ke6316 md-11f sha accident 신 지 수신 지 수. general information date : 1999. 4. 15 place :...
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KE6316 MD-11F SHA ACCIDENT
신 지 수
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General Information
• Date : 1999. 4. 15• Place : SHA • Injury to Person :
– 8 (3 crews, 5 civilians) killed – 4 seriously injured– 36 minor injured
• Damage to Airplane : Hull Loss• A/C Type: MD-11F• Year Built: 1992• Flight Time: 28,347 hrs• Flight Cycle: 4,463• Engine: PW4460 x 3
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Conclusion of Accident Investigation
• CAAC/KCAB/NTSB joint investigation concluded the probable cause of the accident for:
– Flight Crew’s failure of altitude awareness– Confusion between Meter & Feet unit in ATC
instructed Altitude– Insufficient Pre-departure preparation
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Findings
• No Indication of : (No finding actually)– In-flight Fire– In-flight breakage of airplane– System Failure– Failure in Cargo loading– Bomb or DG Explosion in flight – Engine Failure
• F/O’s wrong spoken word• Lateral deviation of Instrument departure• Dive to the ground from 4500 feet in 16 second • Crew expressed difficulty in control
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CAAC’s conclusion basically based upon:
• Wrong spoken word of altitude unit• Stabilizer Trim moved toward AND • Simulator (FSB in Long Beach)
evaluation• No Departure Briefing • Not enough operational experience in
SHA
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Lack of Factual Evidences
• FDR loss• Difficulty in defining position of flight
control related items• Difficulty in Corroboration • No indication of system failure
– No warning or alerts of system failure in CVR
– No indication on the wreckage
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Factual Evidence vs Situational Evidence
• Both requires :– Correlation– Corroboration– Correction– Ask 100 times “Why?”
• Stronger supporting facts needed for analysis by situation evidence
• Both must be feasible : “Make sense!”
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Other View
• KAL analyzed different point of view:– Cockpit Noise Analysis including
Engine Noise level– Flight Path Analysis – Focused on other clues
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Other Important Clues
• Difficulty in Pitch Control• Unidentified Noises• Abrupt Nose up before Dive• Contamination in Elevator control
valve
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Similar Incident or Accident worldwide
• FeDex crash land in Newark• JAL pitch oscillation• CAL abrupt pitch oscillation
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Can human make that kind of control?
• Dive to crash from 4500ft in 16 second with max 20 degrees nose up to max 50 degrees nose down– Physical limitation of human – Engine Noise(Throttle movement)– Pilots’ call out– Continuous Trimming down(beginning
time)
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Investigation should be further reviewed
• CVR analysis• A/C Stability & Pitch Control• Negative-G load stall • Engineering Simulation• EMI(Electro-magnetic Interference)• Flight Path analysis• Reason of Lateral deviation
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Administrational Litigation In Progress
• Cargo Operation continues currently.
감사합니다 .