropics. Of the many species classified as fouling organisms, the mussels and barnacles are considered to be the most trouble- some because of their hardiness and widespread distribution. Consequently, extensive studies have been conducted on these organisms: methods for their effective control have generally been found adequate for controlling other fouling organisms.

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Prior lo the use of any new material for seawater appli- cation, examination of the effects of marine organisms on that material in a marine environment is desirable. Previous studies of titanium have demonstrated that it has no inherent anti- fouling characteristics or toxicity that will deter or prevent attachment by animal or plant life in seawater. One such study1

showed that titanium panels were completely covered by marine growth after 8 months in quiet seawater. Work by others2

observed marine fouling of titanium specimens immersed in flowing seawater for 4 to 5 years at 3 ft/sec*(0.9 m/sec) velocity.

INVESTIGATION

To explore the marine fouling of titanium, a series of tests wa? conducted at Freeport, Texas, to simulate typical shipboard heat exchanger/condenser operating conditions and to determine typical growth characteristics of marine organisms under those conditions. Methods for fouling control and prevention were also evaluated.

FOULING CONTROL TECHNIQUES

Based upon previous studies, it appeared likely that any titanium equipment (such as condensers) in a shipboard seawater system would require some means of fouling protection. There are several techniques taat have proved «.o be at least partially effective for controlling marine growths in noncopper-based seawater systems: mechanical cleaning, heating the seawater or the surface to be protected, maintaining high seawater velocities in the system, or adding chlorine or similar toxic substances to the water. The first two methods are undesirable over the long run for shipboard heat exchanger or condenser use. Mechanical cleaning is very time consuming and difficult to accomplish in a large heat exchanger or condenser where several hundred tubes must be cleaned. Seawater heating is impractical from the standpoint of energy consumption, alone, since the water temperature or ehe metal surface temperature must be raised to 125° F (51-6° C) to ensure complete protection. Even Lne third method, high velocity operation, can be uncertain because of the existence of points of stagnation or low velocity that can normally develop at changes in the flow cross-sectional area.

1 Superscripts refer to similarly numbered entries in the Techni- cal References at the end of the text.

♦Definitions of abbreviations are on page i.

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The application of chlorine gas to seawater has been pre- viously shown to be an effective method for controlling fouling in land-based seawater-cooled power plants and desalination plants. However, the effectiveness of chlorination in a ship- board titanium condenser or heat exchanger system under a variety of operating conditions (including periods of shutdown) was unknown? therefore, it was felt tnat additional investigation of fouling was necessary. Furthermore, it was desired to investi- gate the application of an electrolytic type chlorinator for fouling control as opposed to chlorine gas injection, which is not considered suitable for ship installation for reasons of safety and logistics.

Chemically, there is no real difference between chlorine gas injection and electrolytic generation of chlorine. In the electrolytic process, chlorine collects at the anode as a result of the flow of current between two electrodes. This chlorine

\ then rapidly reacts with water according to the equation:

Cl2 + H20-*-HOCl + H+ + Cl~ .

The hypochlorous acid, HOCl, formed is a weak acid which tends to undergo partial dissociation as follows:

HOCl^l 0C1~ + H+

to produce a hypochlorite ion and hydrogen ion. At a pH level of 6 or less dissociation is negligible. At higher pH levels (6.0 to 8.5), a sharp change in dissociation occurs, until at a pH of 8.5 to 9-0 very little HOCl remains in solution. The significance of this dissociation is the fact that there is a marked difference in the killing capability of the two sub- stances, HOCl and OCl", on various organisms. Since the OCl" ion is a rather poor disinfectant by comparison with HOCl, it is desirable to have the resulting chlorine solution as high in HOCl concentrc.tion as possible. This, of course, is dependent upon the pH level and the resulting dissociation. As the pH increases, then an increasingly greater volume of chlorine gas must be gener^ed to maintain a constant weight of HOCl and, thereby, to offset the effects of dissociation. A secondary reaction that can occur when HOCl is produced in seawater is the formation of toxic bromine residuals. Further details on these topics m?y be obtained from White.3

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DESCRIPTION OF FOULING TEST APPARATUS

An overall view of the system used for the fouling studies is shown in figure 1. In the actual piping layout, figure 2, two identical single-pass titanium heat exchangers were operated in parallel seawater circuits. One heat exchanger (designated No. 1) was used as the control heat exchanger with iio chlorine protection; the other. No. 2, was placed downstream from an electrolytic chlorinator. The heat exchanger, figure 3* con- sisted of six commercially pure ASTM grade 2 seamless titanium tubes 5/8-inch (1.59-cm) o.d., 0.035-inch (0.089-cm) wall, 30-inch (76.3-cm) length rolled into 6 aluminum - 4 vanadium (6hl-hV^ titanium alloy tube sheets. The headers were also constructed of 6Al-4v alloy. Neither exchanger had a shell since it was desired to conduct tests without tube heating. Details of the construction are given xn figure 4.

The chlorinator, figure 5» which was designed for 0.5 Ib/hr (0.063 g/sec) of chlorine generation, was operated with a 0 to 14 vdc power supply. A variable a-c transformer provided regulation of the voltace to the d-c power supply and, hence, control of the chlorine output.

A bronze centrifugal pump supplied the seawater for the test system. The entire «system was set up adjacent to a seawater distribution canal. This canal, which normally furnishes cooling water for chemical processing facilities owned by Dow Chemical Company, has oftrn been used as a test site for fouJing investiqacions by Dow and is known to be abundant in fouling organisms. The properties for the seawater, which is taken directly from the Gulf of Mexico, are given in table 1. Details on the types and abundance of fouling organisms at that location are available.4

METHOD OF TEST

A summary of the fouling test schedule is provided in figure 6. All test run* were conducted by Dow Chemical Company personnel as part of Navy contract N006ü0-7^-C-0287- The initial'runs (0 to 12 weeks) were conducted at low velocities with continuous chlorination of the No 2 exchanger. These were followed by: a series of high velocity experiments (12 to 20 weeks), a run with a period of complete shutdown (20 to 2k weeks), some low velocity runs with intermittent chlorination (26 to 32 weeks'), ind a finul run at intermediate velocity with no chlorination (5? to 3c weeks).

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TABLE 1 GULF OF MEXICO SEAWATER COMPOSITION Annual Average at Freeport, Texas

A

Typical Value Measured Parameters l Range, mg/1 Annual Average

mg/1

Alkalinity as CaC03 75 - 125 100 Aluminum as Al - 0.5 Ammonium ion as NH4+ 0.01 - 0.1 0.05 Calcium as Ca 240 - 400 340 Carbon dioxide (free) 2 - 5 3

as C02 Chloride as Cl 11,700 - 19,400 16,500 Copper as Cu (total) 0.01 - 0.1* 0.01 Hydrogen-sulfide as K2S - <0.0i 1 Iron as Fe (total) 0.5 - 5.0* 2 Magnesium as Mg 780 ~ 1,300 1,100 Mercury as Hg - <0.0001 Oxygen, dissolved as O2 1.5 - 6.0 5 PH 7.5 - 8.6 8.4 Potassium as K 230 - 380 325 Salinity, "normal" 60^ - 100$ 85^ !

Sodium as Na 6,340 - 10,560 9,000 1 Sulfate as SOi| 1,800 - 3,000 2,600 1 Suspended solids 5-50 20 1 Temperature 60° - 80° F 70° - 75° F 1

(15.5° - 27° C) (21° - 24° C) I

♦Varies with suspended sol ids present. .1

f «* The test schedule was set up on a 2-week operating basis. Initially, both heat exchangers were completely clean with no fouling. At the end of each 2-week period, the heat exchanger headers were removed for inspection, and photographs were taken of the tubes, tube sheets, and headers. In some cases, the tubes, tube sheets, and headers were cleaned prior to reassembly by mechanically removing (scraping^ any biological growths or nonbiological deposits. Cleaning of the tubing was accomplished with a brass or stainless steel wire brush run through each tube. As shewn in the test ew*;cdule, the exchangers wer" sometimes put back on line without cleaning.

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The seawater velocity in the two sets of heat exchanger tubes was controlled by bypassing a portion of the pumped sea- j water directly overboard. The flow rate of water to the chlorinator had to be maintained at 20 to 25 gpnt (0.0126 to O.OI58 m3/sec) in order to prevent the formation of calcareous deposits on the chlorinator electrodes.

The level of total chlorine (combined plus free) was measured by the standard orthotolidine method. Chlorine samples were taken at the discharge of the electrolytic generator and at the discharge of the heat exchanger. The chlorinator current was adjusted until the desired residual was achieved. It was neces- sary tc readjust the voltage setting occasionally to maintain this residual.

RESULTS

INITIAL LOW VELOCITY TESTS

The initial runs, wr ch were conducted at 1 and 2 ft/sec (0.3 and 0.6 m/sec) tube velocity in both heat exchangers, established the fact that marine fouling will occur in titanium heat exchangers, both inside the tubes and on the tube sheets and headers, figures 7 and 8. The species of fouling organisms were principally barnacles with some colonial hydroids. Fouling i occurred on the control (No. 1) heat exchanger, whereas the No. i 2 chlorinated exchanger remained void of any marine growth, figure 9« In spite of the fairly extensive buildup of marine life in the tube£, no problems vere encountered in mechanical 1 cleaning with the wire brush. Attachment did not appear to be as ** tenacious as might often be found with other tube materials.

During this first 12 weekc of fouling runs, t.h<D chlorinated J heat exchanger was initially rwv. at 1.0 ppm ariw was then reduced to a range of 0.5 to 1.0 ppm of chlorine. A nummary of the • results of this un and all subsequent runs, evaluating chlorine as a method of fouling control, is given in table 2. The chlorinated heat exchanger surfaces became covered with a chin brown residue. Principal constituents of this residue, which has been previously described,4 are silica, manganese, and iron. When it was wet, the residue could be easily removed by hand- wiping it with a cloth. It was also found in the experiments that the action of flowing seawater gradually removed the residue from covered surfaces. Previous studies of this precipitate4

seemed to indicate that it helps to deter attachment of barnacles.

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TABLE 2 SUMMARY OF HEAT EXCHANGER FOULING CONTROL

WITH CHLORINATION

Inspection I Date

Heat Exchanger 1 Heat Exchanger 2 Average Chlorine

Residual and Chlorinator

Operating Tiroe

Exchangers Mechanically Cleaned 1

Prior to Run? Headers Tube Sheets Tubes Headers Tube

Sheets Tubes

12-5-73 None Light fouling - 10 barnacles and a ct^onial hydroid

Light fouling - few barnalces

None None None 1-2 ppm con- tinuous

Initial run j

1 12-20-73 None Light fouling - 10 barnacles and remains of a colonial hydroid

None None None None 0.9 ppm con- t inuous

NO j

1 1-4-74 None None None None None None 1.5 ppm con- tinuous

Yes j

1 1-18-74 None None 5 or 6 barnacles per tube

Noie None None 0.6 ppm con- tinuous

No f

1 1-31-74 25-30 barn- icles inlet; 30-50 barn- acles outlet

2 or 3 barn- acles inlet; 5-10 barn- acles outlet

5-10 barn- acles per tube

None None None 0.5 Ppro con- t inuous

NO

1 2-14-74 150-200 barnacles inlet; 100- 150 barn- acles outlet

20-25 barn- acles inlet; 15-20 barn- acles outlet

2^-50 barnacles per tube

None None None 0.7 ppm con- t inuous

No 1

4-26-74 Barnacle*, serpuiids, & encrusting bryozoans

Barnacles Barnacles & serpulids

None None None 0.6 ppm con- tinuous

NO 1

|~ 6-7-74 Barnacles & amphipods

Barnacles & amphipods

Barnacles None None None 0.6 ppm for 8 hours per day '5 out of 7 days)

Yes j

6-21-74 Barnacles & amphipods

Barnacles & ivxssels

Barnacles & amphipod3

Nona None None 0.6 ppm for 8 hours per day (5 out of 7 days)

No

7-5-74 Barnacles & amphipods

Barnacles & mussel?

Barnacles & amphipods

None None None 1.0 ppm for 4 hours p*»r day (5 out of 7 days)

No j

Note: water velocity through both sets of heat exchanger tubes was maintained at 1 ft/sec (0.) m/sen) for j all runs except for the first twc 12-5 and 12-20 inspection dates, which were at 2 ft/sec (0.6 m/sec).J

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The electrolytic chlorinator performed satisfactorily during the low velocity runs with water temperatures that ranged from 49° to 7^° F (9.5° to 23.4° C) and salinities from 12.5 to 30.85 ppt. Chlorine concentration was measured only once each day and therefore was not maintained precisely, as is evident from table 3. Since chlorine demand can change appreciably with charges in dissolved and suspended solids, temperature, hydrogen ion concentration, and biological activity, monitoring chlorine concentration once daily is insufficient to maintain precise control. During the first 2 weeks the average concentration leaving the electrolytic generator was 1.1 ppm with a range of 0.8 to 1.5 ppm. During the next several weeks the concentration was reduced to try to maintain a residual of 0.5 to 1.0 ppm from the generator. Actual average concentration from the generator was 0.8 ppm with a range of 0.1 to 3-0 ppm. Similar results were obtained later in the test program when the chlorine was injected on a part-time basis (4 to 8 hours per day).

TABLE 3 MEASURED CHLORINE CONCENTRATION

FOR VARIOUS TEST RUNS

Week No.

Chlorinator Discharge Concentration, ppm

Heat Exchanger Discharge Concentration, ppm

Desired Chlorine Level ppm Average Median High Low Average Median High I.V. ti

0-2 1.1 1.0 1.5 0.8 1.2 1.0 3.0 0.8 1.0 i

2-12 0.8 0.6 3-0 0.1 0.9 0.6 3.0 C.2 0.5- 1.0 |

20-22 0.5 0.5 0.7 0.3 0.6 0.6 1.3 0.3 0.5 i

| 26-30 0.8 0.3 3.0 0.2 0.6 0.3 3.0 0.1 0.5

| 30-32 1.1 0.5 5.0 0.2 1.0 0.3 5.0 0.2 0.5

Note: Chlorinator was not operated foi 12- to 20-week period, 22- to 26-week period, and 32- to 36-week period.

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With regard to the suitability of the chlorinator for ship application, it was found that the unit had one characteristic that might at first glance appear undesirable. A check of the resistance between the end flanges and the cathode and anode electrical connectors to the unit showed a value of only 20,000 ohms. Based on a 28 vdc supply, this resistance could result in a stray current of 1.4 mA at full load. According to the manufacturer, larger chlorinator units 2 lb/hr (0.25 g/sec) and greater do not have a problem with stray current because of the way they are wired. If it is assumed tha«. the chlorinator was connected directly to a copper-nickel piping system at the inlet flange, then the current would be in a direction that would actually reduce galvanic current effects between the external copper-nickel piping and the titanium piping within the chlorinator. -In this respect the current could be considered beneficial.

HIGH VELOCITY TESTS

During the high velocity runs no chlorine was generated. Prior to the run a fouling colony was purposely established on the surfaces of the control heat exchanger. A colony of several hundred live 1- to 2-mm-diameter barnacles was also established on a separate plastic insert strip 1/2 inch (1.27 cm) wide by 12 inches (30.5 cm) long , figure 10. The strip was placed at the inlet end of one of the control heat exchanger tubes at the beginning of the run. The No. 2 heat exchanger was free of fouling at the start of the run, but the brown residue accumulated from pres.'.ous periods of chlorination was purposely left on the tubes. An objective of the run was to determine wl ether an attached colony of marine organisms could be killed by seawater ^lowing continuously at typical shipboard condenser tube velocities 9 ft/sec (2.7 m/sec) maximum Also, it was desired to evaluate high velocity fouling of the previously chlorinated exchanger. Table 4 provides a summary of the results from this run and all subsequent runs that evaluated water velocity as a means of fouling control. The results indicated that approximately 50$ kill occurred on the tubes and tube sheets of the control exchanger. The smaller (1- to 2-mm) barnacles were killed by the high velocity; larger barnacles tended to survive. By comparison, the barnacles on the plastic strip all survived and grew slightly during the 2-week period. The plastic strip apparently affected flow characteristics sufficiently to reduce the velocity at the strip boundary layer by comparison with velocity in the other tubes. In no case was there evidence that water velocity was sufficient to actually sweep attached live or dead barnacles from the tube or tube-sheet surfaces. Heat exchanger No. 2 experienced no fouling attachment, although the brown residue film was gradually washed from the exchanger with operating time.

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During the final 6 weeks (weeks 4-20) of the high velocity tests, the control heat exchanger was cleaned, and both heat exchangers were run with high velocity seawater to observe whether any barnacle attachment might occur. The chlorinator was turned off during the run. Attachment of two barnacles was noted on the outlet end of the tubes of exchanger 2 which was operated at 4.0 to 6.6 ft/sec (1,22 to 2.02 m/sec) water velocity, The control exchanger was operating at 7-8 to 10.5 ft/sec (2.4 to 3.1 m/sec). The point of attachment was at the tube/tube- sheet joint, an area of relatively low velocity. As is apparent from figures 7 and 8, the tube ends were not machined flush with the tube sheet as would normally be done in a shipboard condenser or heat exchanger. Flush machining might have prevented such attachment. During the same operating period, a 3-inch (7.6-cm) PVC pipe in the test loop, which had much lower velocity water 1 ft/sec (0.3 m/sec) , suffered considerable fouling, figure 11.

EXTENDED SHUTDOWN

The next run was designed to evaluate the effect of shutdown of a condenser or heat exchanger system (zero water flow) on marine life growing in the system. A fouling colony was, there- fore, established on the control heat exchanger by running at low velocity for 2 weeks (weeks 20-22). The other exchanger was chlorinated at 0.5 ppm. The system was then shut down but was purposely kept filled with seawater. When the heat exchangers were opened 2 weeks later, all marine organisms (barnacles, serpulids, and encrusting bryozoans) were dead. There was a j noticeable sulfur smell, and a black film covered the surfaces of the controlled heat exchanger. The black silt layer was I apparently ?> result of sulfur-reducing bacteria that are abundant in the Fre.port area. The chlorinated exchanger remained free of fouling growth.

INTERMITTENT CH7X>RINATI0N TESTS

Two runs were conducted to determine the effectiveness of intermittent chlorine on the control of fouling in the titanium heat exchanger. The first run (26-30 weeks) was carried out at an average total chlorine level of 0.6 ppm for a period of 8 hours per day. For the second run (30-32 weeks), the chlorine concentration averaged 1.0 ppm with the chlorinator running for a period of 4 hours per day. Both intermittent injection pro- cedures were successful in preventing fouling. It should also be noted ';hat chlorine was not added over the weekend period of Friday evening to Monday morning. The control heat exchanger, by comparison, experienced barnacle, mussel, and amphipod attachment during these two runs.

PAS-75-29 11

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INTERMEDIATE VELOCITY TEST

During the last 4 weeks of the experiment (32-36 weeks), the effect of intermediate velocity on heat exchanger fouling was investigated. The control heat exchanger was run at k ft/ sec (1.2 ia/sec) velocity, while heat exchanger 2 was run at 2 ft/s c (0.6 m/sec) without chlorination. The heat exchanger running at 2 ft/sec (1.2 m/sec) had light barnacle, amphipod, and serpulid fouling, while the other exchanger showed no evidence of marine growth.

CONCLUSIONS AND RECOMMENDATIONS

Under the conditions conductive to marine fouling encountered in this investigation, chlorine effectively controlled fouling of titanium heat exchanger tubes, tube sheets, and water boxes at levels of 0.5 to 1.0 ppm of total chlorine. Inteimittent chlorination also was effective for preventing marine growth on titanium. A more infrequent dosage schedule than the 4 hours per day investigated might be possible, especially since the exchanger was able to be left unchlorinated over each weekend without suffering fouling. This must be tempered, however, by \ the fact that the intermittent chlorination tests were conducted , [ during a time of year when fouling is relatively light.

■ »

A more sophisticated method of chlorine dosage monitoring f' and control than was used in the experiments is a definite •' requirement. The large variance in chlorine level is an indi- cation that either the rapidly changing water characteristics '] created large shifts in chlorine consumption and/or the chlorine «i analysis technique was extremely inaccurate. In fact, the orthotolidine method is recognized as having considerable inaccuracy, depending upon the water being tested and the pro- cedure used for the test. It is, however, the most commonly used method of chlorine measurement today. Some new commercially available chlorine monitoring and control equipment look promising as a substitute method to obtain more accurate control of chlorine levels.

Chlorination had no detrimental effect on the titanium heat exchanger surfaces other than the deposition of the brown residue. It is possible that this residue might reduce the waterside heat transfer coefficient if allowed to accumulate over a length of time. Therefore, heat transfer tests need to be performed to verify that no appreciable reduction in heat transfer will occur with continuous or intermediate chlorination.

PAS-75-29 12

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Marine fouling problems can be minimized in titanium con- densers or heat exchangers by always operating at water velocities in excess of 4 ft/sec (1.2 m/sec) throughout the exchanger. High velocity 9 ft/sec (2.7 r./sec) water can kill small barnacles (1- to 2-mm size) already attached to a heat exchanger surface. The ability of higher velocity water to prevent attachment or actually kill barnacles already attached is very dependent upon whether uniform velocity conditions exist throughout the con- denser. Tube obstructions, dead end areas, and similar con- figurations are points where marine life can establish colonies even when there is high velocity flow through the tubes. Con- denser or heat exchanger design of waterside passages can, therefore, significantly increase or decrease the fouling char- acteristics of the system.

Complete shutdown of the heat exchanger for an extended time period appears to be 100$ effective for killing fouling organisms such as barnacles and for preventing initial attach- ment. How long animal organisms can live under stagnation conditions in a condenser would have to be established by further study. The time period is probably a function of the oxygen content and the nutrient characteristics of the par- ticular water.

In view of the findings, it is recommended that chlorination be considered for fouling protection in any titanium heat exchanger where seawater velocities of less than 4 ft/sec (1.2 m/sec) are anticipated in the tubes. For higher operating velocities, chlorination might also be considered as a possible deterrent to the gradual long-term buildup of fouling organisms in low velocity areas of the water boxes and tube sheets. Based upon the results obtained. Dr. D. C. Mangum, marinn biologist of Dow Chemical, recommended the schedule given in table 5 as a

guideline for 100% fouling protection.

TABLE 5 PROPOSED SCHEDULE FOR SHIPBOARD

USE OF CHLORINE AS AN ANTIFOULANT

Chlorination Schedule

(1 ppm residual)

First 2 Weeks

of Operation

Foulinq Conditions | Heavy

Coastal or Bay Waters

Moderate Gulf or

Temperate

Light Tropical

Continuous

Intermittent 8 hr/day

j 4 hr/day 1 hr/day

X

X X

X

PAS-75-29 13

For any proposed application of titanium heat exchangers, it would appear to be advisjiblj to review the operating char- acteristics of the exchanger and of the ship thoroughly before making a decision whether chlorination would be required. Every effort should be made to assure that the design of the heat exchanger and the inlet piping does not create possible stagnation areas where marine organisms can attach.

Actual installation of prototype titanium heat exchangers aboard ship is probably the best means of establishing firm shipboard fouling guidelines and expected fouling patterns.

TECHNICAL REFERENCES

1 - Williams, W. L., "The Corrosion and Mechanical Properties of Titanium and Zirconium at Normal Temperatures," (text is unclassified) USNEES Rept C-3395* C-3501B (9 Feb 1950)

2 - Bomberger, H, B., et al, "Corrosion Properties of Titanium in Marine Environments," Journal of the Electrochemical Society, p. 443-447 (Sep 1954) , ~~~~~

3 - White, G. C, Handbook of Chlorination, New York, N. Y., Van Nostrand Rheinhold Co. (1972)

4 - "Methods of Controlling Marine Fouling in Seawater Desalina- tion Plants," Dow Chemical Co., Office of Saline Water Contract 14-30-2829 (Apr 1973) i

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PAS-75-29 14

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1 - Seawater Feed 2 - Pump and Motor 3 - Electrolytic Chlorinator 4 - Chlorinated Heat Exchanger 5 - control (Unchlorinated) Heat Exchanger

Figure 1 Overall View of Fouling Test System

F\S-75-29

OVERBOARD

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DIFFERENTIAL PRESSURE GAGE

IFLOWMETER

14 VDC POWER PACK

A-i TITANIUM CONDENSER

DRAIN SEAWATER

INLET

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A TITANIUM CONDENSER

CHLORINE GENERATOR

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Figure 2 Piping Layout for Fouling Test

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Figure 3 Titanium Heat Exchanger

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HEADER JMLET TU6E SHEET

TITANIUM HEAT EXCHANGER

G- 5/6 0.0. TITANIUM T'JBES 20 8WG

DRILL 6 HOLES (sec DETAIL olx-

/ mm 0ÄH.L AND UP

FOR ' W*T

"7" 5 I ORSLLSHOLES f 7 \ (StF, DETAIL £)

► B SECTION B-B INLET TUBE SHEET

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NOTE ALL 0IM£*S.ON5 ARC GIVEN IN INCHIS

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DETAIL "E" (Full SCO!«) (Ti 6AI-4V)

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V BEGAN TEST RUN

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D UNITS INSPECTED AND CLEANED

CONTROL HEAT EXCHANGER (NO. I)

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M/SKC I FT/SEC

TIME, WEEKS

16 20

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CHLORINATED HEAT EXChANGER (NO. 2)

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NO OPERATION (PUMP MOTOR FAILURE)

Figure 6 Heat Exchanger Operating Schedule

PAS-75-29

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Fiqure 7 - Barnacle Fouling of Titanium Heat Exchanger after 2 Weeks at

1 ft/sec ;0.5 m/sec) Seawater Velocity

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Pi, jure - Close-up of Barnacle Fouling in T it ali i i1it Tubes after ? Weeks at

1 ft./sec '0.7; r/sec Seawater Velocity

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Figure 9 - Typical Unfouled Tube and Tube-Sheet Surfaces Experienced with

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Figure 10 - Barnacle Growth on Heat Exchanger Plastic Insert

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Figure 11 - Barnacle Growth Inside PVC pioing ?t 1 ft, sec 0.3 m/sec

Seawater Velocity

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