fuelling frugal innovation in industry

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    by

    GAGAN GOEL & SHOBHITAGARWAL

    DEPUTY MANAGER

    AONLA UNIT, BAREILLY

    FUELLING

    FRUGAL INNOVATIONIN INDUSTRY

    Technical Seminar on

    Engineers Day-2013Institute of Engineers, Bareilly Chapter

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    Dr. R. A. Mashelkar

    What is Frugal Innovation?

    Frugal innovation or frugal engineering is theprocess of reducing the complexity and cost of a good

    and its production.

    Frugal innovation responds to limitations in resources,

    whether financial, material or institutional, and turnsthese constraints into an advantage through

    minimizing the use of resources in development,

    production and delivery.

    Frugal innovation results in dramatically lowercostproducts and services & a better way of doing a job.

    Successful frugal innovations are not only lower in

    cost, but outperform the alternative, and can be made

    available at large scale.

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    Value forMoney

    Value forMany

    Dr. R. A. Mashelkar,

    President of Global Research Alliance,

    (former Director General of the Council of

    Scientific & Industrial Research (CSIR))

    Frugal Innovation =

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    Drive the

    economicgrowth of

    nations

    Improve

    people welfareSustain

    Organizations

    Why Frugal Innovation is

    Important?

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    FRUGAL Innovation in India ..

    Jugaad is a colloquial Hindi wordthat roughly translates as aninnovative fix; an improvised solutionborn from ingenuity and cleverness.

    Jugaad Innovation is about: Less,but better it concentrates on the

    essential aspects and not burdenedwith non-essentials

    back to purity,back to simplicity.

    Jugaad applications include findingnew uses for everyday objectsIndian kitchens are replete withempty bottles reused as ad-hoc

    containers for dried legumes orcondimentsor inventing newutilitarian tools using everydayobjects, like a makeshift truckcobbled together with a dieselengine slapped onto a cart(makeshift vehicles).

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    FRUGAL INNOVATION - EASY COST

    EFFECTIVE DAILY SOLUTION

    MittiCool Fridge Jugaad Espresso Coffee MakerWashing Machine without Electricity

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    Believe it or NOT Indian Jugaad is

    MOST HAPPENING Thing for the world

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    MANAGING INNOVATION A WESTERN

    APPROACH

    In the 20th century, as North American andEuropean economies expanded, Westerncorporations began to institutionalize theirinnovation capabilities, creating dedicated R&Ddepartments and standardizing the businessprocesses needed to take their ideas to market.

    They focused on managing innovation, just asthey managed any other business activity. Thisindustrialization of the creative process led to astructured approach to innovation with thefollowing key characteristics: big budgets,standardized business processes, andcontrolled access to knowledge.

    But this structured innovation approach, whichhelped Western firms become highly successful inthe second half of the twentieth century, has threeclear limitations in the fast pace and volatility ofthe twenty-first century:

    1. The structured approach is too expensiveand resource consuming

    2. The structured approach lacks flexibility3. The structured approach is elitist and

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    Natural ResourcesCapital

    LandSkilled Labor

    Infrasctructure

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    Diversity- - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -

    Geographic Cultural Social Economic Biological

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    InterconnectivityCloud Computing Mobile Social Media

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    Technological

    Market

    Competitive

    Velocity- - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -

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    Emerging Markets

    More ConsumersGreater Strain on Existing Resources

    Frugal Innovation

    Globalization- - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -

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    THE SIX PRINCIPLES

    OF FRUGAL INNOVATION

    Find more opportunity in adversity.

    Do more with less.

    Think and act flexibly. Keep it simple.

    Include the margin.

    Follow your heart.

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    IFFCO Aonla

    Producing 1.21 lacs Bags having 50 kg

    Urea.

    Plant is continuously running &

    DOWNTIME is not desirable. 1 day DOWNTIME cost = Production Loss

    of Rs.6 crore + Shutdown & Startup

    Energy Loss of Rs.2 crore.

    Shutdown Planning is a mega activity inthe continuous running plants so that all

    activities can be completed within a

    specified span of time.

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    A Brief of IFFCO Aonla

    Certified for following Management System

    ISO-9001 Quality

    ISO-14001 Env ironm ent

    OHSAS-18001 Helath & SafetyISO-16001 Energy

    ISO-26001 CSR

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    " IFFCO Employees Suggest ion

    Scheme"

    IFFCO has always encouraged frugal innovation, novel ideasand creative thinking on the part of employees.

    "IFFCO Employees Suggestion Scheme" is yet another step

    towards utilizing employees creativity and potential for improved

    organizational performance.

    The Scheme is aimed towards an objective of providing a well-structured and formal platform for nurturing, supporting and

    rewarding creative ideas of employees.

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    Computerization

    http://localhost/var/www/apps/conversion/tmp/scratch_1/SuggScheme_Eng.pdf
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    Growth of IFFCO Suggestion Scheme

    969924 897

    156

    802

    1133

    28

    15750

    0

    200

    400

    600

    800

    1000

    1200

    2010-2011 2011-2012 2012-2013

    Number of Employees

    Number of Suggestions

    Received

    No. of Suggestions

    Impleented

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    THE JOB: Inspection of inside wall of Ammonia Convertor which involved

    NDT (DP/UT/Hardness/etc) of 6 nos. of C-Seam weld joints and 5 nos. of

    L-Seam joints.

    To reach different levels of C-seam and L-seam joints, it is necessary to have

    scaffoldings inside the vessel of about 26 meters height and 3.0 metersdia.

    It involves 150M3 ofscaffolding which takes 02 days to erect and 01 days to

    dismantle. Additionally 01 day required for Inspection .

    Reduction in inspection time of Ammonia

    Converter (S-200 ) by providingprefabricated multi-storied inspection cage.

    FRUGAL INNOVATION-1

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    Conventional

    Scaffolding

    Basket support

    ring

    FRUGAL INNOVATION-1

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    In nut shell Reduction in scaffolding activity and

    inspection activity can reduce the Shutdown

    time by 3days to match production targets.

    Something very different and innovative idea

    can only help in this situation.

    FRUGAL INNOVATION-1

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    The Idea struck was :

    Why not to Fabricate and use amulti-storied platform to help the

    Inspection activities inside the

    Ammonia Synthesis Convertor

    Pressure Vessel.

    This will allow inspection of all C-

    seam joints of all 6-levels at a time

    i.e. Inspection time is reduced.

    More safe

    Installation and removal is one

    houreach only.

    FRUGAL INNOVATION-1

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    FRUGAL INNOVATION-1

    This scaffolding structure was actually

    erectedinto vessel in 1 hour instead of2days.

    Inspection was carried out through out

    the vessel in a time in 12 Hrs instead

    24hrs due to easy access.

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    FRUGAL INNOVATION-1

    The scaffolding was de erectedfrom

    the vessel in 1 hour instead of 1 day The whole inspection activity

    completed with in 16 hrs instead of 4

    days

    Net saving of 3 days

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    This innovative idea Reduced shut down time by 3days

    9,090 MT More Urea Production (@ 3030 MT Per day)

    More profit on the production approx.Rs. 1.5 Crore.Other Benfits :

    The fabricated structure can be utilised for such

    applications with slight modification

    The used material can be reclaimed and re-utilised.

    FRUGAL INNOVATION-1

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    REDUCTION IN REPAIR TIME OF

    Syn-loop boiler (E-1501) Ammonia-1

    IMPORTANCE:Use waste heat of syn gas coming from

    converter (Exothermic Reaction).

    Produce HP steam

    OBSERVATION:Tube leakage.

    EFFECT:Boiler steam conductivity running higher

    than normal and Loss of syn gas.

    FRUGAL INNOVATION-2

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    Repair Procedure with

    Hydro Testing

    Shell has to be Hydro tested at max at 80

    kg/cm2 to find out leaks and than carried out

    repair. If repair having some defect repeat

    hydro test in iterations till all leak points

    repaired.

    Tubes were plugged with Inconel plugs and

    welding was done with TIG process using ErNi Cr3 filler wire of 1.6 &2.4 mm size. Tube to

    tube sheet leakage was also repaired by

    welding overlaying process.

    FRUGAL INNOVATION-2

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    Difficulty in hydro testing Procedure:

    In hydro test DM water was being used and after leak detection this

    water required to be drained from shell for leakage repairing.

    Complete cycle of one hydro test (Filling, pressurization and

    draining) takes min. 10 hrs

    Leakage repairing was done by TIG welding, which require clean

    and dry surface. This condition was not achieved in presence of

    water, which results difficulty in welding.

    Note : Through this procedure more time required and also

    difficulty in welding.

    FRUGAL INNOVATION-2

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    PNEUMATICALLY LEAK DETECTION

    INSTEAD OF HYDROTEST,WAS

    CONCEPTUALISED TO

    SAVE TIME & WATER FREE WELD

    REPAIR

    FRUGAL INNOVATION-2

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    New SYN LOOP BOILER TESTING ARRANGEMENTSynthesis Loop Boiler Pneumatic Testing Scheme

    AMMONIA PLANT

    UREA PLANT

    MOTOR

    COMP

    K-3

    Passivation Air Comp.

    for Bimetallic Stripper

    E-1501Synthesis loop

    Air (80 kg/cm )

    To Bimetallic

    Stripper

    Pr. Gauge

    FRUGAL INNOVATION-2

    FRUGAL INNOVATION 2

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    Repair Procedure

    with Pneumatic Testing: Shell was PNEUMATICALLY tested at 3kg/cm2, 7.0 Kg/cm2,

    25 kg/cm2 and max at 62 kg/cm2 and repair was carried out in

    each iterations.

    Tubes were plugged with new modified Inconel plugs and welding

    was done with TIG process using Er Ni Cr3 filler wire of 1.6 &2.4 mm

    size. Tube to tube sheet leakage was also repaired by welding

    overlaying process.

    During last S/D -2012, 04 nos. leaky plugs were removed by grinding

    and new plugs provided and welded. Tubes to tube sheet weld joint

    were repaired by welding.

    FRUGAL INNOVATION-2

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    BENEFITS

    1.Time saving

    2. Defect free welding

    The above suggestion has given a

    Tangible Benefit of 3,00,00,000/- (one time)and other benefit like reduction in overall

    plant shut down period.

    FRUGAL INNOVATION-2

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    Primary Reformer - Ammonia Plant

    FRUGAL

    INNOVATION - 3

    Use of Special Jig for

    handling more than one

    catalyst Tube

    AB Cell

    CD Cell

    View

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    Earlier approach

    Single catalyst Tube removal& insertion time was approx.

    30 min. (One crane operation)

    Total 288 Crane operations

    would be required by

    conventional method.CatalystTube removal & insertion was

    done on single tube basis

    (conventional method).

    Total time taken for tube

    removal & insertion comes

    out

    = 6days

    = 288x30 min= 8640 min

    FRUGAL INNOVATION-3

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    The Idea struck was :

    Why not to Fabricate and use

    fixtures/clamps for removal &

    insertion of two or more Catalyst

    tubes.

    This will reduce the total no of crane

    operation and would reduce total

    time taken for removal & insertion of

    catalyst tube.

    More safe.

    Optimum utilization of Crane

    capacity.

    Conventional Fixture for singletube Removal/insertion

    New Fixture for twotubes Removal/insertion

    New Fixture for threetubes Removal/insertion

    FRUGAL INNOVATION-3

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    IMPLEMENTED APPROACH The Suggestion was

    implemented by

    fabricating new Jigs

    & Fixtures in house

    using the scrapstructural & piping

    material.

    FRUGAL INNOVATION-3

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    Sr

    no

    Activity Conventional

    Fixture for Single

    catalyst tube

    New Fixtures for two or

    three catalyst tubes

    %

    Reduction

    1 Total crane

    operation

    (Usage of

    Crane)

    288 50-AB Cell

    74-CDCell

    60%

    2 Total time

    taken

    =288x30min

    =6 days

    =124x50* min

    =4.3 days

    28.3%

    (1.7 Days

    saved)

    3 Safety Groove for Two part

    ring But no Bolting

    Stopper cleats for two

    part ring and fixtures wereBolted

    More safe

    Note: *Extra time for single crane operation with new fixtures wasdue to Bolting & dismantling of clamps, difficulties in alignment &removal of old catalyst tubes.

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    can only help in such situations

    Out of box thinking

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    CONVERT YOUR IDEAS

    INTO ACTION THROUGH

    FRUGAL INNOVATION