of a modern counterrotating unducted fan engine … · 2013-08-30 · of a modern counterrotating...

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:. 2J, CR-180869 N/ SA National Aeronautics and Space Adm_istratlon FULL SCALE TECHNOLOGY DEMONSTRATION OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST December 1987 by GE Aircraft Engines GE36 Project Department Cincinnati, Ohio 45215 Prepared for National Aeronautics and Space Administration UNjucrt q CA_,t _-r, lC;,lN,_ C'_NC/_I. rh, qJ-N_ l" .,T (".i::) 3"*(.' p Cq_L _£.c oncl,Js ,]__/07 07371S-, I These limitations shall be considered void alter two (2) years after date or such data. This legend shall be marked on any reproduction of these data in whole or in part. NASA-Lewis Research Center Contract NAS3-24210 https://ntrs.nasa.gov/search.jsp?R=19900000733 2020-04-08T18:32:32+00:00Z

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Page 1: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

:. 2J,

CR-180869

N/ SANational Aeronautics and

Space Adm_istratlon

FULL SCALE TECHNOLOGY DEMONSTRATIONOF A MODERN COUNTERROTATINGUNDUCTED FAN ENGINE CONCEPT

ENGINE TEST

December 1987

by

GE Aircraft Engines

GE36 Project Department

Cincinnati, Ohio 45215

Prepared for

National Aeronautics and Space Administration

UNjucrt q CA_,t _-r, lC;,lN,_ C'_NC/_I. rh, qJ-N_ l" .,T

(".i::) 3"*(.' p Cq_L _£.c oncl,Js,]__/07 07371S-,

I These limitations shall be considered void alter two (2) years after date or such data.This legend shall be marked on any reproduction of these data in whole or in part.

NASA-Lewis Research Center

Contract NAS3-24210

https://ntrs.nasa.gov/search.jsp?R=19900000733 2020-04-08T18:32:32+00:00Z

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CR-180869

N/ ANational Aeronautics and

S_)ace Administration

FULL SCALE TECHNOLOGY DEMONSTRATIONOF A MODERN COUNTERROTATINGUNDUCTED FAN ENGINE CONCEPT

ENGINE TEST

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FOREWORD

This report presents the results of engine tests and

a discussion thereof, as conducted by GE Aircraft Engines,

Cincinnati, Ohio. These engine tests were performed on

behalf of the NASA Lewis Research Center, Cleveland, Ohio,

under Contract NAS3-24210. The program was carried out

under the technical cognizance of Mr. R.D. Hager of the

Advanced Turboprop Project Office. The contract effort

was conducted at the Evendale Plant of GE Aircraft Engines

by the GE36 Project Department.

PRECEDING PAGE BLANK NOT FILMED

!

iii

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Page 7: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

TABLE OF CONTENTS

Section

1.0

2.0

3.0

4.0

ENGINE TEST SUMMARY

I. I SIGNIFICANT HARDWARE CHANGES AND MODIFICATIONS

1.2 OVERALL HISTORY OF UDF TM ENGINE TESTING

INTRODUCTION

2.1 ENGINE DESCRIPTION

2.2 INSTRUMENTATION

REVIEW OF UDF TM TESTING

3.1 FORWARD STATIONARY CARBON SEAL FAILURE

3.2 FORWARD TELEMETRY ANTENNA REPAIR

3.3 TELEMETRY SYSTEM TEMPERATURE PROBLEMS

3.4 STAGE 1 TURBINE BLADE FAILURE AND STALL EVENT

3.5 TURBINE BLADE DAMPER EFFECTIVENESS

3.6 SUBIDLE OIL LEAK PROBLEM

3.7 STATIONARY EXHAUST NOZZLE (CENTERBODY) REPLACEMENT

3.8 FAN BYPASS BLEED VALVE CALIBRATION

3.9 FAN BYPASS BLEED VALVE DIFFUSER FAILURE/REPLACEMENT

3. I0 PROPULSOR FAN-BLADE-LOSS EVENT

3.11 PROPULSOR FAN BLADE HISTORY AND TEST DATA

3.11.I Fan Blade Test History3.11.2 Fan Blade Test Data

3 12 POWER TURBINE FRAME STRESS

3 13 EFFECT OF VORTEX DESTROYER ON STRESS

3 14 EFFECT OF TEST SITE CHANGE ON STRESS

3 15 ROTOR LOCKUP AFTER SHUTDOWN RESULTING FROM FUEL LEAK

3 16 LOW/HIGH CYCLE FATIGUE TESTING

3 17 ROTOR-TO-ROTOR LOCKUP/PROPULSOR DISASSEMBLY AND REBUILD

3 18 MISCELLANEOUS HARDWARE STRESS DATA

3.19 OIL LEAK/GULPING PROBLEM

HEAT TRANSFER AND SECONDARY FLOW SYSTEM

4.1 MIXER FRAME HEAT TRANSFER

4.2 POWER TURBINE SECONDARY FLOW SYSTEM

V

'! ..... , .k ,* r TM - _- ....... -r ...... _i! . [;'_

1

6

7

II

II

18

19

20

20

20

32

37

51

52

52

52

57

6O

6O

6O

73

73

8O

85

85

85

99

101

II0

II0

117

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TABLE OF CONTENTS (Continued)

Section

7.0

8.0

9.0

4.3 POWER TURBINE HEAT TRANSFER

4.4 NACELLE VENTILATION

4.5 CENTER CAVITY VENTILATION

ENGINE SYSTEM DYNAMICS

BEARINGS AND SEALS

6.1 HARDWARE CONDITION

6.1.I Rotor Support Main Bearings

6.1.2 Inner Actuation Bearings

6.1.3 Actuation Tapered Roller Bearings

6.1.4 Fan Retention Bearings and Seals

6.2 MEASURED TEMPERATURES

6.2.1 Rotor Support Main Bearings

6.2.2 Fan Retention Thrust Bearings

PERFORMANCE

DATA SUMMARY

DATA REDUCTION METHODOLOGY

7.1

7.2

7.3 COMPARISON OF PRETEST PREDICTIONS AND REDUCED

TEST DATA

7.4 LCF CYCLIC TESTING AND RESULTANT DETERIORATION

7.5 DEFINITION OF PREFLIGHT TEST CYCLE

7.6 COMPARISON BETWEEN GROUND PRETEST CYCLES AND

REDUCED TEST DATA

7.7 PERFORMANCE SUMMARY

7.8 KEY RESULTS

ENGINE OPERABILITY

8.1 IPC STALL MARGIN

8.1.1 IPC Bleed Control System8.1.2 Control Threshold for Throttle Retard Rate

8.1.3 Maximum Allowable IPC Pressure Ratio Schedule

8.1.4 Final IPC Bleed Control Status

8.2 TRANSIENT TESTING EXPERIENCE

8.3 ENGINE TRANSIENT PERFORMANCE ANALYSIS AND PREDICTIONS

ENGINE CONTROL

Page

121

121

127

129

143

143

143

147

147

147

151

151

151

156

156

156

160

174

181

181

185

185

192

192

197

197199

199

2O2

202

208

vi

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TABLE OF CONTENTS (Concluded)

Section

10.0

II.0

12.0

13.0

14.0

9.1

9.2

9.3

9.4

BUILD 1 - ENGINE CONTROL TESTING

9.1.1 Speed Sensing Anomaly9.1.2 Pitch Control

9.1.3 Gas Generator Control

9.1.4 Throttle System

9.1.5 Engine Starting

9.1.6 Off-Engine Harnesses

9.1.7 Lube Oil Bypass

BUILD 2 - ENGINE CONTROL TESTING

9.2.1 Speed Control9.2.2 Duct Bleed

9.2.3 Transient Testing9.2.4 Control Parameters

9.2.5 Vibration System

9.2.6 Overspeed System

9.2.7 Reverse Testing

9.2.8 Control System Modifications

BUILD 3 - ENGINE CONTROL TESTING

Endurance Testing

Core Response Modifications

Reverse Thrust Testing

UPS (Uninterruptable Power Supply) Systems

Transient Testing

SUMMARY

9.3.1

9.3.2

9.3.3

9.3.4

9.3.5

NACELLE STRUCTURES

10.1 FAN BLADE AIRFOIL LOSS

10.2 STRAIN EVALUATION OF THE STRUT

10.3 ACOUSTIC FATIGUE

RESULTS

CONCLUSIONS

SYMBOLS/ABBREVIATIONS

REFERENCES

APPENDIX A - STEADY-STATE TEST DATA - BUILD 3

APPENDIX B - STRAIN DATA FOR THE STRUT

208

208

208

2O8

211

211

211

211

211

212

212

212

219

219

219

219

219

224

224

224

224

224

226

226

231

231

235

235

239

241

243

246

247

279

vii

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LIST OF ILLUSTRATIONS

I-I.

1-2.

I-3.

I-4.

2-I.

2-2.

2-3.

2-4.

2-5.

3-1.

3-2.

3-3.

3-4.

3-5.

3-6.

3-7.

3-8.

3-9.

3-10

3-11

3-12

3-13

3-14

3-15

3-16.

3-17.

3-18.

3-19.

Total Run Time at Various XN48, Times as of July 8, 1986.

Total Run Times at Various XN49, Times as of July 8, 1986.

Total Run Time at Various T46, Time as of July 8, 1986.

Run Time at Various Thrust Levels, Build 082-001/03 Only.

Cross Section of Unducted Fan Engine.

Cross Section of UDF TM Engine (Enlarged View).

UDF TM Engine at Peebles Test Site 4A.

UDF TM Engine at Peebles Test Site 4A.

UDF TM Engine at Peebles Test Site 3D.

Carbon Seal Assembly Fix.

Forward Telemetry System Support.

GE36 Telemetry System.

Telemetry System Scoop Designs.

Forward Telemetry Temperatures - Raw Data.

Forward Telemetry Temperatures - Normalized with TAM B.

Aft Telemetry Temperatures - Raw Data.

Aft Telemetry Temperatures - Normalized with TAM B.

Forward Telemetry Temperatures - Reverse Testing.

Aft Telemetry Temperatures - Reverse Testing.

Summary of Hardware Damage.

Turbine Blade IF Stress Trend.

History of Turbine Blade Response, Run to Thrust and Stall.

Turbine Blade Fix.

Power Turbine Blade Vibratory Response, Damper

Effectiveness - Stage I.

Power Turbine Blade Vibratory Response, Build I (Undamped)

Versus Build 2 (Damped).

Stage 1 Turbine Blade Response, Accel to 25,000 ibf Thrust:

February 4, 1986.

Stage 2 Turbine Blade Response, Accel to 25,000 ibf Thrust:

February 4, 1986.

Stage.3 Turbine Blade Response, Accel to 25,000 ibf Thrust:

February 4, 1986.

2

3

4

5

12

13

14

15

16

21

22

24

25

26

27

28

29

30

31

33

34

35

38

39

40

41

42

43

viii

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3-21.

3-22.

3-23.

3-24.

3-25.

3-26.

3-27.

3-28.3-29

3-30

3-313-32

3-333-34

3-353-36

3-373-38

3-39

3-40

3-41.

3-42.

3-43.

LIST OF ILLUSTRATIONS (Continued)

Stage 4 Turbine Blade Response, Accel to 25,000 ibf Thrust:

February 4, 1986.

Stage 6 Turbine Blade Response, Accel to 25,000 ibf Thrust:

February 4, 1986.

Stage 7 Turbine Blade Response, Accel to 25,000 ibf Thrust:

February 4, 1986.

Stage 8 Turbine Blade Response, Accel to 25,000 ibf Thrust:

February 4, 1986.

Stage 9 Turbine Blade Response, Accel to 25,000 ibf Thrust:

February 4, 1986.

Stage 10 Turbine Blade Response, Accel to 25,000 Ibf Thrust:

February 4, 1986.

Stage II Turbine Blade Response, Accel to 22,000 ibf Thrust:

January II, 1986.

UDF TM Engine Centerbody Separation Parameter, Cruise

Condition M = 0.72; 35,000; PT8/P 0 = 1.4.

UDF TM Engine - Redesigned Centerbody.

Bypass Bleed Valve Diffuser.

Redesigned Bypass Bleed Valve Diffuser.

Spar Schematic.

Total Run Until Fan Failure.

Original Fan Blade Airfoil Mechanical Design.

Improved Fan Blade Mechanical Design.

Stage 2 Fan Blades Engine Test History.

Fan Blade Structural Improvement.

Fan Blade Response Summary - ksi pp.

Stage I Fan Blade Response Summary.

Stage 2 Fan Blade Response Summary.

Fan Blade Response Summary - February 4, 1986 Maximum

Power Run (25,000 ibf Corrected Thrust).

Stage I Fan Blade Response, Accel to 24,000 ibf:

June 24, 1986.

Stage 2 Fan Blade Response, Accel to 24,000 ibf:

June 24, 1986.

Fan Blade Strain Gage Locations.

ix

44

45

46

47

48

49

50

53

54

55

56

58

61

62

63

64

65

66

67

68

69

70

71

72

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LIST OF ILLUSTRATIONS (Continued)

Figure

3-44.

3-45.

3-46.

3-47.

3-48.

3-49.

3-50.

3-51.

3-54.

3-55.

3-56.

3-57.

3-58.

3-59.

3-60.

3-61.

3-62.

3-63.

3-64.

3-65.

3-66.

3-67.

3-68.

3-69.

Fan Blade Response with Facility Fans Turned On.

Power Turbine Frames Vibratory Response Summary.

Power Turbine Frames Vibratory Response, Updated Scope

Limits Versus Site 4A Response.

Power Turbine Frames Vibratory Response, Stage 12 Component

Strain Distribution Test Results.

Power Turbine Frames Vibratory Response, Material HCF

Test Results.

Power Frame Vibratory Response, Build 3.

Fan Blades Vibratory Response, Effect of Vortex Destroyer.

Power Turbine Frames Vibratory Response, Effect of Vortex

Destroyer.

Fan Blade Response Comparison, Site 3D Versus Site 4A.

Power Turbine Frames Vibratory Response, Effect of

Site Change.

Suspected IGV/Spool Rub.

Low Cycle Fatigue Cycle.

IGV and 1-4 Inner Spool.

IGV Crack/Tear at Braze Joint (ALF).

Suspected Stage I Rub.

Stage One Blade Cracks at Leading Edge Root.

Aft Outer Flowpath Seals.

Midsump Seals.

Suspected Stage II Rub.

IGV and 1-4 Inner Spool.

Power Turbine OGV - Engine Test Data.

Power Turbine IGV - Engine Test Data.

Forward Outer Rotating Seal Response, Decel from 25,000

ibf Thrust: February 4, 1986.

Aft Outer Rotating Seal Response, Accel to 25,000 ibf

Thrust: February 4, 1986.

Outer Turbine Spool Response (1-4), Accel to 25,000 ibf

Thrust: February 4, 1986.

Outer Turbine Spool Response (7-11), Acceleration to

35,000 ibf Thrust: February 4, 1986.

Page

74

75

76

77

78

79

81

82

83

84

86

87

90

91

92

93

95

97

98

I00

102

103

104

105

I06

107

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LIST OF ILLUSTRATIONS (Continued)

Figure

3-70.

4-3.

4-4.

4-5.

4-6.

4-7.

4-8.

4-9.

4-10.

4-11.

4-12.

4-13.

4-14.

5-1.

5-2.

5-3.

5-4.

5-5.

5-6.

5-7.

5--8.

5-9.

5-10.

5-11.

5-12.

Inner Turbine Spool (6-11) Response, Accel to 25,000 Ibf

Thrust: February 4, 1986.

Mixer Frame Flows at Takeoff Power, Test Versus Predicted.

Mixer Frame Pressure Losses Comparison of Measured and

Predicted Pressures.

Mixer Frame Flowpath Static Pressure Distribution Takeoff

Power.

Mixer Frame Backflow Margin - Build 01 Engine.

Mixer Frame Backflow Margin - Build 02 Engine.

Mixer Frame Temperatures.

Power Turbine Secondary Flow Circuit.

Potential Forward Seal Problem.

Rotor Cavity Temperatures at Takeoff Power.

Power Turbine Temperatures Based on Analysis.

Spool Temperatures, Hot Day Takeoff.

Nacelle Temperatures Based on Test Data at Takeoff Power.

Forward Fan Blade Hub Temperatures; Hot Day Takeoff,

Mach= 0.0, Full Thrust.

Center Cavity Ventilation at Takeoff Power.

IPC One-Per-Rev Signature Comparison.

HPC One-Per-Rev Signature Comparison.

IPC One-Per-Rev Signature Comparison.

HPC One-Per-Rev Signature Comparison.

Subidle UDF TM One-Per-Rev Vibration Signature Comparison.

Subidle UDF TM One-Per-Rev Vibration Signature Comparison.

UDF TM One-Per-Rev Vibration Signature on 2-Minute Accel to

24,000 ib Thrust, Housing Vertical.

UDF TM One-Per-Rev Vibration Signature on 2-Minute Accel to

24,000 ib Thrust, Housing Horizontal.

Maximum Static Deflection.

Unbalance Forces Lineup in Vertical Plane.

Unbalance Forces Lineup in Horizontal Plane.

GE36 Demonstrator Engine 082-001/3 T/D 7-1-86 Time History

Plots at Ground Idle Power.

Page

108

111

112

113

114

115

116

118

120

122

123

124

125

126

128

130

130

132

132

133

133

135

135

137

139

140

141

xi

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LIST OF ILLUSTRATIONS (Continued)

_re

6-I.

6-2.

6-3.

6-4.

6-5.

6-6.

6-7.

6-8.

6-9.

6-10.

6-11.

6-12.

7-I

7-2

7-3

7-4

7-5

7-6

7-7

7-8

7-9.

7-10.

7-11.

7-12.

7-13.

7-14.

7-15.

7-16.

7-17.

7-18.

7-19.

Seal Cavity Closure.

Possible Running Condition with IR Spanner Nut Loose.

Disassembly Problem and Roller Corner Damage.

Problem Solution - Positive Nut Locking.

Gearbox Stackup Problem Causing Incorrect Loading of

Ball Bearing and Cap Looseness.

Bearing Housing Deflection.

Irregular Wear Pattern of Roller "Path."

Main Propulsor Bearings.

Main Propulsor Bearings, 2-Minute Accel to 24,000 ib Thrust.

Main Propulsor Bearings, 4-Minute Accel/Decel to 1200 rpm.

Forward and Aft Fan Hub Temperatures.

Forward and Aft Fan Hub Temperatures, Accel to Full Power.

Instrumentation for UDFm/F404 Demo.

Core Engine Temperature Ratio Versus Pressure Ratio.

IPC Stall Margin Versus IPC Corrected Flow.

Power Turbine Flow Function Versus Energy Function.

Power Turbine Efficiency Versus Energy Function.

UDF TM Thrust Coefficient Versus Power Coefficient.

Front Rotor Blade Angle Versus Core Engine Pressure Ratio.

Rear Rotor Blade Angle Versus Core Engine Pressure Ratio.

Corrected SFC Versus Corrected Thrust.

UDF TM Engine - Redesigned Centerbody.

UDF TM Engine Centerbody Separation Parameter.

UDF TM Engine - Core Plug Static Pressures.

Nozzle Flow Coefficient Versus Core Engine Pressure Ratio.

Corrected SFC Versus Corrected EPR Power Hook Evaluation.

Corrected SFC Versus Corrected EPR Power Hook Evaluation.

Wind Velocity Versus Wind Angle.

Corrected SFC Versus Corrected Thrust.

Corrected Thrust Versus Corrected Pressure Ratio.

Core Temperature Ratio Versus Control Pressure Ratio.

Page

145

145

146

146

148

150

150

152

153

153

155

155

158

161

162

163

164

166

167

168

169

170

171

172

173

175

176

177

178

179

180

xii

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Figure

7-20.

7-21.

7-22,

7-23.

7-24.

7-25.

7-26.

7-27.

8-I.

8-2.

8-3.

8-4.

8-5.

8-6.

8-7.

8-8.

8-9.

8-I0.

8-11.

9-1

9-2

9-3

9-4

9-5

9-6

9-7

9-8

9-9

9-10.

9-11.

LIST OF ILLUSTRATIONS (Continued)

IPC Efficiency Versus Control Pressure Ratio. 182

IPC Flow Versus Control Pressure Ratio. 183

IPC Flow Versus IPC Corrected Speed. 184

Compare Pretest Cycle Versus Posttest Cycle Versus Test Data. 186

Compare Pretest Cycle Versus Posttest Cycle Versus Test Data. 187

Compare Pretest Cycle Versus Posttest Cycle Versus Test Data. 188

Compare Pretest Cycle Versus Posttest Cycle Versus Test Data. 189

Compare Pretest Cycle Versus Posttest Cycle Versus Test Data. 190

IPC Operating and Stall Line Sea Level Static. 193

Steady-State IPC Operating Lines; 2,750 ft. 194

Steady-State IPC Operating Lines; 38,000 ft. 195

IPC Stator Schedule. 196

Predicted IPC APRS Usage During Throttle Decels; 2,750 ft. 198

Predicted IPC APRS Usage During Throttle Decels; 38,000 ft. 200

Maximum Allowable IPC Pressure Ratio. 201

Predicted IPC APRS Usage During Throttle Decels; 2,750 ft. 203

Predicted IPC APRS Usage During Throttle Decels; 38,000 ft. 204

Transient Testing Analytical Comparison with Updated

Transient Cycle Deck T/C from 97% Takeoff Thrust. 206

Transient Testing Analytical Comparison with Updated

Transient Cycle Deck Burst to 20,000 ib Thrust. 207

Fan Speed Sensor Segments. 209

Fan Speed Sensor Segments. 210

Duct Bleed System. 213

Throttle Chop Decels. 214

Throttle Chop. 215

Throttle Chop. 216

Throttle Chop. 217

Throttle Chop. 218

Reverse Thrust. 220

Reverse Thrust. 221

Reverse Thrust. 222

xiii

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LIST OF ILLUSTRATIONS (Concluded)

Figure

9-12

9-13

9-14

9-15

9-16

9-17

10-1.

Reverse Thrust.

PS3 Accumulator Configuration.

Throttle Burst.

Throttle Burst.

Throttle Burst.

Throttle Burst.

UDF TM Engine 082-001Accelerometer Definition.

223

225

227

228

229

230

232

xiv

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LIST OF TABLES

Table

1-1.

1-2.

1-3.

3-1

3-2

3-3

4-I

7-1

7-2

8-1

I0-I

10-2

10-3.

GE36 Test History - Engine 082-001, Build I/IA.

GE36 Test History - Engine 082-001, Build 2.

GE36 Test History - Engine 082-001, Build 3.

Power Turbine Vibratory Response Resolution.

GE36 HCF Cycle Count.

Turbine Blade Inspection Summary.

Power Turbine Secondary Flow (%W25), Takeoff Power.

Data Summary.

Chronology of the Acquired Data.

Significant Transients - GE36 Proof-of-Concept.

Vibration Response.

UDF TM Engine Mount Loads Due to Airfoil Loss.

UDF TM Engine Comparison of Mount Loads for

Airfoil-Out Event.

UDF TM Engine Airfoil-Out Event Comparison of Deflections.

Stress Data - Strut.

Page

8

9

I0

80

88

96

119

157

157

205

233

234

236

236

237

XV

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1.0 ENGINE TEST SUMMARY

This Engine Test Report covers the UDF TM (unducted fan) Engine 082-001

ground testing at the GE Aircraft Engines Peebles Test Facility and includes

Builds I through 3 of Engine 082-001. Note: A new build number indicates a

significant change in engine hardware.

The UDF TM engine successfully completed a ground-test program exceeding

100-hours duration. The basic concepts of the engine have been successfully

demonstrated. Some of the accomplishments are as follows:

• Full thrust (25,000 pounds corrected) demonstrated

• Full propulsor rotor speed demonstrated (1393+ rpm)

• Specific fuel consumption (sfc) was better than predicted; sfc

of < 0.24 ib/hr/ib was demonstrated

• Flawless operation of the F404 gas generator

• Counterrotation of structures, turbines, and fan blades

• Actuation system operation successfully demonstrated

• Control system operation successfully demonstrated

• New fan blade design successfully demonstrated

• Reverse thrust successfully demonstrated.

The UDF TM was ground tested at Peebles for a total run time of 100:51

hours. This was split between Builds I through 3 as follows.

Run Time Total

Build per Build Run Time

1 5:24 5:24

2 29:20 43:44

3 66:07 100:51

In Figures I-I through I-4, the engine run time is a function of Stage 1

propulsor fan speed (XN48), Stage 2 propulsor fan speed (XN49), exhaust gas

temperature (T46), and thrust, respectively. Thrust data were available for

Build 3 only. Note that on the plots of run time as a function of propulsor

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speed, there is a large amount of time spent in the ranges of 600 to 700 rpm

and 700 to 800 rpm. Most of this time was spent in the immediate vicinity of

700 rpm, which is idle for this engine. Also note that the vast majority of

time spent in the 1400 to 1500 rpm range was actually spent near 1400 rpm.

i.i SIGNIFICANT HARDWARE CHANGES AND MODIFICATIONS

Significant hardware changes and modifications which occurred during the

UDF TM ground test are listed below. A more detailed discussion is provided in

the sections enumerated.

Build I to IA

Forward stationary carbon seal and 2R bearing replaced

Build IA

Forward telemetry system antenna modified

Added pipe-elbow air scoops to exhaust nozzle to aid aft

telemetry system cooling

Build IA to Build 2

All propulsor turbine blades replaced (Stages I-4 and 6-11)

Propulsor turbine blade tip clearances increased

Damper pins added between all propulsor turbine blades

Spool distress repaired

Pipe-elbow scoops were replaced with aerodynamic air scoops

Leading edge plugs were installed in propulsor fan blades

Installed redesigned stationary exhaust nozzle (centerbody)

Installed hardware to solve subidle oil leak problem

Build 2

Propulsor Stage 2, No. 7 fan blade replaced after blade-out

Added additional holes to telemetry system air scoops

Installed compressor discharge pressure (PS3) accumulator

system

Installed redesigned fan bypass bleed valve diffuser

Section

3.1

3.4

3.4

3.4,3.5

3.4

3.3

3.11

3.7, 7.3

3.6

3.10

3.3

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Build 2 to Build 3

Installed redesigned propulsor Stages 1 and 2 fan blades

Installed improved PS3 accumulator system

Build 3

No significant changes

Postbuild 3

Replaced all propulsor Stage I turbine blades

Replaced three propulsor Stage II turbine blades

Added positive mechanical retention feature to IR bearing nut

Replaced IR and 2R bearings

Repaired IGV (inlet guide vane) - lip replaced with honeycomb

Drilled oil drain holes in propulsor

Borescope ports added to mixer frame to gain better

access to Stage 1 turbine blades

Replaced actuator control rods

Installed additional air scoops for cooling aft

telemetry system

1.2 OVERALL HISTORY OF UDF TM ENGINE TESTING

Tables I-I through 1-3 present an overall history of UDF TM testing.

Section

3.11

6.0

3.17

3.17

3.17

3.17

3.17

3.17

3.17

3.17

3.3

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Table I-I.

Date (1985)i

Aug. 29

Aug. 30-Sept. II

Sept. 14

Sept. 15-17

Sept. 18

Sept. 19

Sept. 20-26

Sept. 27

Sept. 28-0ct. 1

Oct. 2

Oct. 3

GE36 Test History - Engine 082-001, Build I/IA.

TRTi

0:02First Run to Idle; Broken Carbon Seal

Caused Internal Oil Leak Resulting in

a Rotor Unbalance; Caused a Turbine Rub

Which Cracked Some Stage II Turbine Blades

Engine Removed from Site; Carbon Seal and

2R Bearing Replaced

Build IA

Engine Returned to Test; Idle Achieved

Worked Instrumentation Faults

Mechanical Check-Out

Mechanical Check-Out

Reached Full Propulsor Speed

Modified Forward Telemetry Antenna

Reached 22,000 Ibf; Shutdown Due to

High Aft Telemetry Temperatures

Added Air Scoops to Exhaust Nozzle to

Cool Aft Telemetry System

Reached 24,000 ibf; Engine S/D Following

Stall (Stage I Turbine Blade Failure)

Engine Removed for Repair

0:II

0:14

1:10

3:43

5:24

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Table I-2. GE36Test History - Engine 082-001, Build 2.

Date (1986)

Jan. 30-31

Feb. 2-3

Feb. 5-8

Feb. 9

Feb. 17-18

Feb. 28

March 5

March 6-30

April I-2

April 3-7

April 8

April 18

April 19-23

April 24

Resumed Testing; Mechanical Check-Out;

Reached 22,000 Thrust

Testing With Facility Fans On; Fan Bypass

Bleed Valve Calibration; Bleed Valve

Diffuser Can Failure; Engine Trim Balance

(20,000 Maximum Thrust)

Repaired Instrumentation and Aft

Telemetry System

Telemetry System Check-Out (to 1200 rpm

Fan Speed); Started Down Power Calibration

Ran Twice to 24,000 Thrust; on 2nd 24,000

Pt. Lost Stage 2, No. 7 Fan Blade Shell

Engine Health Check - With New Blade

Reached 1200 rpm Fan Speed; 16,000 Thrust;

Tested with Vortex Destroyer

Turbine Frame Stress Investigation;

I000 rpm Maximum Fan Speed

Stress Survey; 1029 rpm Maximum Fan Speed

Moved Engine from Site 4A to 3D

Stress Survey; 1150 rpm Maximum Fan Speed

Added Additional Holes to Aft Telemetry

System Cooling Scoops

Reverse Testing/Cooling Scoop Testing

Control Verification; Control Fault Caused

Stage 20verspeed; Engine Shutdown

Installed PS3 Accumulator to Slow

Propulsor Accel Rate

Engine Test With PS3 Accumulator;

1150 rpm Maximum Fan Speed

Build 2

Run Time

3:38

9:49

13:28

15:16

16:30

20:36

22:55

25:44

26:22

28:30

29:20

TRT

9:02

15:13

18:52

20:40

21:54

26:00

28:19

30:68

31:46

33:54

34:44

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Table 1-3. GE36Test History - Engine 082-001, Build 3.

Date (1986)

June 20

June 23

June 24

June 25

June 26

June 29

June 30

July 1

July 3

July 4

July 4-7

July 8

Returned to Test; Achieved Idle

Reverse Testing;Mechanical Check-Out; 1270 rpmMaximumFan Speed

Mechanical Check-Out/Trim BalanceReached24,000 MaximumThrust

Trim Balance/Bleed Valve CalibrationReached18,000 Thrust

Bleed Valve Calibration/Trim BalanceReached23,000 Thrust

Bleed Valve Calibration; Reached19,000 Thrust

DownPowerCalibration; Shutdownfrom19,000 Thrust Due to Fuel Leak; AftPropulsor Rotor Locked up UntilEngine Cooled

DownPower Calibration; Reached24,000 Thrust;PerformanceOptimization Testing

PerformanceOptimization/VibrationSurvey/Trim Balance; Reached21,000Thrust Control Tests; Reached24,000 Ibf

Reverse Testing (to 850 rpm Fan Speed)

LCF Cycles (lO0)

Bodes; Reached 21,000 Thrust; Trim

Balance; Reached 22,000 Thrust;

Propulsor Rotors Locked Togetherafter a Normal Shutdown

End of Ground Testing at Peebles

Build 3

Run Time

0:16

0:45

2:07

4:33

8:18

I0:00

12:17

12:51

17:36

20:18

25:38

29:53

30:34

59:45

62:31

66:07

TRT

35:02

35:29

36:51

39:17

43:02

44:44

47:01

47:35

52:20

55:02

60:22

64:37

65:28

94:29

97:15

i00:51

IO

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2.0 INTRODUCTION

2.1 ENGINE DESCRIPTION

The UDF TM engine is a new aircraft engine concept that is based on an

ungeared, counterrotating, unducted ultra-high-bypass turbofan configuration.

This engine is being developed by General Electric to provide a high thrust-

to-weight ratio power plant with exceptional fuel efficiency for subsonic

aircraft application.

The engine encompasses the operational flexibility and fuel efficiency of

a two-spool core gas generator with the propulsive efficiency of a propeller

(moderate diameter and tip speed). The engine is based on an aft-mounted,

counterrotating power turbine that aerodynamically couples with a basic gas

generator engine and provides for direct conversion of the gas generator

engine power into propulsive thrust without requiring a gearbox or additional

shafting. The concept of counterrotating fan blades is being utilized to

capitalize on the full propulsive efficiency of this configuration; that is,

the exit swirl from the first blade row is recovered by the second row and

converted into propulsive thrust. The turbine transmits its power through two

counterrotating power turbine frames which, in turn, transmit power to the

UDF TM blades through the polygonal support rings which act as the primary-load

carrying support structure for the fan blades. This isolates the turbine

flowpath from out-of-round distortions from the fan blade loads.

The counterrotating turbine rotors, power turbine frames, fan blades, and

static structures are components which comprise the "propulsor" for the UDF TM

engine. Mounted in front of the propulsor is a gas generator engine which

provides the required gas horsepower. The gas generator is a modified produc-

tion F404 turbofan engine.

Figure 2-I shows a cross-sectional view of the UDF TM engine. An enlarged

cross section of the propulsor is presented in Figure 2-2. Figures 2-3 and

2-4 are UDF TM photos at Peebles Test Site 4A, and Figure 2-5 depicts a UDF TM at

Test Site 3D.

ii

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i5

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ORIGINAL PAGE

8LACK AND WHITE P_APH

Figure 2-5. UDF'M Engine at Peebles Test Site 3D.

160F _O_T'_)!"J'ALIT y

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The major design characteristics of the UDF TM engine are as follows:

Gas Generator

Model F404-GE-400

Type Low bypass turbofan

Fan 3-stage axial flow

Compressor 7-stage axial flow

Turbines

Low pressure One stage

High pressure One stage

Rotor speeds

Fan 13,270 rpm (100%)

Compressor 16,810 rpm (100%)

Maximum airflow Approximately 140 ibm/s

Thrust 16,000 ibf class

Thrust-to-weight ratio 8:1 class

Overall compression ratio 26:1

(maximum climb)

UDF TM Engine Propulsor

Maximum nacelle diameter 76.4 inches

Fan blade tip diameter 11.67 feet

Fan design point tip 780 feet/second

speed, physical (maximum

cruise; 35,000 ft; 0.80 Mach;

ISA)

Fan rotor speed 1393 rpm (100%)

Fan disk loading, class SHP/A 87 HP/ft 2

(maximum cruise; 35,000 ft;

0.80 Mach; ISA)

Fan blade radius ratio 0.415

Power turbine inlet temper- 1310 ° F

ature (SL, T/O, ISA +27 ° F).

The gas generator/propulsor combination produces an engine with a net

thrust of 25,000 pounds. Other significant design features which have been

incorporated into this engine are:

• Advanced unducted fan aerodynamics that incorporate custom-

tailored composite fan blades over an inner titanium spar that

17

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serves as the attachment mechanism to the engine for the fanblades.

Fully developed and available gas generator to provide the

necessary power for the engine.

DEC (digital electronic control) that provides overall engine

control by monitoring gas generator power and speed and propul-

sor speeds and pitch angles. The engine uses the existing gas

generator control and a separate propulsor control to minimize

development costs without sacrificing control flexibility.

Hydraulic/mechanical actuation system enabling setting the fan

blade pitch angle of the two fan blade rotors either together

or differentially; this system is driven by the control system.

Modular assembly of the gas generator and propulsor.

Individually replaceable propulsor fan blades with the engineinstalled on the aircraft or test stand.

2.2 INSTRUMENTATION

The UDF TM instrumentation consists both of static and rotating instrumen-

tation, with the rotating instrumentation being read out by telemetry on the

rotors. Static instrumentation includes temperature, pressure, kulite, strain

gage, and accelerometer instrumentation on the engine, pylon, and nacelle.

Rotating instrumentation includes temperature, pressure, and strain gage

instrumentation on the counterrotating rotors. Detailed information on UDF TM

instrumentation is contained in the Instrumentation Plan (Statement of Work

Paragraph 4.2 of Contract No. NAS-24210). Included in this is Drawing No.

4013341-034, which shows the engine cross section with the location of engine

instrumentation and the corresponding parameter names. Reference GE36 Second

Ground Test TPS No. MA-0004 for a detailed description of the instrumentation

system and for a list and description of all parameters.

18

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3.0 REVIEW OF UDF TM TESTING

The following significant events, data points, and problem areas from

UDF TM testing will be expanded upon in the indicated sections:

Builds

Involved Section

Forward stationary carbon seal failure 1 3.1

Forward telemetry antenna repair I 3.2

Telemetry system temperature problem

(includes reverse thrust test data) 1,2,3 3.3

Stage I turbine blade failure and stall event I 3.4

Turbine blade damper effectiveness 1,2,3 3.5

Subidle oil leak problem 1,2 3.6

Stationary exhaust nozzle (centerbody) replacement 1,2 3.7,7.3

Fan bypass bleed valve calibration 2,3 3.8

Fan bypass bleed valve diffuser failure/replacement 2 3.9

Propulsor fan-blade-loss event 2 3.10

Propulsor fan blade history and test data 1,2,3 3.11

Power turbine frame stress investigation 2 3.12

Effect of "vortex destroyer" on stress 2,3 3.13

Effect of test site change on stress 2,3 3.14

Rotor lockup after shutdown resulting from fuel leak 3 3.15

LCF/HCF (low cycle fatigue/high cycle

fatigue) testing 1,2,3 3.16

Rotor-to-rotor lockup/propulsor disassembly and

rebuild 3 3.17

Miscellaneous hardware: stress data 1,2,3 3.18

Oil leak/oil gulping problem 2,3 3.19

Heat transfer and secondary flow system 1,2,3 4.0

Engine systems dynamics 1,2,3 5.0

Bearings and seals 1,2,3 6.0

Performance 1,2,3 7.0

Engine operability 1,2,3 8.0

Engine control 1,2,3 9.0

Nacelle structures 1,2,3 I0.0

19

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2O

3.1 FORWARD STATIONARY CARBON SEAL FAILURE

After the first engine start, the engine was shut down due to a low oil

level warning. Carbon seal pieces were found in the propulsor scavenge

screens. The engine was removed from the test site, and the propulsor was

separated from the gas generator. After separation, it was found that the

forward stationary carbon seal was damaged. It was determined that the seal

was damaged during assembly. The 2R bearing was also found damaged, this due

to carbon seal debris. New hardware was added to the engine to help guide the

propulsor rotors together to avoid any damage to the seal (Figure 3-I), which

was completely replaced with new hardware, along with the 2R bearing. The

propulsor was remated with the gas generator with no problems, and the engine

was put back on test. There were no oil leaks when the engine tests resumed.

While running the engine with the damaged carbon seal, the resulting

internal oil leak caused an unbalance in the rotors. This unbalance caused

the Stages 7, 9, and II propulsor turbine blades to rub hard against the inner

6-11 spool. Twenty-two Stage II blades were found to have cracks in the root.

It was decided to not replace these blades but to closely monitor their stress

levels.

3.2 FORWARD TELEMETRY ANTENNA REPAIR

Operational problems with the forward telemetry system were caused by

insufficient clearance between the static and rotating forward telemetry

antenna components. These components were modified to increase the cold run-

ning clearance from 0.135 to 0.250 inch, as diagrammed in Figure 3-2.

3.3 TELEMETRY SYSTEM TEMPERATURE PROBLEMS

Problems with the telemetry system, due to high temperatures, resulted in

design changes to increase cooling. Cooling scoops were added to the rotating

exhaust nozzle to bring in additional ambient air to cool the telemetry system

(especially that of Stage 2). Prior to the addition of cooling scoops, there

were flush vent holes in the exhaust nozzle. The following summarizes the

design changes:

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Run Time With

ConfigurationConfiguration

No Scoops - flush holes (0.468-inch diameter) in 3:43 hr

exhaust nozzle, 60 total. Build I; August 29 to

September 27, 1985

Data Symbol: None

Pipe Elbow Scoops - with 0.375-inch diameter 1:41 hr

openings, 30 total. Build I; October 2, 1985

Data Symbol: Pipe

Aerodynamic Scoops - with 0.500-inch diameter 25:44 hr

openings, 30 total. Build 2; January 30 to

April 2, 1986

Data Symbol: Aero

Modified Aerodynamic Scoops four 0.188-inch diameter 69:43 hr

holes added to side of scoops, 30 total. Build 2;

April 8 to 24, 1986. Build 3; June 20 to July 8, 1986

Data Symbol: Mod Aero

The addition of four holes to the side of the scoops were an attempt to

increase flow to the telemetry system during static ground testing. Sixty of

the modified aerodynamic scoops will be used for flight test. Figures 3-3 and

3-4 illustrate the telemetry system and cooling scoop designs.

Figures 3-5 through 3-8 show both raw telemetry temperature data and data

normalized with the ambient temperature (TAMB). The data was normalized due

to the large variation in ambient temperature which has a direct effect on the

telemetry temperatures. Note that temperatures recorded during Configuration

3 were cooler than those of Configuration 4. This shows the effect of ambient

temperature on the telemetry temperatures. Also during Configuration 4, there

was more test time and more time at power which would tend to increase temper-

atures. Also note that there is no data for the first two configurations for

Stage i; the thermocouple was not reading at those times. The telemetry

temperature limit set during ground testing, after the first configuration,

was 300 ° F.

During reverse thrust testing, Stage 2 telemetry temperatures increased

throughout the time the engine was in reverse. Figures 3-9 and 3-10 show the

telemetry temperatures during a reverse thrust cycle. This was the fifth of a

series of consecutively run reverse cycles.

23

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30

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Figure 3-i0. Aft Telemetry Temperatures - Reverse Testing.

31

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32

3.4 STAGE i TURBINE BLADE FAILURE AND STALL EVENT

Sequence of Events

• Engine operating on point at takeoff power (24,000 ibf), 1,350

rpm propulsor fan speed for 4 minutes

• Stage 1 turbine blade failure: high cycle fatigue (first flex)

cracking at blade root resulting in aft lean of blades

• Contact of Stage 1 blades with Stage 2

• Reduction of Stages I and 2 flow area

• IPC stall

• Engine stopcocked about 1.5 seconds after stall initiation

• Rotor axial excursion

• Secondary damage to remaining stages resulting from failure of

Stage I

• Additional rubs experienced by Stages 7, 9, and II

• Fast coast-down

• Rotor-to-rotor lockup.

Figure 3-11 shows a diagram summarizing the hardware damage.

Results

During testing, prior to the stall, significant first flexural vibratory

response had been observed on all stages of power turbine blading (Figures

3-12 and 3-13). Teardown revealed significant damage to Stage I. Several

blades had large leading edge root cracks and were leaning aft toward Stage 2.

One local segment of blades was buckled aft into Stage 2. All Stage 2 leading

and trailing edges, as well as all Stage 3 leading edges, were bent circum-

ferentially and severely rubbed. Stages I, 7, 9, and 11 exhibited severe tip

rub. While Stages 7, 9, and II had rubbed previously during Build No. I due

to oil leakage past a broken carbon seal, the poststall rubs were more severe.

Stage 4 had very light tip rub only at the trailing edge. Stages 2, 3, 6, and

8 exhibited no tip rub. Stage I0 rubbed only one blade, which was bent at the

platform. Stages 7, 9, and II had several bent airfoils. The rotor inner

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spools exhibited local burn spots at Stages I, 7, 9, and 11 rub locations,

with cracking evident at Stages 7 and II. Domestic object debris damage was

confined to the power turbine flowpath. Nicks and dents were significant only

on the forward turbine blade stages. The power frame and OGV (outlet guide

vanes) airfoils exhibited only minor debris damage.

Metallurgical evaluation of the Stage 1 blades found root leading edge

cracks on 117 of 124 airfoils. However, none of the airfoils were completely

separated. Crack lengths varied from approximately 0.02 to 1.2 inch. SEM

(scanning electron microscopy) revealed evidence of high cycle fatigue along

the entire fracture surface. Evidence of root fatigue cracking was also found

on Stages 2, 4, 6, and 11. Stages 7 and 9, and the one bent Stage I0 blade,

were found to have tensile cracks at the root braze joints and tensile tears

in some of the platform braze joints. Local burn spots on the spools showed

evidence of severe overtemperature of the Inco 718 substrate. Four locations

at Stage II and one at Stage 7 were confirmed cracked.

Posttest review of recorded data indicated stable engine operation while

sitting on point until approximately 0.5 to 1 second prior to the stall. At

that time, propulsor speed started dropping slowly while the control increased

fuel flow to compensate, and vibratory response on the forward turbine blade

stages showed a sudden increase.

Conclusions

Based on the responsiveness of all stages of power turbine blading at

first flexural frequency, it is concluded that the blade and spool design con-

figuration did not provide effective dovetail Coulomb damping as anticipated.

Hardware condition indicates that the Stage I blades were cracked to varying

degrees prior to stall and that these cracks propagated in high cycle fatigue

while sitting on point on October 2, 1985. As the cracks grew, the blades

leaned further aft until one or more contacted Stage 2, causing the slow drop-

off in propulsor rotor speed prior to the stall. Contact with Stage 2 rolled

the leading edge, resulting in a sudden reduction in power turbine flow func-

tion. The reduction in flow function caused the F404 gas generator to stall.

The remainder of the damage was secondary during the rapid shutdown.

36

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Corrective Action

All power turbine blades were replaced for Build 2. Spanning across

adjacent blades, coulomb dampers (in the form of Ren4 41 pins) were designed

for all stages of blading as illustrated in Figure 3-14. Effectiveness of the

damper design has been substantiated by component rig spin ("whirligig") and

bench wear tests. Although no evidence of fatigue was indicated for the power

frames, dampers were also added to Stage 12 as a precaution due to a predicted

first flexural response with the outlet guide vane passing frequency. Strain

gages have also been added to the Stages 5 and 12 power frame airfoils for

Build 2.

Low cycle fatigue and crack growth analyses of the spools indicate that

they have sufficient life capability for the remainder of planned testing.

The spools have been weld repaired and the rub coats stripped and reapplied to

provide additional margin.

Because of the severity of rub during Build I when oil leaked past the

forward intershaft carbon seal and during the Build IA stall, power turbine

blade tip clearances have been increased an additional 0.050-inch on the outer

attached blades and 0.030-inch on the inner attached blades, and all tips have

been tapered to 0.005 to 0.015-inch thickness as a precautionary measure.

3.5 TURBINE BLADE DAMPER EFFECTIVENESS

Coulomb damper pins were added to all turbine blade stages (I-4, 6-11)

and to Stage 12 power turbine frame airfoils (Section 3.4 and Figure 3-14).

Figure 3-15 demonstrates the Stage 1 turbine blade vibratory-stress reduction

resulting from the addition of the damper pins. Figure 3-16 shows the Stage 1

vibratory stress in relation to the scope limits before and after addition of

the dampers. Figures 3-17 through 3-26 illustrate the vibratory stress for

all turbine blade stages after installation of the dampers. Data are from an

accel to 25,000 ibf, except for Stage 11 blades data (bad telemetry signal)

which is from an accel to 22,000 ibf. Section 3.11 contains stress data for

the turbine frame blades.

37

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3.6 SUBIDLE OIL LEAK PROBLEH

After the carbon seal failure from assembly damage was repaired, the

propulsor still leaked oil into the rotors, flowpath, and nacelles. 0il loss

was visible, both during operation and on shutdown, in the form of smoke and

oil drips. The oil was leaking through the carbon seals during low speed ope-

ration. Although the amount of oil lost was not large, it was decided that it

was desirable to reduce the amount of smoke after shutdown.

During early operation, much of the engine testing was at subidle speeds

and below, as control and starting problems were worked out. The design idle

speed was 650 rpm. Initial testing proved that idle speed had to be increased

to 700 rpm for several reasons: the 650-rpm idle speed was too close to the

subidle rotor critical; the vibration level was unacceptable; the telemetry

cooling system was not effective at the lower speed; and propulsor stresses

were lower at the higher idle speed.

Test data showed that the pressure drop on the aft carbon seal approached

zero using the 650-rpm idle speed. The carbon seal leaked without a positive

pressure drop. At 700 rpm, the seal pressure drop is increased enough to

limit the oil loss out of the aft carbon seal. At higher power settings, the

pressure drop across the seal is well above that which is required for oil

sealing.

At low speeds (subidle), for very short runs, and during starts until the

elevated idle speed is reached, the propulsor sump is not scavenged properly.

At low speeds, the oil is not pumped to the ends of the rotating sumps where

it can be scavenged. Due to the frame design, scavenge lines at each end of

the sump run uphill initially; this forms a trap that requires some small sump

pressure to overcome prior to flowing to the scavenge element. The scavenge

pump used (from a CF6-50 engine) has a reputation as one that is difficult to

get primed and establish full scavenge flow. For these reasons, a subidle

lube bypass valve was designed and installed on the propulsor lube system.

The initial bypass system was a facility design - air actuated and con-

trolled by the engine stopcock. In order to preclude complete loss of oil to

the engine in a control or valve failure, the system was designed to divert

most, but not all, of the supply oil to the propulsor. At subidle, supply oil

51

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52

was diverted to the scavenge circuit just at the exit of the air oil cooler.

Hoses and hardware used were madeon site and were not flight quality. The

system, combinedwith the new higher idle speed, reduced or eliminated the lowspeed leak/smoke problem.

For flight-test, the system had to be replaced with a digital electronic-controlled solenoid valve. The facility system as configured above did not

function as desired on engine shutdown. The scavengepressure decay lagged

the supply pressure decay, so that the propulsor supply was actually divertedto a higher pressure circuit, and briefly, oil flow was increased to the pro-

pulsor. This condition was somewhatalleviated by removing the air oil cooler

from the scavengecircuit (which wasnot required) and by lowering line lossesin the bypass circuit with flight quality hardware. These changes ended the

leak and smokeproblems.

3.7 STATIONARY EXHAUST NOZZLE (CENTERBODY) REPLACEMENT

Between Builds 1 and 2, a redesigned centerbody was installed on the

engine. This redesign was necessary, because analysis and wind tunnel testing

indicated that at some flight conditions there would be an undesirable flow

separation from the centerbody. The predicted flow separation data for both

centerbodies is shown in Figure 3-27. No flow separation was detected or pre-

dicted for ground testing. Figure 3-28 compares the two centerbody designs.

Further information is provided in Section 7.3, Performance.

3.8 FAN BYPASS BLEED VALVE CALIBRATION

During Builds 1 and 2, tests were performed to calibrate the fan bypass

air (from the gas generator) bleed valve. This was done to provide necessary

information about the amount of fan bleed air required to maintain stall

margin in the UDF TM. These data are extrapolated for use in finding the amount

of bleed air required in flight.

3.9 FAN BYPASS BLEED VALVE DIFFUSER FAILURE/REPLACEMENT

During Build 2, the fan bypass bleed valve diffuser failed in high cycle

fatigue (Figure 3-29). Until a redesigned diffuser (Figure 3-30) could be

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designed and manufactured, the damaged portion of the diffuser was cut off and

used "as is." When the redesigned diffuser was available, it was installed on

the engine.

3. i0 PROPULSOR FAN-BLADE-LOSS EVENT

Summary of Event

The engine reached test point:

fan speed.

24,000 ibf, 1371 rpm propulsor

Stage 2, No. 7 composite fan blade shell separated from tita-

nium spar and was released; however, the spar remained attached

to the trunnion.

No high fan stress or other anomalies prior to blade loss.

Shutdown initiated at blade loss - I second chop to idle and

stopcock within 9 seconds.

No gas generator stall.

Propulsor spool-down was normal.

Due to a large imbalance (approximately 260,000 gm/inch) caused

by the missing composite, a noticeable amount of engine vibra-

tion was experienced.

Control/actuation system functioned normally after blade loss.

Spar Damage

Inspection of the spar following shutdown indicated the titanium had

cracked at the EB (electron beam) weld line the entire width of the spar. The

EB weld crack was clearly visible over the midspan of the blade (Figure 3-31).

Secondary Damage

Blade No. 6, which was next to the released blade, had a slight nick in

the polyurethane coating where the composite material from Blade 7 hit Blade

6 before striking the ground. The nick was an indication that only light

contact occurred.

The isolators contain an absorption material which is intended to yield

under high unbalance conditions such as blade loss. Deformation of the aft

57

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Figure 3-31. Spar Schematic.

58

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isolator pads was observed, and the isolators were returned to the vendor for

inspection. The aft isolators had their original values of spring rate and

damping coefficient. Since there was deformation of the aft isolator pads,

they were refurbished as a precautionary measure and returned to engine test.

No damage to the forward isolator was observed.

There was also concern that the transfer gearbox attached to released

blade trunnion No. 7 may have suffered some damage. The gearbox was torn down

and both the MPI (magnetic particle inspection) and FPI (fluorescent penetrant

inspection) of the gears and pinnions indicated no abnormal wear.

Bolts attaching the Stage 12 power frame to the rotating exhaust nozzle

showed interference with the OGV assembly, with the heaviest wear at blade

Location 7. The OGV assembly is designed to clear the bolt circle by 0.I00

to 0.160 inch. The OGV assembly showed light wear all the way around, with

a l-inch section indicating a harder rub. No repair was required. The OOV

assembly had no other distress.

The Stage II turbine blades rubbed the inner spool at some time during

the event, leaving a 4-inch x 3/8-inch rub mark on the inner rotor. The rub

coincided with Stage 2 fan blade Location 4. The indication was a surface

discoloration with no measurable depth. The Stage II blade trailing edge tip

did not have any discoloration or tip curl that would suggest a heavy rub.

Both Stages I and 2 fan blades were returned to Evendale for inspection.

No debonding was found in the Stage I set, but one Stage 2 blade was found to

have a section of composite separating from the spar.

Fan Blade Corrective Action

Corrective action included the addition of a portable ultrasonic scan of

all fan blades following each hour of engine run time. Ultrasonic scanning at

Evendale proved to give accurate results when trying to determine if debonding

has occurred. The ultrasonic scan used when the blades were returned to Even-

dale indicated a Stage 2 blade had started to debond. Portable scan equipment

also verified debonding of the composite. Because the previous test method,

ping checking, indicated the debonded blade was acceptable, the ping test was

discarded as a debonding check.

59

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6O

Test History of Failed Fan Blade

The blade that failed had been run 20:40 hours prior to the failure. A

breakdown of run time versus propulsor fan speed is provided in Figure 3-32.

3.11 PROPULSOR FAN BLADE HISTORY AND TEST DATA

3.11.1 Fan Blade Test History

None of the original design Stage 1 fan blades had to be replaced due to

failure or debonding. After Build 2, the blades were replaced with redesigned

blades with mechanical retention features. Figures 3-33 and 3-34 compare the

original and redesigned fan blades. All of the redesigned Stage l fan blades

ran through Build 3 without problems.

Some of the original design Stage 2 fan blades failed inspection during

Builds 1 and 2 due to debonding. These were replaced once any discrepancy was

found. Figure 3-35 depicts the history of the Stage 2 blades during Builds I

and 2. Investigation into the two debonded blades found after Build 1 deter-

mined that the probable cause of debonding was from propagation from cracks in

the foam inside the blades. This foam filled the cavity between the composite

shell and the titanium spar. Cracks in the foam during manufacturing propa-

gated into the shell/spar bond. A design change was made (Figure 3-36) to try

to prevent this from happening.

Section 3.10 discusses the Stage 2 fan blade failure in Build 2. After

this fan blade failure, the engine was limited to 1000-rpm fan speed until the

redesigned fan blades were available (Build 3 testing).

3.11.2 Fan Blade Test Data

Figure 3-37 summarizes fan blade vibratory stresses for Builds l, 2, and

3. Figures 3-38 through "3-42 present specific examples of stress data. Note

there are differences in fan blade stress levels with seemingly equivalent

test points. This difference is caused to a large degree by differing wind

conditions (that is, wind direction, velocity, gusting). Figure 3-43 depicts

the strain gage locations. Location No. 4, which gives the highest first flex

vibratory stress, is the strain gage used for the given data.

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• Composite Shell(Carbon Fiber-S-Glass Epoxy Matrix)

• Titanium Spar• Foam Filled Cavities

!

, 0=.i =

iS 'If !

tBJ

, !

_| ;,

Figure 3-33. Original Fan Blade Airfoil

Mechanical Design.

Page 81: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

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Page 83: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

F Laminated Composite

Stiffener Bonded

CompositeDowel

Pins

• Plug Retrofit Creates Stiff'Closed-Box' To Preclude Crack

Propagation And Increase ToleranceTo Thermal Cycling

Figure 3-36. Fan Blade Structural Improvement.

65

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Page 91: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

Fan Blade Response with Facility Fans

At the first test site (4A) a set of 12 facility fans were arranged in

front of the UDF TM inlet. Figure 3-44 shows a schematic of the facility fan

configuration. These fans attempt to simulate forward velocity of an engine

and try to smooth out airflow through and around the engine. It was desired

to see if some combination of these fans would lower fan blade stress. The

results can be seen in Figure 3-44; the first data point (no fans on) gave a

lower vibratory stress level than with any number of fans on. Stress levels

varied widely, depending on the number of fans that were on, but all levels

were higher than those without any fans. Since the engine centerline and

the facility fan centerline were not in line, it was believed that the fans

created additional disturbances in the flow field instead of smoothing the

airflow.

3.12 POWER TURBINE FRAME STRESS

During Build 2, power turbine frame vibratory stresses were higher than

predicted. The stresses were found to be predominantly 2/rev forced response.

This was caused from the fan Rotor 2 nodal, first flex mode (note that the

turbine frame and the fan blade rotor are mechanically linked). This causes

the frame stress to track the fan blade stress. Figure 3-45 provides a stress

comparison.

A detailed investigation into the frame stress allowed the vibratory

stress limits to be increased for the forced response mode (Figure 3-46). A

summary of this investigation and its results is in Table 3-I; supporting data

is shown in Figures 3-47 and 3-48. Build 3 data is presented in Figure 3-49.

3.13 EFFECT OF VORTEX DESTROYER ON STRESS

Vortices were seen between the ground and the fan blades at the bottom of

the engine. Visualization of these vortices was aided by having moisture on

the ground or by releasing smoke bombs. To see if the placement of a vortex

destroyer (a large metal grating) under the fan blades would reduce the fan

blade and power turbine frame vibratory stress levels, a vortex destroyer was

placed under the fan blades approximately 6 inches off the ground. Fan blade

73

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40

200

///

I\i \

/ \

/

II

//

• Fans Turned

On Produce

Higher

ResponseThan Without

1 2 3 4 5 6 7 8 9 10 11 12 13

Fan Turn On Sequence

Figure 3-44. Fan Blade Response with Facility Fans Turned On.

74

Page 93: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

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Page 94: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

Results:• Updated Scope Limits Versus Site 4A

Response• HCF Testing

Stage 5 Strut Gage #KD4H06

5O

40:°_.V

==

°110.7 0.9 1.1 1.3

Rotor Speed (rpm/thousand=)

2/17 2/18 2/18 2/28 2/28o 4- # • x

Stage 12 Strut Gage #KD4S07

i:io.L,_..0.7 0.9 1.1 1.3

Rotor Speed (rpm/thouunda)

2/17 2/18/ 2/18 2/28 2/28o .$- # • x

Figure 3-46. Power Turbine Frames Vibratory Response, Updated Scope

Limits Versus Site 4A Response.

?6

Page 95: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

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Page 96: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

• Frame Properties Better ThanMaterial Handbook Average

900°F Smooth Bar vs. 1100°F Smooth Bar vs.Material Handbook Material Handbook

50 50

_'_40 _ 40

I _ _ Tested Frame30 Tested Frame

_30 !- _'_ Minimum _ [_ __Minimum I

P .nd okAv..,.iI ..od_ook Minimum I I , Handbook Minlmum I

0_ 0_

0 20 40 60 80 100 0 20 40 60 80 100

Mean Stress (ksi) Mean Stress (ksi)

Figure 3-48. Power Turbine Frames Vibratory Response, Material HCF

Test Results.

?8

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Peak Levels

- Consistent withBuild 2

- Below Scope Limits

STAGE 5

KD4H06O' "

STAGE 5

KD4H09

20

Figure 3-49. Power Frame Vibratory Response, Build 3.

79

Page 98: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

stress data both with and without the vortex destroyer is contained in Figure

3-50. The same type of data are shown for the turbine frames in Figure 3-51.

Since this testing was performed after the Stage 2 fan blade loss, and before

installation of the redesigned fan blades, the engine was limited to 1000-rpm

fan speed, thus limiting available analytical data for comparison. The vortex

destroyer seemed to have a small positive or negligible effect on stresses;

however, it was decided to complete all remaining engine testing with the

destroyer in place. Wind conditions and the limited data (due to the 1000-rpm

fan speed limit) did make comparisons difficult.

Table 3-1. Power Turbine Vibratory Response Resolution.

Vortex Destroyer

Change Test Sites

Component Strain Distribution Test

Material HCF Testing

Updated Scope Limits

No Significant Effect (Section 3.13)

Slight Improvement (Section 3.14)

Mean Stress Analysis Verified

Stage 12 Engine Gage Poorly Located

for 2N Mode

New Stage 12 Gage Applied Which

Read Maximum Stress

Significant Property Improvement

Over Handbook Average

Stage 5 Frame Okay

Stage 12 Frame Marginally Okay

8O

3.14 EFFECT OF TEST SITE CHANGE ON STRESS

To try to reduce vibratory stress levels in the fan blades and the forced

vibration of the power turbine frames, the engine was moved from Site 4A to

3D. The site change increased the clearance between the ground and fan blades

from 28 inches to 64 inches as well as eliminated the frontal blockage area at

Site 4A caused by the permanent facility fan system that was in front of the

UDF TM inlet. Stress data are shown from both sites for the fan blades (Figure

3-52) and the turbine frames (Figure 3-53). There was no significant decrease

in either fan blade or turbine frame stresses. Fan blade stress data, after

the site change, was prior to the installation of the redesigned fan blades

Page 99: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

>-O

Stage 1 Fan Blade Gage #KD9108Baseline

24

o 2-17-86

20 + 2-18-860 2-18-86

_ 16 A 2-28-86x 2-28-86 • " ° °¢o 12 • • l . .

• o ii a

=_ ." : ! 0 ° ° o ,, a8 "'. ; :, :: .

i! +I

RotorSpeed(rpm)

24

"o 20.

=_.,

j 18w 12

• 80

Stage 2 Fan Blade Gage #KD9212Baseline

o 2-17-86

+ 2-18-86

0 2-18-86

• 2-28-86

x 2-28-86

ou

o °o

o on

o u o. 1 f

i o ° ° °n +

iiii 'i4 :

07oo mo 90o I+ +too I+ I_ 1,oo

Rotor Speed (rpm)

Stage I Fan Blade Gage #KD9108With Vortex Destroyer

24

_" _ 2-28-862o

+ 3-5-86

= 18

!u_ 12

; 8o

4 z ; ;t 1 ; '

lO0 81)0 900 11)00 1100 1200 1300 1400

Rotor Speed (ri m )

Stage 2 Fan Blade Gage #KD9212With Vortex Destroyer

24-

20'

:1 16e

u) 12

O• 8O

4

O 2-28-86

+ 3-5-86

io

' ; _i ,_ 9 aQ

• II

0

700 800 900 1000 1100 1200 1300 1400

Rotor Speed (rpm)

Figure 3-50. Fan Blades Vibratory Response, Effect of Vortex Destroyer.

81

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Page 102: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

Stage 5 Strut Stage 12 Strut

100, . _ _ 100 , , v _. ..

120 I-_"l u. 20

0 -- I 0 I I I I I I I I

600 800 1000 1200 600 800 1000 1200

XN48 (rpm) XN48 (rpm)

_,_ _: -_t _ _ t._.., ":

o_ 20 _ 20_ .____.._-_0 0 I I I I I I

600 800 1000 1200 600 800 I000 1200

XN49 (rpm) XN49 (rpm)

Figure 3-53. Power Turbine Frames Vibratory Response, Effect of

Site Change.

84

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so that a direct comparison of fan blade stress could be made. Fan speed was

limited to I000 rpm until the redesigned fan blades were installed. Turbine

frame stress data, after the site change, is from Build 3 (after installation

of the redesigned fan blades).

3.15 ROTOR LOCKUP AFTER SHUTDOWN RESULTING FROM FUEL LEAK

While running a power-down calibration at 19,000 ibf on June 30, 1986, a

fuel leak was observed, and the engine was quickly shut down. After propulsor

spoo_ down, the Stage 2 rotor would not rotate until the engine had cooled for

several hours. At that time, the exact cause was not known; however, based on

a later teardown, it is believed that the IGV lip seal had deflected thermally

and bound to the 1-4 inner spool. When the engine had cooled sufficiently,

the IGV and the spool separated enough to allow rotation of the Stage 2 rotor.

From looking at strain gage data for Stages i and 2 turbine blades, it appears

(Figure 3-54) that the IGV and spool had started to rub as early as June 24.

Heat generated from this interference eventually closed the Stage I turbine

blade clearance causing severe turbine blade tip rubs; Section 3.17 discusses

this further.

3.16 LOW/HIGH CYCLE FATIGUE TESTING

During Build 3, 100 low cycle fatigue cycles were run for endurance test-

ing. The cycle that was run is shown in Figure 3-55.

No dedicated high cycle fatigue testing was necessary because cycles in

excess of I x 106 were accumulated through the course of normal testing. The

number of cycles accumulated on each component was calculated using the compo-

nent first flex natural frequency and the engine run time versus propulsor rpm

relationship.

Table 3-2 shows the number of high- and low-cycle fatigue cycles that the

turbine blades, fan blades, and power frame airfoils experienced.

3.17 ROTOR-TO-ROTOR LOCKUP/PROPULSOR DISASSEMBLY AND REBUILD

During an attempt to make a normal start, it was noticed that the forward

and aft rotors although locked together could be turned with force. During

85

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6-24-86, 1260 rpm

9:53:09

9:53:10

9:53:12

9:53:12.5

9:53:12.8

9:53:13.5

-_"_1 !'

_. r-: i L. I.

,. " 2

_'!i.l _":

_i _ I_i T

!P. _ ....... :p. _, .....

Stage 2Blade

GageKD4E02

i_:_t- !"!-_-t'_ ,__:, i _1_! I ! ;: '_i i,i ec

i_ _,-.",:;

I

_I -1̧ -I ._- _-._ •_-"_

Figure 3-54. Suspected ICV/Spoo! Rub.

86

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3.0

2.6

2.2

1.8

o. 1.4

ul

1.0

0.6 _

m

0.2-

0

i

-- Flight Idle

I I I I L I I I I I I I = =2 4 6 8 10 12 14

Time, minutes

16

Figure 3-55. Low Cycle Fatigue Cycle.

87

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trim balancing, previously, the engine had run up to 22,000 ibf. No problems

occurred before the rotors locked. The force required to turn the rotors

increased when the blade actuation system was commanded to full reverse. It

was found that the forward actuator would not move to full reverse (-20°), but

only went to -12 ° . The rotors did not free up as the engine cooled, and the

decision was made to remove it from the test site to investigate the problem.

Turbine Blades

Stage 1

Stage 2

Stage 3

Stage 4

Stage 6

Stage 7

Stage 8

Stage 9

Stage I0

Stage l1

Fan Blades

Stages I/2

Power Frames

Stage 5/12

Table 3-2.

HCF Cycles

6.23 x 106

4.09 × 106

5.00 x 106

18.18 x 106

14. I0 × 106

7.5 × 106

15.15 x 10 6

1.2 × 106

2.5 × 106

1.3 x 106

3.69 × 106/

3.78 x 106

4.04 x 106/

4.2 x 106

GE36 HCF Cycle Count.

LCF Cycles

100

100

100

100

100

100

100

100

100

100

100

100

100

100

Remarks

53 Cracked Blades

No Discrepancies

No Discrepancies

No Discrepancies

No Discrepancies

No Discrepancies

No Discrepancies

No Discrepancies

No Discrepancies

3 Cracked Blade

No Discrepancies

No Discrepancies

When the engine was returned to the vertical build stand, it was noted

that the rotors rotated freely. The actuation system was exercised and found

that the forward system still would not travel to the full reverse extension.

With the actuation system in the stopped reverse position, the rotors became

bound in the same manner as seen on the test stand. A scale was utilized to

measure the force required to rotate the forward rotor holding the aft rotor

stationary. With the engine vertical and the actuator fully forward (feather

or 90°), the force to turn the Stage i rotor was 4 lb. When the actuator was

88

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driven fully aft (full reverse or -20°), the rotors bound, and the force which

was required to turn the forward rotor increased to 40 lb.

Full Forward Full Reverse

Forward Rotor 4 pounds 40 pounds

Aft Rotor 5 pounds 10 pounds

The above tabulation provides a comparison of the forces required to turn

the rotors independently, with the other held stationary. It was also found

that the lack of full travel in the actuator could easily be seen when watch-

ing the actuator. The forward system lacked 0.5 inch of its full travel. As

the pressure in the hydraulic system was increased (actuator in reverse), the

force required to turn the forward rotor increased to 40 Ib at 600 psi. The

decision was made to pull the propulsor from the gas generator and begin the

teardown to investigate the rotor binding.

Removal of the propulsor revealed problems unrelated to the rotor bind-

ing. Inlet guide vanes to the propulsor had cracks at the trailing edge ID

(inner diameter) braze. The ID was very irregular, and evidence of contact

with the Stage I-4 inner spool was noted. The area between the IGV and the

inner seal was black from oil coking, and the Stage I-4 inner spool was dis-

colored from varnishing. Figure 3-56 diagrams the IGV seal area as-designed,

and after test. Figure 3-57 shows the ALF (aft looking forward) view of the

tear/crack.

The IGV had worn a O.O10-inch groove in the Stage 1-4 inner spool around

the entire circumference. The heat generated by the continual interference

between the IGV and spool resulted in a spool growth that closed the Stage 1

blade tip clearance. The spool had heavy rub indications where the Stage 1

blade tips rubbed. The Stage 1 blade rub appears to have begun as early as

June 24, after 3 hours of Build 3 testing (Figure 3-58). Examination of the

strain gage data for Stages 1 and 2 of the power turbine indicates the IGV-to-

inner spool rub occurred prior to the Stage 1 blade rub (Section 3.15).

The Stage 1 blades were found to have HCF cracks that initiated at the

leading edge root. The blades with the most visible cracks are illustrated in

Figure 3-59. There is a total of 124 Stage 1 blades; of these, 19 blades had

89

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360 ° Braze Tear/(:

360 ° Hard Rub

360 ° Rub-

(0.01 Deep, No Discoloration)

Figure 3-56. IGV and 1-4 Inner Spool.

9O

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94

cracks visible to the naked eye, and an additional 34 were found cracked when

examined at 40x. The entire set was removed, and new blades were installed.

Tip clearance was increased an additional 0.037 inch at the blade leading edge

and 0.016 inch at the trailing edge for the new set of blades.

The Stage 2 polygonal ring was removed, followed by the outer seal. The

seal teeth had no damage, and coating wear was normal for the engine run time.

A cross-sectional view of the seal is shown in Figure 3-60.

Following removal of the Stage 1 polygonal ring, the aft stationary hard-

ware was removed. The eight actuator control rods which penetrate the No. 2

bearing static housing were all observed to have varying degrees of wear. The

heaviest wear was on the rods at 12 and 6 o'clock. The aft support had heavy

scoring on the forward OD (outer diameter) where the aft actuator travels over

it. Wear marks were in the same position as the sting tube support brackets.

Blocks providing support were reduced to lightweight springs during rebuild.

The scored area was cleaned and covered with a Teflon coating (Emralon 333) to

reduce friction between the actuator and support. The coating when scratched

will not flake but will lubricate to protect the material below.

Tile aft actuation subassembly was lifted out followed by a borescope of

the forward sumps. Entering the sump through the mid-driveshaft actuator rod

cutouts revealed the source of the binding rotors. The No. I roller bearing

(IR) outer race nut had come completely off (Reference Figures 6-2 and 6-3,

Section I.I). The actuator could not travel the full distance because the nut

was interfering with the last 0.5 inch of actuator travel.

The 6-12 assembly, less the midshaft, was removed for further inspection

and set in the teardown tooling.

Upon removal of the forward actuator, the IR bearing housing was removed

so that access to the IR bearing could be made. The outer race nut was laying

inside the actuator assembly, and the outer race was found almost completely

off. The rollers were pushed inward and the two shafts were easily separated.

The rollers sustained disassembly damage, making the bearing not serviceable

but repairable. The outer race had no visible grooves. The outer race nut

backed off as a result of Stage i-5 rotor aft shaft growth caused by thermal

expansion.

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A

_J

@

0

c_I

_J

95

Page 114: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

Because the carbon seal aft of the IR bearing, sealing the cavity, was in

remarkably good condition and repairable, the seal was removed for inspection,

the carbon segments were replaced, and the seal assembly installed. The mid-

sump seal aft of the carbon seal had rubbed grooves about O.14-inch long ×

0.04-inch deep in the honeycomb. As shown in Figure 3-61, the honeycomb and

seal teeth were all serviceable and reused.

All Stage II blades were heavily rubbed, and Stage I0 was lightly rubbed

(Figure 3-62); 3 Stage II blades were discovered with cracks in the leading

edge root, and the inner spool had evidence of a hard rub. The outer spool

(odd rotor) aft stages are cantilevered from the Stage 5 power frame. If the

IR bearing were not providing adequate radial support, it would account for a

rub at the aft stages of the outer spool. The 3 cracked Stage II blades were

replaced prior to rebuild. Table 3-3 summarizes the results of the turbine

blade inspection.

96

Table 3-3.

Stage

No. of Blades

No. Cracked

(IX Visual)

Additional No.

Cracked

(Borescope)

Additional

No. Cracked

(fOx Visual)

Additional

No. Cracked

(40× Visual)

Total Cracked

Turbine Blade Inspection Summary.

1 2 3 4 6 7 8 9 i0 11

124 118 120 94 90 72 84 54

19 0 0 0 0 - -

82 56

- 0

0 0 0 0 0* 0* 0* 0 3

0 0

34

53 0 0 0 0 0 0 0 0 3

(42.7%) (5.4%)

* Approximately 25% Sample; Others Inspected 100%

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o'-"

I.-

I

0 m

coo

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=

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._

97

Page 116: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

V_

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Page 117: OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE … · 2013-08-30 · OF A MODERN COUNTERROTATING UNDUCTED FAN ENGINE CONCEPT ENGINE TEST. FOREWORD ... 8.1 IPC STALL MARGIN 8.1.1

The 2R bearing was removed for a detailed examination at Evendale. One

roller had a rounded micro dent which would not affect the design intent of

the part. The 2R bearing was serviceable and was stored for later use, if

required.

Corrective action for the binding rotors included an improved locking

feature for the 1R outer race nut and other spanner nuts in the propulsor

assembly. Upon installation of a new No. 1 roller bearing, the spanner nut

was installed with a small amount of Loctite applied axially in four places

across the threads of the nut. Both threaded surfaces were cleaned and dried

prior to nut installation. An additional locking feature was added with two

pins installed between the shaft and nut, which were also tack welded in place

(Reference Figure 6-4). The inner race nut was installed only with Loctite.

A new carbon seal was also installed to replace the one damaged from the 1R

bearing problem. In addition, the 1B inner race nut had Loctite applied; all

others were untouched and remained as they were.

The IGV was repaired and modified to include a honeycomb seal to prevent

spool damage if a reoccurrence of the rub persists in later engine operation.

Figure 3-63 is a view of the IGV/spool seal area. During assembly of the pro-

pulsor to the gas generator, the gap between the IGV and spool was checked and

measured at 0.125 to 0.188 inch, with a minimum of 0.125 inch per the drawing.

Oil drain holes were drilled into the 1-4 inner, 1-2 outer, and 3-4 outer

turbine spools to drain any accumulated oil.

Borescope ports were added through the mixer frame flange for better

visibility to the IGV and Stage 1 blades. The inspection interval was set at

10 hours to keep better records of Stage 1 blade activity and IGV spool gap.

3.18 MISCELLANEOUS HARDWARE STRESS DATA

This section presents data on hardware that had no indication of high

stress (vibratory stress was always under limits) during testing and has not

been previously presented in other sections.

99

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L i 1-4 Inner Spool

_Honeycomb

Figure 3-63. IGV and 1-4 Inner Spool.

I00

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Nomenclature

Outer Guide Vanes (OGV)

Inner Guide Vanes (IGV)

Forward Outer Rotating Seal

Aft Outer Rotating Seal

Turbine Spools

I-4 Outer

7-11 Outer

6-11 Inner

* I0.0 for Turbine Blade Rubs

Limits

(ksida)

20.0

3.4

74.0 (2/rev)

II.0 (3,4/rev)

8.0 (5/rev)

15.0

30.0*

Fi__ure

3-64

3-65

3-66

3-67

3-68

3-69

3-70

3.19 OIL LEAK/GULPING PROBLEM

During the latter portion of Build 2 and, more markedly, during Build 3,

the propulsor oil consumption limited the UDF TM test time (oil consumption

increased from 0.35 to 1.58 quarts/hour from Build 2 to Build 3). The engine

was limited to about 2.5 hours of testing to allow for reservicing of the pro-

pulsor oil tank. By this stage of testing, the test site facility remote oil

fill system had been removed since it would not be available for flight-test.

Two major leaks contributed to the high oil consumption. The carbon seal

in the starter gearbox was leaking into the core nacelle and then back into

the fan, and oil leaked through worn actuation rods and seals in the aft sump

wall into the sting tube area in the center of the propulsor (aft stationary

support). Oil lost into the sting tube could be pumped out after engine shut-

down. A total of 39 quarts was recovered during Build 3 testing (66 hours).

The fan nacelle and propulsor rotors remained dry, indicating the oil loss was

not through the main propulsor carbon seals. Oil was also found leaking from

an instrumentation fitting in the aft sump wall. The propulsor lube oil leak

limited the engine test time in two ways.

First, as previously stated, the low lube level inside the sting tube

required careful monitoring to ensure that enough oil did not collect to flow

out of the mixer frame. The cavity was pumped approximately every 2.5 hours,

and about 2.5 quarts were removed each time (toward the end of Build 3).

101

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2000

1600

Frequency

1200

8OO

400

1st

Torsion

1stFlex

0

700 800 900 1000 1100 12001300 1400

XN49 rpm

Maximum Stress

1 ksipp

• 1F And 1T Responses

• Low Amplitude

• Maximum Allowable 20 ksipp

• Predicted Values

- 1F 600 Hz

- 1T 970 Hz

• Data Typical For Engine

Testing To Date

Figure 3-64. Power Turbine OGV - Engine Test Data.

i0_

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Frequency

2000

1600

1200

80O

400

IGV Frequency Prior To Stall Event

1 ksida

XN48-- 1350 rpm

T46 -- 1360 ° F

i "-----T----I ----I .... I - I ---I I I I I I-- I | I

0 20 40 60 80 I00 120 140

Time (Sec)

• Engine Test Dynamic Strain

Gage Frequency -- 1475 Hz(1 Flex)

• Predicted 1st Flex Frequency Is1425 Hz

• Allowable Stress Level Is3.4 ksida

• Trace Is Typical Of VaneData Seen During Engine Test

Figure 3-65. Power Turbine IGV - Engine Test Data.

103

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450

400

350

300

= 250

@

200 -

150

500 600 700 800 900 i000 ii00 1200 1300 1400 1500f

I w _I _ ° I XN48, rpm

YIIIEINM.J. i• IN TOP[ tlS8 lidlqPU[ Mlrl[. 1600 OENSITIUITY- I SO

TKI6 I(DAS0! lue _s Buy,, cvcu. o ee Kect o;m. It|HCZL ,_L_ CUt- O _,rrxe,, cem- t

£3G e82-eo ,2 2-4-86 now

Figure 3-66. Forward Outer Rotating Seal Response, Decel from

25,000 ibf Thrust: February 4, 1986.

104

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ORIGINAL PAGE IS

OF POOR QUALITY

450

400

350

150

i00

50

#20--

o

15

10"

i

5"

500 600

INOaqlI m " [

Om

TNKI? KD4$04

700 800 900 i000 ii00 1200 1300 1400 1500

XN49, rpmT*I'( Iml] _ k_. t_ II[nllTlUI_. |U/ICCEL 15'13 J4tS IIUTVeke" t _ K0_ IIU* |1| NI

FILTI[J _" 0 WUNCTIm GON* I

GE36 eBa-_l/_ 2-4-86

Figure 3-67. Aft Outer Rotating Seal Response, Accel to

25,000 ibf Thrust: February 4, 1986.

105

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i000

900

800

700

600

500

400

300

200

i00

0

500 600

I Ml_qll I_ * J

'l_gllllm,Jh 0 |lION

TKIII?, KD4EOS

700

TAP(I|I|

GE36

800 900 i000 ii00 1200 1300

XN49, rpm _m_EM_. B_

FILYI_I cI- ?

eB2-eel/e 2-4-86

1400 1500

I[IltlTIUllrV* I SOlllll* IM4

JrkeCTlm COU- I

mlJ

Figure 3-68. Outer Turbine Spool Response (I-4), Accel to

25,000 ibf Thrust: February 4, 1986.

106

ORIGINAL ..... _

OF POOR Qu_

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OF POOR QUALITy

450

400

350

300

L3

250

200

150

.

50

.._+

JOO 600l"1 00 ipel l

_8IIIOLI- I 1O81O

TKI4 KD4L$3

+.++..

..++

+.

700 800 900 i000 ii00 1200 1300 1400 15OO

T_ U_I XN48, rpm _ b_- IlMII IINIIIIIVIW. t N

till tells ItttV ¢_tJr. t IS IILO_ Jill- ltlACCIL Ir|LTIN COE- lJ IrMI_TIONCON- t

GE36 082-e_)1/2 2-4-86 m

Figure 3-69. Outer Turbine Spool Response (7-11), Acceleration

to 35,000 ibf Thrust: February 4, 1986.

107

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ORIGINAL P_.C_ iSOE POOR QUALITY

I,,,,I,,,,I,,,,I .... I,,,,I,,,,I,,,,I,,,,I .... I,,,,,

- t i il i

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108

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Second, combined with the excessive leakage, the gulp limited testing

duration. The propulsor gulps about 2.5 quarts of oil with increasing power

from idle to maximum. This is consistent over all engine testing. As speed

is reduced, the oil level will return. That is, it will return if the propul-

sor is not losing oil from leaks in the sump wall or gearbox carbon seal.

With a normal oil consumption rate, oil gulping is not a problem with the II

quart tank.

Following Build 3, the leaks were fixed; new actuation rods and seals

were installed in the actuation system, a new starter adapter gearbox was

installed, and the instrumentation fittings were replaced. A larger scavenge

port was installed in the new starter adapter gearbox to improve scavenging

and to keep oil away from the aft carbon seal that leaked on Build 3. A new

flight-type static vent air demister was installed, and oil drain holes were

added to the turbine spools.

109

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4.0 HEAT TRANSFER AND SECONDARY FLOW SYSTEM

4.1 MIXER FRAME HEAT TRANSFER

The mixer frame flow circuit is shown in Figure 4-i. At takeoff power,

film-hole flow is 15% less than predicted, outer flowpath secondary flow is

10% less than predicted, and total sump flow is 6% higher than predicted. The

outer flowpath flow and sump flow are determined through use of pressure tap

readings, and film-hole flow is determined by subtracting these flows from the

total fan bypass flow.

Figure 4-2 provides a comparison of mixer frame predicted and measured

internal pressures at takeoff power; whereas, a comparison of predicted and

measured flowpath static pressures at takeoff power is depicted in Figure 4-3.

Although very few pressure readings are available, test data indicates that

the pressure drop across the film holes is close to that predicted. The low

film-hole flow appears, therefore, to be due to undersized film flow area.

The total pressure drop available to the frame film holes is very low,

making BFM (backflow margin) a concern. The regions of minimum BFM are the

inner flowpath fairing upstream of the strut leading edge and strut leading

edge cavity at the root. A comparison of predicted and measured pressures for

engine Build 1 is shown in Figure 4-4. While the BFM across the inner flow-

path fairing film holes is slightly less than predicted, the BFM across the

strut leading edge cavity film holes is much higher than predicted.

Installation of power turbine blade dampers for engine Build 2 resulted

in a lower level BFM. The inner flowpath fairing pressures for engine Build 2

are shown in Figure 4-5 for takeoff and maximum cruise, the minimum backflow

condition. Takeoff pressures are taken from test data, and the maximum cruise

pressures are predictions based on test results. The 0.79% BFM at maximum

cruise condition is low, but it is in a very localized region. The BFM in all

other regions is significantly higher.

Figure 4-6 illustrates mixer frame metal temperatures, both predicted and

actual, for hot day takeoff power. All thermocouple data have been scaled up

to hot day conditions by multiplying the raw data by the ratio of the hot day

iiO

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..... ,"L :o/:l,i_F i_

I Test iPredictedJ

All Flows in %W25

1.41

.56

4.27

5.63

0.32

0.31

9.77

2.13

2.45

2.62

2.47

0.32

0.32

Figure 4-I. Mixer Frame Flows at Takeoff Power, Test

Versus Predicted.

III

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47.4

47.2

47.0

C_ 46.8

46.6

46.4

46.2

46.0 "15

? Predicted Total Pressure

I I Ii 16 2

Station

e2

112

Figure 4-2. Mixer Frame Pressure Losses Comparison of Measured

and Predicted Pressures.

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45

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i_ _ Outer Fl°wpath Predlcte d

Q Test Data

40 _ _ i i I-4 -2 0 2 4 6 8 10 12

Axial Distance from Strut Leading Edge, inches

14

Figure 4-3. Mixer Frame Flowpath Static Pressure Distribution Takeoff Power.

113

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ambient temperature over the test day ambient temperature. No thermocouplesare available along flowpath portions of the frame, but the existing thermo-

couple readings indicate that the frame is adequately cooled. Also, there are

no visible signs of overtemperature.

4.2 POWER TURBINE SECONDARY FLOW SYSTEM

Figure 4-7 illustrates the power turbine secondary flow system. The flow

rates, predicted and actual, are tabulated in Table 4-I. Although the total

secondary flow for engine Build I neared prediction, the Stage I inner flow-

path purge flow was significantly lower than predicted. This redistribution

of flow is a result of a mixer frame supply hole flow coefficient that is

lower than predicted and shafting hole flow coefficients that are greater than

predicted. The increased pressure drop across the mixer frame supply holes,

combined with reduced pressure drop through the shafting annular holes, serves

to lower the supply pressure to the forward seal. Also, the sump vent flow

was higher than predicted due to large carbon seal leakage areas. This addi-

tional vent flow results in a further decrease in Stage I purge flow.

During Build 1 testing, Stage I cavity temperature was 830 ° F at takeoff

power, as compared to 795 ° F predicted. Although there was no evidence of gas

ingestion, it was observed that the forward seal AP decreases with increase in

power setting. Figure 4-8 plots AP versus P46Q2.

Extrapolation of the test data indicates that for Build 1 testing, back-

flow could occur at maximum power. To maintain positive flow in all cases,

the mixer frame supply hole area was increased from 5.4 in 2 to 5.84 in 2. The

resulting increase in forward seal AP from Build 1 testing to Build 2 testing

is significant (Figure 4-8); however, the impact of this area increase on the

remaining purge flows is negligible. The aft labyrinth seal flow increased

significantly from Build 1 to Build 2 testing, presumably due to an increased

seal clearance, indicated by a reduction in pressure drop across the seal.

During Build 3 engine testing, rubs occurred on two middle inner flowpath

seals (G and H). There is an increase in the flows of these two seals, but

because the system is metered for the most part by the supply hole and the

shafting holes, the total secondary flow increases only slightly (Figure 4-7).

i17

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PROBLEM. EXTRAPOLATIONOF TEST DATA

INDICATESTHAT FORWARDSEALCOULDBACKFLOWAT MAX POWER,

| CAUSE: UNDERSIZEDSUPPLYHOLE AND

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Figure 4-8. Potential Forward Seal Problem.

120

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It should be noted that the very limited amountof instrumentation makes

direct measurementof most of the individual flows impossible. The available

pressure and temperature readings were used to rebalance the analytical flownetwork model which yields the best estimate of the flow distribution. The

two flows leaving the mixer frame (S and T) are directly measured.

According to thermocouple data, all cavities are adequately purged. Acomparison of predicted and actual temperatures is presented in Figure 4-9.

4.3 POWER TURBINE HEAT TRANSFER

The power turbine spool and frame temperatures, predicted and actual, are

shown on Figures 4-10 and 4-11 for hot day takeoff power. The original pre-

dictions (Figure 4-10) were determined using a finite difference heat transfer

program. The actual temperatures (Figure 4-]I) have been scaled up to hot day

conditions, as described in the mixer frame section. Because the fan bypass

air temperature is lower than predicted, most of the cavity temperatures are

also lower. The cavity temperatures have a direct impact on the inner spool

temperatures. Unfortunately, there was too little instrumentation to be able

to draw any firm conclusions about inner spool temperatures, as compared to

predictions.

4.4 NACELLE VENTILATION

The nacelle ventilation system is depicted on Figure 4-12, with component

temperatures at takeoff condition. All thermocouple data have been scaled up

to hot day conditions, as described in the mixer frame section. Although some

components are higher in temperature than predicted, all of the hardware is

adequately cooled.

During initial engine Build 1 testing, ambient air was to be brought in

to the nacelle cavity aft of the Stage 2 telemetry through radial holes in the

cowling. However, poor ventilation in that region led to an overheating of

the aft telemetry, probably due to a low level of static pressure at the inner

flowpath. A total of 30 air scoops were then mounted to the holes. The addi-

tional ventilation air resulted in the temperatures presented in Figure 4-13.

121

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Steady-State Conditions

h - [BTU/hr. ft.2 ° F]

Figure 4-10. Power Turbine Temperatures Based on Analysis.

123

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ITest DataPredicted

]'Air = i00° F 174 ° F

152 ° F

281 ° F

226 ° F

l404 ° F

Figure 4-13. Forward Fan Blade Hub Temperatures; Hot Day Takeoff,

Mach= 0.0, Full Thrust.

126

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It was determined during initial Build 1 testing that, although the aft

telemetry modules were adequately cooled, the solder which fixes the thermo-

couple leads to the aft telemetry circuit board, was overtemperatured. Eventhough the solder temperature is not measureddirectly, it was found that thesolder melts when the nearby air thermocouple reaches a temperature of just

over 300° F.

The solder, although adequately cooled during high power, is marginallycool at idle conditions. Set to match the prop flow at takeoff, the scoop

direction is misaligned with the flow direction at idle. For +27 DTAMBcondi-

tions, the solder temperature is 219° F at takeoff, 235° F at flight idle, and

283° F at ground idle.

Figure 4-13 gives a breakdownof the forward fan blade hub temperaturesfor hot day takeoff. The 404° F trunnion temperature is taken from thermo-

couple data. All other temperatures are determined by rebalancing the heattransfer model on the basis of the trunnion temperature. All temperatures are

higher than predicted, but are still within allowable limits.

4.5 CENTER CAVITY VENTILATION

The center cavity is portrayed (Figure 4-14) with temperatures at takeoff

power; normal operating temperatures are as listed. The actuator axial posi-

tion sensor (LVDT) temperature of 312 ° F is well below the normal operating

temperature of 360 ° F (the maximum temperature limit is 400 ° F). The speed

sensor temperature was not measured directly, but it is probably less than the

LVDT temperature since it sees less radiation from the cavity wall than does

the LVDT. In addition, the sump oil may provide a sink to the speed sensor.

There is no indication of speed sensor or LVDT overtemperature problems.

127

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5.0 ENGINE SYSTEM DYNANICS

Valuable engine dynamics experience was obtained during ground testing of

the UDF TM Demonstrator Engine (GE36 S/N 082-001). This ground testing, along

with a series of mechanical impedance tests conducted on the support system

and Peehles test facility, was used to modify and verify the analytical model

of the engine. Topics that are discussed in a later section regarding this

subject include such gas generator vibration signatures as: synchronous I/rev

IPC and HPC responses, linear subidle UDF TM I/rev signature and its dependency

on support structure/test facility stiffness, linear UDF TM I/rev response

recorded in the operational speed range, and nonlinear UDF TM I/rev response

observed during the Stage 2 propulsor airfoil separation event.

The UDF TM, with its counterrotating propulsion system, also demonstrated

that more sophisticated methods and hardware are required beyond turbofan

engine experience with regards to propulsor trim balancing and vibration

measuring techniques.

Gas Generator Vibration Signature

The gas generator used to power the GE36 Demonstrator is an F404 engine.

Its rear frame is replaced by the mixer frame, and the gas generator is mated

to the UDF TM. Gas generator synchronous IPC (intermediate pressure compressor)

and HPC (high pressure compressor) vibration levels were well within the pre-

scribed F404 limits throughout ground testing. Both the maximum IPC and HPC

1/rev levels observed in the operational speed range during testing occurred

at the F404 fan case vertical location.

0.24-inch/second (average velocity) at

Build 3 testing.

The maximum IPC 1/rev response was

11,700 rpm and was observed during

Figure 5-I presents IPC signatures for Builds IA, 2, and 3, demonstrating

that the IPC I/rev levels remained similar and low throughout ground testing.

The maximum HPC 1/rev response was 0.28-inch/second at 13,700 rpm as observed

on Build 2. Figure 5-2 compares HPC I/rev vibration signatures for Builds IA,

2, and 3 (F404 fan case vertical location). Like the IPC vibration signature,

the HPC synchronous response remained similar and low throughout testing.

129

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The F404 predicted engine dynamics show little changebetween the turbo-

fan engine and the GE36gas generator application. These predictions wereverified by comparing the vibration data from the check-out (at GE-Lynn) of

the turbofan configuration with the results observed during the GE36groundtest. Demonstrating little change between both configurations, the results

are shown in Figures 5-3 and 5-4; readings were taken at the F404 midframe

horizontal location (only commonaccelerometer location between the two con-

figurations) for the IPC and HPC1/rev vibration signatures, respectively.

UDF TM Vibration Signature

The test facility and aircraft structure play a major role in the overall

support structure stiffness of the engine and resulting rigid body mode defi-

nition of the entire system. Mechanical impedance tests were conducted during

January 1986 (between Builds IA and 2) to obtain the support structure stiff-

ness. The pylon/isolators system was tested with the pylon attached to ground

to obtain pylon and isolator stiffnesses and also mounted at Peebles Site 4A

facility to obtain the entire support system stiffness. These results were

incorporated in both updated linear and nonlinear (propulsor blade-out) ana-

lytical dynamic models and will be referenced in subsequent discussion of UDF TM

vibration results.

The rigid-body modes occur primarily in the subidle speed range. Since

the demo engine was tested at both Sites 4A and 3D, subidle resonances were

subject to change due to the differences in facility stiffness properties. To

demonstrate these differences, a comparison of Build 2 UDF TM I/rev vibration

signature obtained during engine starts at both sites are shown in Figures 5-5

and 5-6. Figure 5-5 compares the subidle vibration signatures at the F404 fan

case vertical location (vertical direction for Peebles test is in line with

the strut). The signatures indicate that the overall support system stiffness

was softer at Site 3D in this direction. Figure 5-6 compares the two subidle

signatures at the same location in the horizontal (normal-to-strut) direction.

Overall system stiffness effects at Site 3D acted to decouple the predominant

rigid-body modes observed at Site 4A.

The UDF TM I/rev operational speed range vibration signature at the No. 2

ball bearing housing location is illustrated in Figure 5-7 for the vertical

131

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direction and in Figure 5-8 for the horizontal direction; each indicates the

deflection in mils (DA) as a function of propulsor speed for accels conducted

to 24,000 ibf at Sites 4A (Build 2) and 3D (Build 3). Although the signatures

are similar, differences in levels were noted; the differences in levels are

accounted for by two explanations. The first is that the propulsor blades

were modified, and a nominal correction weight was added to the Stage 2 rotor

between runs. The second explanation deals with the repeatability of vibra-

tion on a closely synchronized counterrotating propulsion system; this subject

will be discussed in a later section.

Stage 2 Airfoil Separation Event

The Stage 2 propulsor airfoil separation event that occurred on Build 2

(Site 4A) led to an opportunity to modify and verify the nonlinear dynamic

model predictions (by mechanical impedance test results) for this event and,

subsequently, to apply this knowledge to the blade-out design criteria of the

aircraft application. The dynamics, both actual and predicted, were presented

during the May 13, 1986 Quarterly Review at the Nasa-Lewis Research Center in

Cleveland, Ohio. A major benefit resulting from this event was proof that the

pylon isolators function as designed. This was demonstrated by a significant

reduction of motion through the isolators, and the fact that the isolators

soften with the increased loading and, thus, lower the system resonant speed.

Trim Balance Experience

The initial efforts to trim balance the propulsors during Build 2 were

hampered by the hardware used. The basic trim balance test sequence was to

separate propulsor speeds by 100 rpm (1.67 Hz) and take amplitude and phase

readings from the existing SDll9C Trim Balance Analyzer unit at predetermined

steady-state speed conditions. Making the initial trim balance unsuccessful,

the built-in 3 Hz (41.5 Hz) bandwidth tracking filter of the SDll9C unit did

not adequately separate the vibration response of the two rotors and, thus,

did not give correct amplitude and phase information.

A modified SDll9C unit was purchased with a 1.0 Hz (40.5 Hz) bandwidth

tracking filter and was evaluated during Build 3 testing. Improvements were

achieved in the balance of each rotor utilizing this new unit and applying

134

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20.0

_o:2_aLL_eaLr_n__°u_ngVertical

<_vv15.0J .................. , .............................................................................................................

| I sS_ u_,o.d...................,_.........._.-/..................................................:..-........-t/ ' I' l_'^ /-- Build 3

| ...................

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/500 700 1100 1 00

Forward and Aft Propulsor Speed, rpm

Figure 5-7. UDF TM One-Per-Rev Vibration Signature on 2 Minute Accel to

24,000 ib Thrust, Housing Vertical.

15.0

<c_

10.(._.-4

Q.I5.

C_

I

No. 2 Ball Bearing Housing Horizontal I

T

.............:i:!-:/..................... ..........'--_- .:,,d,,--,f/_--_1-....................',-'II_.....',, ...................................... " ............

_Ioo " ",'oo...... _,'oo"" " ,Joo......... ' I " ! I ' ' ' !• ' ' i.'O0

500

Forward and Aft Propulsor Speed, rpm

Figure 5-8. UDF TM One-Per-Rev Vibration Signature on 2 Minute Accel to

24,000 ib Thrust, Housing Horizontal•

135

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force correction weights. The sensitivity to the force unbalance was deter-

mined to be 325 gram-inches/mil which is 2 to 3 times less sensitive than fan

unbalance in a large bypass turbofan engine. But even with the improvements

noted above, the vibration response observed during power hooks (constant rpm

thrust excursions) was still considered undesirable. The test on this build

ended before a good set of high thrust data could be obtained during the power

hook excursions.

The amount of data accumulated in these balance exercises did, however,

indicate that one or more excitation sources, other than a pure force unbal-

ance, was contributing significantly to the UDF TM vibration signature of the

engine. Efforts are currently underway to evaluate each of the following

possible sources:

• Changes in either force or mechanical moment unbalance due to

the blade actuation system (from low- to high-power condition)

• Aerodynamic moment unbalance being introduced by any propulsor-

blade tracking problem.

Measuring Techniques

For a simpie one degree of freedom system, the maximum sensed deflection

would lag the forcing function (rotor unbalance) by 90 ° at its first natural

frequency. The deflection level is a function of the unbalance force magni-

tude, the damping, and the mode shape at this given frequency. For a single

rotor application, such as a high bypass turbofan engine, the maximum static

deflection at any circumferential location, even though not necessarily equal,

would occur in one revolution of the rotor and wouid be repeatable from one

revolution to another, provided the unbalance or rpm were unchanged. Using

this simpie one degree of freedom system and assuming that the mode shapes in

the vertical and horizontal directions are identical, Figure 5-9 demonstrates

this point.

The UDF TM engine, on the other hand, may not sense the maximum deflection

at a given circumferential location during a revolution of its counterrotating

propulsor rotors. For example, assume that both the forward and aft rotors

are exactly synchronized, that the forcing functions are equal at each rotor,

and the mode shapes are identical in both the vertical and horizontal planes.

136

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0

4.;

u3.

t,,

4-I

-f

,7

0>

4.1

4.1

0°_

t_

4-J

_q

E

I

c_

137

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Now, using the single rotor exampleabove, we have two cases (Figures 5-10 and

5-11) which showeither the vertical or the horizontal deflection at a maximum

level, and the other plane at a minimum.

This example indicates that for a given revolution, if the vertical loca-tion is at the maximumlevel, the horizontal response is zero, and vice versa.

This example also shows that the maximumdeflections in each plane are equal,

and that the minimumdeflections are not only equal but are, in fact, zero.Expanding this example into real-world application, we find that the maximum

response in a given plane will always result in the minimumresponse occurring

in its orthogonal plane.

First, let the force unbalance of each rotor be different. In this case,

maximumdeflection for both the vertical and horizontal planes will still beequal, as will the minimumlevels, but these minimumvalues will no longer bezero. Second, let the modeshape definition and force unbalance be different.

At this point, neither maximumnor minimumdeflections between the two planeswould be expected to be equal. The final step in approaching the real world

is to leave the one degree of freedom system and enter the actual multidegree

freedom system situation. This step does nothing more than to vary the phase-angle lag between the lined up forces, and the resultant maximumdeflection

circumferential location, as a function of the engine dynamics.

Test data is provided in Figure 5-12 demonstrating the above discussion

and illustrating the UDFrMI/rev response at ground idle power for the approxi-mately orthogonally mountedaccelerometers at the No. 2 ball bearing housing

location. Also shownis the phase-angle lag between the forward and aft pro-pulsor i/rev indicators. The phase data indicates that the rotors are close

but not totally synchronized. The vibration data shows the 1/rev levels are

modulating at the samefrequency as the propulsor rotors difference frequency.These data demonstrate, as earlier stated in the discussion, that the maximum

response in one plane occurs at the minimumresponse of the other plane, andvice versa. The two rotors unbalance line up at a phase-angle lag of 240° to

yield the maximumvertical response and at a phase-angle lag of 60° to yield

the maximumhorizontal response.

138

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Cx,I

0

_ g

T "_

¢n

©.r-t4_

0>¢)

cI

rJ

,.-!.r-I

r_

0

U

I

¢1

139

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f_

0

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,--t

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140

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NmZ

CD"

_4

<J

O-

L_

50--

No. 2 Ball Bearing Housing Vertical

40-

30- _UDF One-Per-Rev Velocity Response

20- . ' i _IU_,,,,,,.

I0 ,J ,_l l i. I

0

5O

200.

_J

"o I00.

g_

No. 2 Ball Bearing Housing Horizontal

40-

30- /--UDF One-Per-Rev Velocity Response

04 ..... [ ..... I''"''1 ..... I'"'''1 ..... } ..... t ..... I ..... I .....

-I00-

iiiiiiiiiiiiiiiii":: ..- iiiiiiiii!iiii

....

1.0 2.0 3.0 4.0 5.0 6.0 7.0 8.0 9.0 I0.0

Time, minutes

Figure 5-12. GE36 Demonstrator Engine 082-001/3

T/D 7-1-86 Time History Plots at

Ground Idle Power.

141

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This discussion explains why variation in vibration would be expected in

the UDFTM I/rev levels shown in Figures 5-7 and 5-8. Although the rotors are

not precisely synchronized during the throttle advances, they are close, and

therefore, the response at any given speed is dependent upon the orientation

of the unbalances to each other and to the sensing device.

Realizing that this characteristic existed prior to initiation of ground

testing, GE Aircraft Engines developed a system to optimize the chance of cap-

turing the maximum vibration level each revolution. The automatic vibration

engine shutdown/aircraft monitoring system has two sets of orthogonal acceler-

ometers mounted on the engine. Each signal of the orthogonal accelerometer

goes through a software package that takes the square root of the sums of the

responses squared. This method vastly increases the probability of capturing

the maximum vibration response each revolution and is, by far, a more accurate

measuring tool for synchronized counterrotating rotors than the conventional

method utilized to measure high bypass turbofan engine vibration.

142

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6.0 BEARINGS AND SEALS

This section covers the main propulsor bearings and all actuation system

support bearings. All of the bearings performed well during ground testing,

from a design standpoint. Some problems arose as a result of debris produced

during manufacture of other engine parts; however, engine operability was not

compromised. Seals in the fan blade retention system performed well during

testing except for a few torn fan blade thrust bearing seals resulting from

insufficient lubrication.

6.1 HARDWARE CONDITION

6.1.i Rotor Support Main Bearings

Debris Ingestion

The main bearings operated well, which was to be expected, as they had

ample capacity.

The two roller bearings were replaced twice during ground testing when

they were exposed at disassembly. They were replaced because debris damage

had scored some of the rollers. The debris was comprised almost exclusively

of O.007-inch-diameter steel shot particles, with some other manufacturing and

wear debris present in very small quantities. Prior to engine teardown, oil

sample analysis had identified the possibility of a debris problem.

A blind cavity in the forward intershaft carbon seal land, designed to

prevent possible thermal coning, had trapped a quantity of steel shot during

the peening process. The shot did not wash out during manufacture but was

sluiced out by the hot lube oil during engine running.

Causing extensive scoring of the rollers, the shot became imbedded in the

soft silver plate of the rolling element retainer of the bearing. This would

cause both a breakdown of the hydrodynamic lube film because of the high loads

and low rotational speeds and a diminished fatigue life. However, no surface

distress due to rubbing was observed.

Bearings were returned to the manufacturer for refurbishment, although

only inner rings and cages were usable. The rings were rehoned and the cages

143

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stripped and replated. The design of the roller retention features permitted

roller removal without damage to the cage.

To prevent further debris damage, the blind cavity was ultrasonically

cleaned and sealed closed with a nichrome strip (Figure 6-I). This was fairly

successful, although one or two pieces of shot were still found in subsequent

oil samples.

Retent_n Nut Loosening

The outer ring retention nut of the IR intershaft bearing came loose and

completely disengaged during the final stage of ground testing; this permitted

axial movement of the outer ring.

The nut is believed to have jammed the actuation system preventing blade-

angle adjustment. On teardown, forward and aft rotors could not be separated

in the normal disassembly sequence. This was caused by the rollers no longer

being in contact with the outer raceway. Borescope inspection prior to dis-

assembly had shown the rollers still engaged, so running in this disengaged

condition had not occurred. When the rotors were separated, the bearing was

found to be in remarkably good condition, except for the damage to the roller

corners caused when the rollers dropped into the region of the outer shaft,

from which the ring had moved, and hung up on the shaft shoulder (Figures 6-2

and 6-3).

Examination of the spanner nut indicated no obvious thread damage, and

the Vespel insert retention feature appeared undamaged. The appearance of the

raceway did not indicate any running off the normal roller path; however, some

coning was indicated. The shaft coning was in the direction to move the shaft

radially away from the nut, and the wedge effect would exert an axial force on

the nut in the direction to promote untorquing. There was no damage from ring

spinning on either the outer ring OD or the shaft bore.

For subsequent engine testing, a hole was line-drilled axially in the

thread, and a roll-pin was mechanically locked in the thread to prevent the

nut becoming untorqued (Figure 6-4).

144

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_ircumferentia!Nichrome Strip

Figure 6-1. Seal Cavity Closure.

SpannerNutOuter Race

Figure 6-2. Possible Running Condition withIR SpannerNut Loose.

145

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Rollers Having MovedRadiallyOutwardContact Shaft Sho_

Figure 6-3. Disassembly Problem and RollerCorner Damage.

Axial Roll PinWeldedin Place

Figure 6-4. Problem Solution - PositiveNut Locking.

146

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6.1.2 Inner Actuation Bearings

Actuation Ball Bearings

No problems were encountered with the large mainshaft actuation ball

bearings. These bearings were examined at the last teardown for any evidence

of irregular wear or cage impact that might occur due to the calculated axial

distortion of the outer ring from the four gear rack loads, but no indication

of abnormalities was seen.

Radial Quill Shaft Gearbox Bearings

The inner bearings supporting the radial shafts could not be seen without

teardown of the gearboxes; however, since no problem existed and they operated

flawlessly, no teardown was performed.

The outer gearboxes were examined because of the loosening of the outer

housing nut. The nut butts against and clamps the outer ball bearing, which

locates the pinion gear. The cause of the loosening was found to be a stackup

problem incurred by a change in a washer thickness (Figure 6-5), and the prob-

lem was corrected. Although the bearings are grease lubricated, most of the

grease had been expelled, and some bearings showed wear.

6.1.3 Actuation Tapered Roller Bearings

The tapered roller bearings supporting the counterbalance torque tubes

and bevel gears were examined and showed no deleterious effect except for some

slight corrosion. This problem was manifest because the grease lubricating

these bearings is centrifuged outwards, and the bearings are not adequately

protected from the high humidity experienced during testing, some of which

occurred during moderate rain.

6.1.4 Fan Retention Bearings and Seals

Setup Bearing

The setup bearing is incorporated to react the blade overturning moment

and carry most of that load. However, at speed, the centrifugal load is suf-

ficiently high that a very large moment would be required to unseat the main

147

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ii

m n

Oversize Vespel Washer

Cap

Figure 6-5. Gearbox Stackup Problem Causing Incorrect Loading

of Ball Bearing and Cap Looseness.

148

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thrust bearing. Therefore, the setup bearing has a relatively easy life. The

only problem associated with these bearings was, again, corrosion. Although

protected by a silicone seal and lubricated by grease, because the grease ispermeable, somecorrosion was seen, but not severe and none on the active sur-

faces of the bearing.

Fan Thrust Bearing

Bearing Condition and Seal Condition - The main fan thrust bearing reacts

the considerable centrifugal load of the blade and is subjected to dither from

blade vibrations and actuation system load fluctuations. Therefore, false

brinelling and fretting were the major concerns.

Most noticeable about the condition of the bearings was the disparity in

appearance between forward and aft rotor parts. The front rotor was in a much

hotter environment, sometimes as much as i00 ° F hotter. Bearings from this

rotor were slightly blued, but the aft rotor bearings were not discolored.

Some fretting corrosion was present on both rotor bearings; however, this had

not progressed to the point were the bearings were unserviceable.

The lubricant in the forward rotor was dry and discolored; whereas, the

aft rotor grease looked like new. Grease seals in some of the forward rotor

parts had been torn due to lack of lubrication.

The roller wear paths on the raceway of the cup and cone showed evidence

of bearing distortion due to the unsymmetrical loads caused by the housings

deflecting, as was predicted by finite element analysis. The bearing cone had

been made more flexible to compensate; however, even the cone bending was not

enough to provide an even loading. Deflection analysis was performed using a

lighter blade weight than we currently have (Figures 6-6 and 6-7).

Thread Clamp Condition - During ground check-out for flight, play in the

trunnion support bearings was discovered which caused blade tip movement. The

clamp load was measured using a unique eddy-current technique for determining

the stretch in the trunnion threads. The technique had been calibrated during

ground testing at Peebles to substantiate the torques used at assembly. The

results revealed a loss of clamp load, and the rings were returned to Evendale

for retorquing the trunnions. This gave us the opportunity to examine all the

149

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Actuation GearStub-Shaft

90°

Figure 6-6. Bearing Housing Deflection.

0.08 Min

0.170

0+

Min

(a)

0,12

0.095

Cup

0.08 Min

0.170

Max.

Min

i(b) Cone

Figure 6-7. Irregular Wear Pattern of Roller "Path".

150

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trunnion bearings. Thus, the condition of all of the retention bearings was

known. Due to minor surface distress, coupled with increased trunnion/bearing

thread torque, two bearings were replaced; however, all other bearings were

acceptable for flight testing as is. The consumable parts (seals, shims, and

grease) were also replaced where necessary.

6.2 MEASURED TEMPERATURES

6.2.1 Rotor Support Main Bearings

The main bearings were instrumented initially with three thermocouples at

each bearing location. The thermocouples were at 120 ° circumferential loca-

tions; however, loss of signal and lack of available recording channels left

only one gage at each position providing good data.

Steady-State Temperatures

The bearing temperatures were influenced by environment (oil, metal, and

cavity temperatures) and by engine speed. The intershaft bearings ran hotter

than the Stage 2 rotor supports, as would be expected due to the higher rela-

tive speed (Figure 6-8).

The Stage I rotor bearing temperatures increased from 240 ° F at 700 rpm

(idle) to 340 ° F at 1393 rpm (maximum thrust). The Stage 2 rotor bearing

temperatures were lower, with that of the 2B bearing rising 50 ° F, to 250 ° F

at maximum thrust. Oil supply temperature rose 100 ° F over the same ranges.

Transient Temperatures

The bearings did not pick up temperature very rapidly during fast accels.

A 40 ° F rise in intershaft bearing temperatures is attributable to increased

centrifugal loads. The Stage 2 rotor support bearings changed little during a

2-minute accel to full power. However, a 4-minute accel/decel demonstrated a

similar 40 ° to 50 ° F rise in all bearings (Figures 6-9 and 6-10).

6.2.2 Fan Retention Thrust Bearings

The fan retention tapered roller bearings were not instrumented; however,

thermoeouples were placed inside the trunnion adjacent to the bearing. Since

151

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i,

3

hl

2OO

I_0

100

_0

0

3OO

I00

_0

(a)

u

i

(b)

0,_

1R

b

Steady State RDGS

I I I l I I

4 8 12 16 20

¢n_u,or_.)24

1R

IB

2R

2B

-- • .___%_----- - _;- _

[] 2R + 1R 0 1R _ oR

IIJILD 00.3 - R00t B1-102

Steady State RDGS

I I I I I I I I

0.7 0.9 1,1 1.3

O_umnd=)

P

Figure 6-8. Main Propulsor Bearings.

152

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LL

W

F-

LU

LL

Ld

Ld

1GO

1OO

O

2R

Transient RDGS

| I I I I I I I i I I I I I i i I |

20 40 60 80 100 120 140 180 180 :2CX)

Figure 6-9.

•_ (_=,)

Main Propulsor Bearings, 2 Minute Accel to

24,000 ibs Thrust.

Q 21R + 1B @ IlR A ,._

3:)O

f_

0

o

Transient RDGS

40 BO 1"_ I00 2QQ 240 :2;BO

_ME (..=,)

Figure 6-10. Main Propulsor Bearings, 4 Minute Accel/Decel

to 1200 rpm.

153

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this is a closed cavity, the temperature would not be too far from that of the

bearing.

Steady-State Temperatures

The forward hub temperatures rose from approximately 340 ° F at 700 rpm to

about 390 ° F at 1393 rpm. The aft hub went from 190 ° to 250 ° F in the same

range (Figure 6-11).

Transient Temperatures

There was little difference between a 2-minute accel and a 4-minute

decel, in that the temperatures of both forward and aft hubs rose about 20 ° to

40 ° F. This is due to the fact that the thermocouples were in a closed cavity

anti, although influenced by turbine air gas temperatures, they are shielded

from the immediate effect by the fan ring bulkhead plate (Figure 6-12).

154

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4OO

.3OO

2OO

100-

o

0.5

o _ HI.IR 4" 6Fr I-IjR

Steady State Readings

| I I I I I I I I

0.7 0.9' 1.1 1.:q(T_u,,',_s)

1.5

Figure 6-ii. Forward and Aft Fan Hub Temperatures.

I,

W

a.3

4OO

3OO

2OO

10000

o _o HUB A _ HUBTransient Readings

I I I I I I I I I I I I I I I I I I I

0 20 40 60 £0 1(:]0 120 140 1_ laO 200

TIME (_s)

Figure 6-12. Forward and Aft Fan Hub Temperatures, Accel to

Full Power.

155

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7.0 PERFORMANCE

This section describes the steady-state data acquired during Build 3

testing at Peebles Site 3D and the various analyses employed to support the

test effort. The major items covered are as follows:

• Data summary

• Data reduction methodology

• Comparison between pretest predictions and reduced test data

• LCF cyclic testing and resultant deterioration

• Comparison between ground and flight pretest cycles and reducedtest data

• Overall summary

• Key results

• Conclusions.

7.1 DATA SUMMARY

During Build 1 testing at Site 4A, a total of 46 steady-state DMS (data

management system readings were taken, none of which were usable for perform-

ance analysis since all the points were recorded mainly for mechanical check-

out and were not stable.

During Build 2 testing, 104 steady-state DMS readings were taken at Site

4A, and an additional 31 at Site 3D. Some of the data points were usable for

analysis.

Table 7-i shows the breakdown of steady-state DMS readings for Build 3.

Note that of the total of 358 data points recorded, 27 readings were expressly

taken to define the baseline performance, with an additional 48 data points

recorded to map the UDF 'M performance at off-schedule conditions. Table 7-2

shows the chronology of the acquired data.

Appendix A presents a listing of the Build 3 steady-state data points.

7.2 DATA REDUCTION METHODOLOGY

Figure 7-1 shows the schematic of the engine and the positioning of the

performance-related instrumentation.

156

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Table 7-1. Data Summary.

Breakdown of Steady-State DMS Readings

for Build -03.

Zero Readings

Ground Idle Readings

Flight Idle Readings

Trim Balance Data Readings

Bleed Evaluation Readings

EPR Power Hooks

Down Power Calibration

LCF CyclesMiscellaneous Data Points

Points

86

2

16

36

28

48

27

102

15

Total 358

Table 7-2. Chronology of the Acquired Data.

Breakdown of Steady-State DMS Readings

for Build -03

Readings Date Points

1 to 5

6 to 15

16 to 31

32 to 47

48 to 56

57 to 70

71 to 77

78 to 149

150 to 197

198 to 209

210 to 251

252 to 304

305 to 330

331 to 358

6/20/86

6/23/86

6/24/86

6/25/86

6/26/86

6/29/86

6/30/86

7/I/867/3/86

7/4/86

7/5/86

7/6/867/7/86

7/8/86

5

I0

16

16

9

14

7

72

48

12

42

53

26

28

Total 358

157

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idr

|

• "_ • C

_ ,

>

+

4(1;

0

0

0

_J

m

158

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IPC

Inlet flow - From inlet total rakes, circumferential pressure

statics, physical area, flow coefficient

Pressure ratio - From inlet and exit total pressure rakes

Efficiency - From inlet and exit total pressure and temperature

rakes.

HPC

Flow - From HPT flow function (iteration)

Pressure ratio - From IPC exit conditions and stratification logic to

define inlet pressure, PS3 correlation to define P3

Efficiency - From matching core overall performance.

Bypass Duct

Flow - From IPC exit conditions and stratification logic

Pressure drops - Measurements at IPC exit and duct exit

Temperatures - Measurements at IPC exit and duct exit.

Combustor

Efficiency - Assumed (map value)

Pressure drops - Assumed (map value)

Fuel flow - Measured (including all parameters for corrections).

HPT

All parameters assumed (map).

IPT

Efficiency

Exit from IPT

- Energy balance with IPC

- (T46) - From fuel flow and inlet airflow, together

with assumed secondary flows

- (P46) - Measured.

Mixer Frame

Assumed losses, mixing characteristics.

Secondary Flows

Assumed level and distribution (based on model test and some

measurements).

Power Turbine

Inlet - Mixer frame exit conditions, secondary flows

Exit - From total pressure and temperature rakes

159

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Power

Efficiency

Core Nozzle

Inlet

Exit

Thrust

Installed

- From airflow, delta temperature

- From delta temperature and delta pressure.

- PT (power turbine) exit conditions

- Ambient conditions.

- Measured

Core component - From PT exit conditions, nozzle coefficients

Uninstalled From installed thrust, assumed drags

UDF TM component From uninstalled thrust and core thrust.

7.3 COMPARISON OF PRETEST PREDICTIONS AND REDUCED TEST DATA

The steady-state data points used for the performance evaluation were

restricted to the down power calibration and maximum power points recorded on

July I and July 3, 1986. Data points taken for UDF TM mappingEPR (engine pres-

sure ratio) power hooks were recorded on July I, 1986. The pretest prediction

used to compare the test data is the Status D5C cycle. The Status D5C cycle

was expressly defined for Build 3, and it includes the following major items:

• PT derates on efficiency due to open clearances and the blade

damper pins

• PT flow function adjustments for open clearances and the blade

damper pins

• Revised exhaust nozzle characteristics as a result of new

nozzle hardware.

Core Performance - Figure 7-2 shows the overall core (F404) temperature

ratio versus pressure ratio. Note that the core performance is approximately

as predicted at takeoff power conditions and is better than predicted at lower

powers (70% takeoff and below). Figure 7-3 presents IPC stall margin versus

corrected flow, illustrating that the IPC operating line was approximately as

predicted.

Power Turbine Performance - Figure 7-4 shows the PT flow function versus

the PT energy function. The PT flow function was within 0.5% of the predicted

value at higher powers (80% takeoff and above). Figure 7-5 illustrates the PT

160

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efficiency versus PT energy function. The efficiency was within +1.5% of the

predicted value and within the scatter range observed in LP turbines of large

turbofan engines.

UDF TM Performance Figure 7-6 depicts the UDF TM thrust coefficient versus

power coefficient. Note that the test data describe a shallower slope than

predicted. Thrust coefficient is approximately 4% worse than predicted at a

power coefficient of 1.95 (takeoff condition), nearly as predicted at power

coefficient of 1.70 (92% takeoff), and approximately 4% better than predicted

at power coefficient of around 1.32, which covers a range of power from 30% to

80% takeoff thrust. Figures 7-7 and 7-8 compare predicted versus actual UDF TM

rotor blade pitch angles for front and rear rotors, respectively.

Overall Performance - Figure 7-9 shows corrected installed specific fuel

consumption (SFCIIR) versus corrected installed thrust (FNIIQA). The SFCIIR

can be seen to be approximately 4% poorer than predicted at takeoff power. At

92% takeoff thrust the SFCIIR is about as predicted; whereas, at 80% takeoff

thrust and below, SFCIIR is 4% to 6% better than predicted. Most of the dis-

crepancy between actual and predicted performance is due to the characteristic

exhibited by the UDF TM, as discussed above under "UDF TM Performance." Magnitude

of overall improvement in excess of that expected from the UDF TM performance

at 70% takeoff thrust and below is due to the core engine performance being

better than predicted, as discussed in "Core Performance."

Nozzle Performance - Between Builds 1 and 2, a redesigned stationary

exhaust nozzle (centerbody) was installed on the engine. The original plug

was analytically predicted to have flow separation at cruise conditions. The

plug was redesigned so that no flow separation would occur at any flight con-

dition. Figure 7-10 compares the original and redesigned plug lines. Scale

models were made of both the original and redesigned plugs, and then tested.

Figure 7-11 makes a comparison of the separation parameter (Fse p) for the two

plugs at cruise conditions, illustrating that the new plug lines would keep

F below potential separation conditions. Figure 7-12 shows a comparisonsep

between predicted and actual engine test data for both plugs to demonstrate

good match between prediction and data. Figure 7-13 presents a comparison

between predicted and engine test nozzle flow coefficient versus core engine

pressure ratio (P46Q2). Note that at P46Q2 of 2.9 and below (approximately

165

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172

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80_ takeoff thrust and below> the calculated flow coefficient is within +I_ of

the prediction. However, at takeoff power there is a discrepancy of about 3_.

This is probably due to the fact that the flow coefficient is sensitive to the

[IDFTM exit pressure which was not a measured parameter, but rather, the value

being ass_ed from the performance maps. This discrepancy is not a concern,

since 3_ change in flow coefficient changes sfc at thrust by only 0.005_.

EPR Hooks - These test points were run to map UDF TM performance at off-

schedule speeds. The test was conducted at six different propulsor rotational

speeds where the propulsor speed would be held constant, and core power level

would be varied by demanding various EPR levels; hence, EPR hooks.

Figure 7-14 shows installed corrected specific fuel consumption (SFCIIR)

versus installed corrected thrust (FNIIQA) for on-speed schedule and constant

propulsor speed pretest prediction, with Figure 7-15 showing the equivalent

reduced test data. Note that the on-speed schedule lines on both figures are

the same as those found in Figure 7-9. The test further proved that the UDF TM

characteristics were different than predicted, with significantly higher speed

sensitivity than prediction.

7.4 LCF CYCLIC TESTING AND RESULTANT DETERIORATION

The LCF testing involved running the engine through a power cycle as is

illustrated in Figure 3-54; a total of 100 complete cycles were run. In the

following comparisons, a sample of early data is compared with a sample of

late data in order to quantify the magnitude of scatter as well as the magni-

tude and source of deterioration. Figure 7-16 shows that the wind conditions

were relatively consistent, and all data points, except one, were within the

prescribed performance testing wind envelope.

Figure 7-17 shows that at corrected installed thrust, corrected installed

specific fuel consumption deteriorated by approximately 0.040_.

Figure 7-18 demonstrates that at EPR, corrected installed thrust followed

the predicted trends and showed no signs of degradation. This indicates that

the power extraction at EPR by the LP turbine and the thrust produced by the

UDF TM for LP turbine power remained unchanged during the tests. Figure 7-19

174

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180

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reveals that at EPR, core engine temperature ratio was essentially unchanged,

and the core showed little or no signs of deterioration.

Figure 7-20 illustrates that at EPR, intermediate power compressor (IPC)

efficiency was down 0.60 points during the latter part of the test compared to

the early part of the test. However, Figure 7-21 shows that at EPR, IPC flow

follows the predicted trends, confirming that inlet flow and core engine power

output remained consistent. This implies a dirty IPC, which is further sub-

stantiated by Figure 7-22 indicating that the flow versus speed characteristic

of the IPC deteriorated, with approximately 0.50% drop in corrected IPC flow

at corrected IPC speed.

In general, there was no evidence of mechanical deterioration, with

performance degradation due mainly to a dirty intermediate power compressor.

7.5 DEFINITION OF PREFLIGHT TEST CYCLE

The base cycle used for Build 3 pretest predictions was the Status D5C

cycle. Listed beiow are the changes made to the Status D5C cycle to define

the preflight test cycle; this being the Status D8B cycle:

• Modify IPC flow-speed characteristics

• Modify IPC efficiency characteristics

• Modify HPC flow-speed characteristics

• Modify HPC efficiency characteristics

• Revise bypass duct losses and effective area

• Scale IPT efficiency

• Modify LPT efficiency characteristics

• Modify LPT flow function characteristics

• Modify UDF m thrust coefficient characteristics at Mach No. = 0.00,

no change at Mach No. _ 0.20

• Use NASA MPS test-derived UDF _ maps for Mach number _ 0.67

• Extra cooling air scoops for telemetry system modeled.

7.6 COMPARISON BETWEEN GROUND PRETEST CYCLES AND REDUCED TEST

DATA

The following comparisons between the ground pretest cycle (Status D5C),

flight pretest cycle (Status D8B), and reduced test data are made to compare

181

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183

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the starting status, ending status, and data used to define the ending status

against each other.

Figure 7-23 shows the core temperature ratio versus core pressure ratio,

Figure 7-24 illustrates LPT flow function versus LPT energy function. Figure

7-25 demonstrates IPC stall margin versus IPC corrected flow. Figure 7-26 is

a comparison of UDF TM thrust coefficient versus UDF TM power coefficient. Figure

7-27 depicts the overall performance, corrected installed sfc versus corrected

installed thrust. Note that in all of the above comparisons, the Status D8B

cycle more closely matches the test data than did the Status D5C cycle.

7.7 PERFORMANCE SUMMARY

In the testing of the UDF TM engine at Peebles, the following performance

and capabilities were demonstrated:

Performance

• 25,000 ibf installed corrected thrust

• 0.232 ib/hr/ibf installed corrected specific fuel consumption

• 15,000+ physical total shaft horsepower.

Capabilities

• Running at full power statically

• Data was repeatable statically

• Prediction of low speed, low pressure, counterrotating turbine

performance with an accuracy comparable to that of high speed,

conventional, low pressure turbines.

Comparing data recorded early and late in the LCF testing, performance

deterioration was confined to a dirty IPC; there was no evidence of mechanical

deterioration.

7.8 KEY RESULTS

The F404 gas generator provided repeatable and predictable performance

and was better than predicted at lower powers (below 70?0 takeoff power).

UDF TM blade performance sensitivity to rotational speed was much greater

than predicted.

185

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At power coefficient = 1.32, thrust coefficient was 4% better than pre-

dicted (approximately 60% takeoff power). At power coefficient = 1.95, thrust

coefficient was 4% worse than predicted (approximately 100% takeoff power).

Power turbine efficiency was approximately as predicted, being within

+1.5 points over the major portion of the operating range. The flow function

was within +0.5% of prediction at high powers (above 80% takeoff thrust).

Overall performance was better than predicted up to 92% takeoff power

(23,000 ibf corrected installed thrust), but was poorer than predicted beyond

92% takeoff power (23,000 ibf corrected installed thrust) due to UDF TM speed

sensitivity as noted above.

At 60% takeoff thrust (15,000 ibf), sfc was approximately 5.50% better

than predicted. At 92% takeoff thrust (23,000 ibf), sfc was approximately as

predicted. At 100% takeoff thrust (25,000 ibf), sfc was approximately 4.00%

worse than predicted.

191

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8.0 ENGINE OPERABILITY

The most important operability concern with the GE36 proof-of-concept

engine is the stability of the IPC (F404 compressor). Replacing the F404

variable area exhaust nozzle with the GE36 UDF TM propulsor assembly reduced the

Station 48 (F404 nozzle/UDF TM power turbine inlet) flow function by about 15_.

This raises the IPC operating line (Figure 8-1) and reduces the stall margin.

To help increase IPC stall margin and ensure stall-free operation of the IPC,

two design modifications were incorporated:

• Variable Stator 1 and more closed IGV schedule (raises the IPC

stall line)

• IPC bleed system (lowers the IPC operating line).

The GE36 proof-of-concept HPC has an adequate stability margin since the

stall and operating lines are similar to those for the F404. Due to the more

limited operating range and flight envelope encountered during GE36 ground and

flight test, the stall margin requirements are lower.

8.1 [PC STALL MARGIN

Steady-state IPC operating lines at 2,750 ft/OMn/+31 ° F and at 38,000 ft/

0.80Mn/ISA, as predicted by the Status D6C cycle model, are shown in Figures

8-2 and 8-3. Also shown is the nominal IPC stall line and the, statistically,

worst-case IPC stall line which includes analytical estimate of effects due to

deterioration, inlet pressure distortion, and IPC tracking error. The nominal

stall line shown in these figures is from the F404 green run results with the

GE36 variable geometry schedule (Figures 8-i and 8-4).

Transient cycle model predictions of IPC operating line migration during

decel transients from maximum power with no IPC bleed and with maximum IPC

bleed are included in Figures 8-2 and 8-3. These predictions demonstrate the

need for, and potential of, the IPC bleed system to prevent IPC stalls during

rapid decel transients.

192

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195

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60

Closed

_0

50

oO

J 40,-.-t

<

O

*_ 30

0

m 20

0

_ 10

Open 0

-" "_--_- -- Ground

, _ _ Test

F404 Nominal_ Ik I

40 50 60 70 80 90 i00

Corrected IP Rotor Speed - % _ere 100% = 13,270 rpm

Figure 8-4. IPC Stator Schedule.

196

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8.1.i IPC Bleed Control System

The IPC bleed valve position is controlled by the DEC. The control logic

opens the bleed valve in response to any one of the following inputs:

a. d(PLA)/dt throttle retard rate > threshold

b. PLA - throttle step > threshold

c. d(P)/dt - IPC exit pressure decay rate > threshold

d. IPC P/P - scheduled maximum allowable P/P (f[XN2R]).

Thresholds "a" and "b" indicate a decel transient condition to the con-

trol, in which case additional IPC stall margin could be required. Threshold

"c" would be exceeded in the event of engine surge. Schedule "d" is designed

to maintain a minimum level of IPC stall margin under all normal operating

conditions.

If thresholds a, b, or c are exceeded, the control logic is designed to

"kick" the valve full open, hold for 5 seconds after the last demand for full

open, and then ramp close in 5 seconds. The slow closing will avoid transient

pressure pulses. In addition, for Input c, the control downtrims fuel flow to

maximum authority, further decreasing engine system pressures. If scheduled

Value d is exceeded, the control modulates the bleed valve to maintain the

scheduled maximum allowable IPC pressure ratio. In the event multiple inputs

are received, the valve kicking logic takes precedent.

8.1.2 Control Threshold for Throttle Retard Rate

Figures 8-2 and 8-3 show the PRS usage (stall pressure ratio normalized

to stall line), as predicted by the transient cycle model, during decel tran-

sients from maximum power without IPC bleed. Shown are decels at various PLA

rates at 2,750 ft/OMn/+31 ° F and at 38,000 ft/0.8Mn/ISA. Also indicated in

these figures is the current status available PRS and the minimum available

PRS as a worst-case estimate. Figure 8-5 shows that with the current level of

available margin at SLS (sea level static) conditions, an IPC stall would be

predicted during a throttle chop from maximum power without IPC bleed, yet a

decel transient at -lO°/second d(PLA)/dt would not consume all of the current

available margin. A decel transient from high power at -10°/second d(PLA)/dt,

without IPC bleed, was successfully accomplished without stall during ground

197

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14

12

_Du I0

g 8

_ 6

°,-Ir/lm

_ 4

< 2

0

2O

| l I |

2750ft/M.O/+31 ° F ATam b

_ I N° IPC B_eed I

Clean ---I

[ [ X I Available _I

I I X[ APES

< -9olsec--/// ] _"",,_,. Worst Case

30 40 50 60 70 80 90 i00 II0 120

W2R , ibm/sec

Figure 8-5. Predicted IPC APRS Usage During Throttle Decels; 2750 ft.

198

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testing; thus, confirming the analytical prediction. At altitude, however,

the operating line migration during a decel exceeding -9°/second d(PLA)/dt is

expected to consume all of the available margin, even at the current quality

of the engine (Figure 8-6).

Considering the statistically worst-case IPC stability condition, Figures

8-5 and 8-6 show that even an IPC bleed kick threshold of -5°/second d(PLA)/dt

is not sufficient to assure stall-free operation. This illustrates the neces-

sity of the maximum allowable P/P schedule (bleed valve modulation).

8.1.3 Maximum AHowable IPC Pressure Ratio Schedule

The maximum allowable IPC pressure ratio (P15/P2 versus XN2R) was set at

approximately 1_ above the engine ground test operating level (Figure 8-7).

This was accomplished at the end of ground testing, after analysis of control

measurement data. The effect of the expected control measurement variation on

this maximum allowable P/P schedule was determined to be equivalent to approx-

imately +0.015 PRS (pressure ratio schedule).

This bleed modulation function will be effective during steady-state

operation if the IPC operating line migrates upward due to the altitude/Mach

effects (not predicted) or deterioration effects. It will also be effective

during decel transients which do not exceed IPC bleed kick threshold levels.

8.1.4 Final IPC Bleed Control Status

During the engine ground testing, the IPC bleed system was successfully

demonstrated; proper mechanical function and pressure relief capability were

verified. Each of the control inputs (a through d) were individually checked

and verified. By the end of the ground test, threshold levels were adjusted

to appropriate levels, as follows:

a. d(PLA)/dt (throttle rate threshold = -5°/second)

b. PLA (throttle step threshold = -2°/0.25 second)

c. d(Pl5)/dt (IPC exit pressure decay rate threshold = -20%/second

d. PIS/P2 versus XN2R (scheduled maximum allowable IPC pressure

ratio set at approximately I% above engine ground test operat-

ing level).

199

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14

12

i0

8m

= 6

co

_ 4

a::

"_ 2

0

40 140

I l l38,000 ft/0.8Mn/ISA

o _ No IPC Bleed-15 /sec

--- _i3O/sec f _

-_/sec __ ]

_ o__--I I _[--- _--Clean

_-5°/sec _X _ I Avaiilable APRS

5{) 60 70 80 90 I00 Ii0 120 130

W2R, ibm/sec

Figure 8-6. Predicted IPC APRS Usage During Throttle Decels; 38,000 ft.

200

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Cq

oQD

4.5

4.0

3.5

3.0

2.5

2.0

1.5

1.0

30

Control Schedule for PC Bleed Modulation

(Maximum P/P Schedule)

* Flight Test Schedule

40 50 60 70 80 90 i00

PCN2R, percent

Figure 8-7. Maximum Allowable IPC Pressure Ratio.

201

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Figures 8-8 and 8-9 show the predicted PRS usage during decel transients

at 2,750 ft/0Mn/+31°F and at 38,000 ft/0.SMn/ISA, with bleed system control

thresholds set as defined previously. For decel transients which exceed -5°/

second d(PLA)/dt, the kick function is effective, and the PRS transient usage

is zero. This was demonstrated during a throttle chop from high power in

which the bleed valve kicked open, and the transient data indicated that the

IPC operating line during decel was lower than the steady-state level. For

decel transients which do not exceed -5°/second d(PLA)/dt, the bleed modula-

tion function is effective. If the operating line migrates above the steady-

state ground test level, the control will modulate the bleed to maintain the

maximum allowable P/P during the decel.

Figures 8-8 and 8-9 show that the IPC bleed control system should prevent

the IPC operating line from migrating to even the worst-case stall line, thus,

assuring stall-free operation.

8.2 TRANSIENT TESTING EXPERIENCE

Table 8-I summarizes the significant transient tests conducted. Small

PLA acce[s and decels were conducted to verify control functions and to adjust

control gains to appropriate levels to ensure control stability; control fault

trips were checked, resulting in throttle chops and stopcocks.

Several unintentional decel transients were encountered, both operator

and control initiated, due to instrumentation faults and operating limits.

For cycle operability evaluation, large PLA accels, decels, and bodes were

conducted. All transient testing of the demonstrator engine during ground

testing was accomplished without adverse results.

8.3 ENGINE TRANSIENT PERFORMANCE ANALYSIS AND PREDICTIONS

The transient cycle model is used to predict the operating line migration

of the compression components during engine transients. In order to foresee

any stall or operational problems prior to transient testing, good agreement

between the cycle model predictions and test data is necessary. Two engine

transients conducted during the ground test were simulated by the transient

cycle model with good results; a throttle chop from 97% thrust and a throttle

202

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14

12

i0

_ 8

_ 6',-"1

m

1-4

_ 4

<3

2

I i I

2750 ft/M.O/+31 ° F &Tam b

_I IPC Bieed SY itiieaEifectiv i

I Available APRS - -

P --I ---- I -- 'A_aa&ilRble

-->-5 /_FRS : O) _-__Iwors_ica '' ""_.X_/---'_:--t Case --

<-5°/see IPC Sieed Modulation-_ _ Il i .i I i

20 30 40 50 60 70 80 90 i00 ll0 120

W2R , ibm/sec

Figure 8-8. Predicted IPC _PRS Usage During Throttle

Decels; 2750 ft.

203

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14 I ; i i

38,000 ft/0.8 Mn/ISA

12_ii_i_ IPC Bleed System Effective_ lO

I Available APiS

_ .

_ ,I l "_"---_,1 I_-_:::::_:_y_

o .,_:o> ,\--_1 ,' I2--<-5 Isec IPC Bleed Modulation --_

40 50 60 70 80 90 i00 ii0 120 130 140

W2R , ibm/sec

Figure 8-9. Predicted IPC APRS Usage During Throttle

Decels; 38,000 ft.

204

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burst to 20,000 thrust. Figures 8-10 and 8-11 show the transient cycle model

simulations, as compared to the test data, for selected parameters.

The results of these comparisons provide confidence in transient cycle

model predictions of IPC operating line migration during decel transients

which were used in designing and optimizing the IPC bleed control system.

Date

2-09-86

4-18-86

7-8-86

7-8-86

7-8-86

7-8-86

Table 8-1. Significant Transients - GE36 Proof-of-Concept.

Maneuver Reason

Throttle Chop from 24,000 Fn

Stopcock at II,000 Fn

I0 Throttle Bursts to 18,000 Fn

2 Throttle Bursts to 20,000 Fn

Throttle Burst to 21,000 Fn,

Chop to Idle

2 Bodes (Chop from 20,000 Fn

to Idle, Burst to 20,000 Fn)

No. 7 Aft Blade Debonded

XN49 O/S Trip

Planned

Planned

Planned/Overspeed

Planned

2O5

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9.0 ENGINE CONTROL

This section provides a summary of the GE36 control system performance

during the ground test program performed at GE's engine test facility near

Peebles, Ohio. This summary is divided into three parts; each portion covers

the milestones associated with each of the three engine builds.

9.1 BUILD i - ENGINE CONTROL TESTING

The control system performance for Build I was successful. A limited

amount of testing was performed due to the propulsor turbine failure.

9.1.1 Speed Sensing Anomaly

During Build 1 testing, it was discovered that the speed being sensed by

the control for the forward propulsor rotor (XN48) was incorrect. A further

study as to the cause showed that the gaps in the target wheel, which was

divided into eight segments, were inducing a superfluous signal onto the mag-

netic speed-sensing pickups (Figure 9-1). This caused a higher sensed speed,

up to two times actual. The situation was initially corrected by a change

in speed signal processing. A more elegant solution was identified for imple-

mentation on Build 2. This solution consisted of locating the teeth on the

target wheel directly at the segment gaps (Figure 9-2).

9.1.2 Pitch Control

For Build I, the engine was controlled to pitch angle, rather than to

propulsor speed.

9.1.3 Gas Generator Control

The gas generator control performed as expected. The EPR (engine pres-

sure ratio), HP (high pressure) and IP (intermediate pressure) stator control,

and the control of the duct bleed system all exhibited stable operation during

this engine build testing. A new control strategy for stall avoidance and

recovery for the duct bleed system was identified during this build and was

incorporated into the control system during Build 2.

2O8

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• Original Design

• 8 Segments Total

• 1 Tooth Centered

In Each Segment

,oth Locallon

Toolh - Top View 4-- 0.016 - 0.034 Gap

Figure 9-1. Fan Speed Sensor Segments.

209

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• Redesign

• 8 Interlocking Segments

• 1 Tooth Per Segment

• Toolh Positioned On End

• Gap Width Reduced

0.012 - 0.028

Toolh - Top View

Figure 9-2. Fan Speed Sensor Segments.

210

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9.1.4 Throttle System

The throttle system was redesigned to minimize hysteresis. The resolver

was relocated to the HMU (hydromechanical unit) fuel lever to provide a more

accurate indication of fuel lever angle. A rotary potentiometer was added to

the system at the throttle converter to provide an input for PLA which would

provide for a reverse indication and redundancy for the resolver.

9.1.5 Engine Starting

Starting tests during this build achieved expected results. The engine

was first dry motored to check instrumentation and control signals. After

successful dry motoring, the engine was wet motored (engine motoring with fuel

on), also without incident. After wet motoring, the engine was fired to idle

power. The control performed as expected, successfully controlling HP rotor

speed to the HP rotor starting speed schedule. Due to the aforementioned

speed sensing anomaly, limited propulsor speed control testing was performed.

9.1.6 Off-Engine Harnesses

Crosstalk was observed on mulLiconductor off-engine cables during testing

as well as inaccuracies on alternating current type sensors. This situation

was corrected by placing twisted pairs for each circuit inside the same shield

and removing unused pairs.

9.1.7 Lube Off Bypass

Scavenge capability of the propulsor lube oil system was marginal during

Build I testing. A solution was identified for use on Build 2. This solution

involved installing in the propulsor lube system a bypass valve which allowed

lube oil into the propulsor only after a light-off had been detected by the

control. This prevented excess lube oil from entering the propulsor during

start operations, thus minimizing the effects.

9.2 BUILD 2 - ENGINE CONTROL TESTING

Due to lessons learned during Build 1 testing, Build 2 testing involved

further testing of the engine in the realms of transient testing, verification

211

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of control schedules, and modifications to the control. This testing further

demonstrated the stability of the control system. Full control was maintained

under a blade-out condition.

9.2.1 Speed Control

Closed-loop speed control (modulation of fan pitch to maintain scheduled

fan speed) was used by the control successfully for all power settings, with

the exception of reverse and windmill testing. The propulsor speed was demon-

strated to be stable from 550 rpm to 1400 rpm and from idle to 25,000 lbs,

corrected thrust. This modulation of pitch to control fan speed also was

demonstrated for Mach numbers up to 0.1 using facility fans.

9.2.2 Duct Bleed

Modifications to the duct (fan bypass) bleed control logic were verified

for PI5Q2, PLA chop, and simulated stall. A throttle chop from 97_ takeoff

thrust was performed without IPC stall; also, unrestricted throttle chops from

all power settings were performed. Figure 9-3 is a schematic of the engine

bleed system.

9.2.3 Transient Testing

A limited number of small, part, and full power throttle chops and small

part power accelerations were performed. During a throttle burst from idle

to 1150 rpm, an overspeed incident occurred. It was determined to have been

caused by the fan pitch actuator becoming force-limited due to a too rapid

response time of the gas generator. A fix was identified to slow down the

accel rate of the core by putting an accumulator on the CDP (compressor dis-

charge pressure) sensing line to the HMU. A preliminary fix was installed

on the engine which adequately slowed the core accel rate. A more polished

design was used on Build 3.

As a result of the blade-out incident, the engine was chopped from 24,000

corrected thrust to idle, then stopcocked approximately 10 seconds later. As

illustrated in Figures 9-4 through 9-8, the control system maintained complete

control during the blade-out, chop to idle, and subsequent stopcock.

212

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STA 225

ManifoldJunction

Servo Fuel

Digital/o- ._p Electronic

.... :1 co_._ol

AftNacelleBulkhead

STA 255

ButterflyValve

' "91_- 2 ports2.85" I.D.* 'q"'" 1 porl3.60" I.D.

m

Mount Beam

Fuel

\ /

leed Manifold

Electrical

Air

Figure 9-3. Duct Bleed System.

213

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, i

o

• • _!g_goooo°_" s_aJ6ap 'O00V'ldI ! I ! I ! ! I I !

0 _ _ _ 0 0 0 _ 0 0

z:OL x sqi 'lsnJqJ. o

,I0

I I I I I I I I l I,_ _, _ _ _ _ _ _ _ ,_,_

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INdO 'MOl-.Ilan..-I

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214

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¢MoI"*

x

EO.¢._

-o"

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oO.m

o

200

180

160

140

120

100

80

60

40

20

0

• 24,000 FN/8 to Idle

• P46Q2 Control Prior to Chop

• Blade Out Incident

-- 180

0194 202 210 218 226 234 242 250

Time, seconds

Figure 9-5. Throttle Chop.

OF POOR QUALITY

2].5

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• 24,000 FN/8 to Idle

• P46Q2 Control Prior to Chop

• Blade Out IncidentmFT ROTOW |LAO| LO_S - TIIBQT_LE [ilOP TO lULl

'_. ,-- [", ,i; -, " ';; I....

,.,i, i

i,!,!, I. :.i! :,',_,. ":" iI I i' ;'i P'

i :, I}..._

0 X" "" _'""--"-' _ _'"

190 198 206 214 222 230 238 246

Time, seconds

Figure 9-6. Throttle Chop.

216 OF POOR QUALITY

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OR]O;,_L;,L " __':..,,.:,= ISOF POOR QUALITY

100

90

80

70

60m i

so_ 4o

30

2O

10

_

• 24,000 FN/8 to Idle

• P46Q2 Control Prior to Chop

• Blade Out Incldent,o"'''' _.o,,oAFT IOTOR 9LRO( LOS_ - TNRO

_ 100 ,_,,__,.,: ,_.....v ,. ,,,

I: IIIII,h ,If _-,_I!_!i!_I:::I_: ":,:; " _: :I

, l,,j,,,i,it,.';,,.:,-,-,-'-,-.i....:.._ .......i..i, i'_ T; ::' _ ;; .

'-. _n LLI-I}U_!!! 'I_!I!!!!,!!'!!_'!':'!'J ! ;!"!" I' F_, v.. !lll'!lfi!li;il;!!_!llill;:_iu_ :;__', i: _li:_' I:, /-o ,:. _-l_':'._!li!_.I I:1,1,1.1 I I i / f.= "" _!lli_!l!l;l!!_l!__i_1;' 1.,_.,, I:.. ::.

An 'i_]',J:!IIIilii!i,'_lliil::ili,q_;:li.!l:I_I;l;..l';,....

,,)n _-:,-_J; m, '"d__r_lrA_ ' :1: I ! / 1

t;l il, tl :: .' , ' '

•I:I.I.I ! '\ _o k,l:.;.:.... ..: , : ,194 202 210 218 226

Time, seconds

234 242 250

Figure 9-7. Throttle Chop.

217

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0

o

u_

• • •

0

®IEm

0

! Io o.e_ ...

0-- 0

00')

m

0

0

m_<

0

4-1

0

E_

I<_

218

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9.2.4 Control Parameters

All control parameters were stable.

9.2.5 Vibration System

The vibration monitoring system proved to be functional; however, it was

discovered that there was not enough gain in the amplifier for small vibration

signals. As a result of the blade-out incident, readings were gathered that

allowed for the scaling of the vibration signal. To increase its gain by a

factor of four, the amplifier was reworked; this change was implemented during

Build 3 testing.

9.2.6 Overspeed System

The capability of the overspeed system was demonstrated during an over-

speed incident. During a throttle burst from 550 to 1150 rpm, the fan pitch

actuator became force-limited and was unable to modulate fan pitch to control

rear rotor speed. An overspeed condition resulted, which was quickly sensed

by the overspeed system which immediately shut down the engine in a controlled

manner.

9.2.7 Reverse Testing

Limited by the telemetry system, this due to high temperatures, reverse

testing for Build 2 consisted of a throttle push from idle to 1000 rpm (3000

lb reverse thrust at static conditions). Figures 9-9 through 9-12 illustrate

a transient from forward idle, to reverse idle; then throttle is pushed until

a maximum propulsor speed of 1000 rpm is obtained, followed by a decel and

return to forward idle. The fan speed is controlied by modulating pitch in

forward thrust, and PLA is used to scheduie pitch directly in reverse thrust,

hence, the difference in propulsor speeds in reverse thrust.

9.2.8 Control System Modifications

Two areas of the control system hardware were modified during this build

to improve performance. The hardware modified was the pitch actuation system

transfer valves and the watchdog monitor circuit of the control computer.

219

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20

18

16

14

8U,,,

<4 6

4

2

0

• Forward Idle to Reverse Idle

• Throttle Push to 1000 rpm Maximum Fan Speed• Return to Forward Idle

o_. -100

--_ -200

- _-300

0 -400

- -500

- -600

- -700 - -1000 40 80 120 160

Time, seconds200 240

Figure 9-9. Reverse Thrust.

220

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• Forward Idle to Reverse Idle

• Throttle Push to 1000 rpm Maximum Fan Speed• Return to Forward Idle

TR_NSItNT PLiIT

140 - 140

130

_:_ 120I"'

x 110

_100

.._90

a,,m 8o(..)a. 70

O 60

5O

4O

•" 110 i_ _ _X ';;i............. _,,-;i_ -_........

E • "1' "'1 I ,I ,pt ; , ' I I"- 100 ..,,, ...:,; I!_r" ';i'::,' :.... 'z._

O¢Z,

-- (/)

L_

-- OO

- i-1

0 .i + =1 ,

• n.. | , i .| .. g .... | ,_,=....= ., .t_

70

60

so-t40

0

• ii ..... /;.:":I':'

j/4O

%.

80 120Time, seconds

iI

i'-- |

i

I I

160 200

Figure 9-10. Reverse Thrust.

221

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• Forward Idle to Reverse Idle

• Throttle Push to 1000 rpm Maximum Fan Speed.• Return to Forward Idle

TmANS I( NT PLOT

110 -- 110

100

_o 9OX

E 80O.t_

-d 70

_ so

_ 5O

_. 40o

300 2O

10

--_o100 -_ , _ ............ ,.K__/-

-- 90 _'_

_ so

, i_ 70_ - .-_ L......

60 - _ f_¢/) i

-- _502I_. 40

_ 3o--020 ..............

I,I.

-- n 100 20 60 100 140 180 220

Time, seconds

Figure 9-11. Reverse Thrust.

222 ORIGINAL PPGE _SOF POOR QUALITY

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ORIOLN_.Lr_RQ_ ISOF F_ro::_' Q_-,v",LITy

• Forward Idle to Reverse Idle

• Throttle Push to 1000 rpmMaximum Fan Speed

• Return to Forward Idle

TRONSI|N_ PLOT

40 80 120 160Time, seconds

200

Figure 9-12. Reverse Thrust.

223

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The transfer valves exhibited erratic performance during the beginning

of this build. It was determined that the filtering of the hydraulic oil was

inadequate. To correct this problem, the filters for the hydraulic system

were changed from 5 micron to 3 micron.

The watchdog monitor circuit on the control initiated several inadvertent

automatic shutdowns, later discovered to be caused by noise on the backplane

of the control propagating into the watchdog circuit and inducing erroneous

pulses. This condition was corrected by adding filters to all high speed

lines on the watchdog circuit card.

9.3 BUILD 3 - ENGINE CONTROL TESTING

Build 3 testing was the most successful portion of the ground test, both

in terms of time on test and control system testing.

9.3.1 Endurance Testing

Pitch and EPR controller gains were optimized during the 100 LCF cycles

which were performed (Reference Figure 3-54).

9.3.2 Core Response Modifications

The gas generator response time was reduced with an orifice/accumulator

system (Figure 9-13) in the CDP (compressor discharge pressure) line to the

HMU (hydromechanical unit) and a control rate control. This modification was

due to an overspeed incident caused by a force-limited actuator. The orifice/

accumulator was sized to give an 8-second idle-to-rated-thrust response.

9.3.3 Reverse Thrust Testing

Reverse testing during Build 3 achieved maximum speeds of 850 rpm limited

by high telemetry temperatures.

9.3.4 UPS (Uninterruptable Power Supply) Systems

The UPS systems for the control were successfully demonstrated during

this build. The UPS powered the control computer, the overspeed unit, and the

peripheral computer. The UPS systems were tested, by removing/reconnecting

224

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TO MEC

Ps3TAP-_--____ It_-_FAN DUCT CASE

Ps3 LAG ORIFICE (_ .03 e)

CHECK VALVE

L

.02

WEEP );(HOLE

TO Ps3 LAG VOLUME

(= 30 IN 3)

Figure 9-13. PS3 Accumulator Configuration.

225

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input power, both statically and with the engine running without affecting

control performance in any way.

9.3.5 Transient Testing

Transient testing consisted of accelerations, decelerations, and throttle

bodes. The controller was found to exhibit an underdamped response above 2.85

engine pressure ratio.

Figures 9-14 through 9-17 depict a throttle burst from idle to approxi-

mately 18,500 lbf. Satisfactory control response was demonstrated.

9.4 SUMMARY

Testing of the UDF rM provided valuable data and demonstrated the viability

of the unducted fan concept and its control system.Q

Further, test results verified that the control system concepts of using

EPR as the thrust parameter and utilizing EPR to schedule propulsor speed are

sound. The modulation of pitch to maintain scheduled propulsor speed has been

demonstrated statically and for Mach numbers up to 0.I.

226

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100 -

90

80

70

60

_ 5o

5 4on

Z_ 30

2O

10

2

Time, Seconds

Figure 9-14. Throttle Burst.

227

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ORIGhNAL P_,GE iS

OF POOR QUALITY

100 - 160 - 160

9O

8O

7O

6O(/)

o_ 50

2O

10

- 150

- 140

- _ 130

- _ 120

110

- = 100

- 8O

130-- 120

_ A".+It

- _ 1010

u.

- [] 90

- 8O

- 7O

- 600 4 6 8 10 12 14 16

Time, Seconds

18 20

Figure 9-15. Throttle Burst.

228

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OF PO0;-_ QUALITY

100

90

80

7O

CR

60014)

a 50

.JQ.

40ZX

30

20

10

200_

180

- 160

- 140Ea.

- .1=- 120

- _ 100

Un

- 800

- 60

- 40

- 20

- 0

- 2OO

- 180

- 160

I I 1 I I i

/ :t

!

i

._ _ 7.

i

I

I....... L --

i

: I

16 18 20

Figure 9-16. Throttle Burst.

229

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OF POOR QUALITY

20-

18-

16-

=E 14 --O.

3" 120

Ix.

® 10 -=1u.

ZX 8

6

4 -

2--

O-

200 --

180

160

140

_120

gP 100

0 8O

6O

40

2O

0

100 , , , , ,_ , , _ , ,

90

eo _! , I ....

7O ,

60 - -

o,o /_: ,, I,o ]2°1 ._ . .... I i =

10 ._0_, L " - " I' ; -

0 2 4 6 8 10 12 14 16 18 20Time, Seconds

Figure 9-17. Throttle Burst.

230

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10.0 NACELLE STRUCTURES

No problems occurred for any of the nacelle structures components during

ground testing conducted at Peebles, Ohio.

The fan blade airfoil loss provided valuable data pertaining to the

nacelle structural and dynamic integrity. No structural damage occurred, and

the isolators absorbed the unbalance as expected. Based on data taken during

the airfoil loss, the isolator/mount structure provided a minimum margin of

safety of 0.47 and an average margin of safety of 2.54 for all components.

Strain measurements taken on the strut during ground testing revealed

extremely low stress levels. The maximum stress level recorded, 1.4 kpsi peak

to peak, corresponds to a margin of safety of 80.4 based on shear strengths of

the strut material. The minimum margin of safety was found in the composite

mid-fairing. Based on the interlaminar shear strength, this margin was 2.7,

which is an acceptable figure. Based on the strain measurements, the acoustic

fatigue of the strut and fairings was deemed to be of little concern.

10.1 FAN BLADE AIRFOIL LOSS

The fan blade airfoil loss incurred on February 9, 1986 caused a 262,000

gm-inch (577 ib-inch) unbalance load. This failure occurred at a fan speed of

1371 rpm and a thrust level of 24,000 pounds. Engine, isolator, mount beam,

and strut acceierometers were located as shown in Figure 10-I.

At blade-out, the rear-mount horizontal vibration ievel reached 200 mils

double amplitude, while its normal level is 10 mils. The front mount along

the horizontai axis reached 95 miis, while its normal levei is I5 mils. The

engine was then chopped to idle (680 rpm) in 1.23 seconds, where it remained

for 9.0 seconds before being shut down. Vibration levels of the vertical axes

of the front and rear mounts reached 200 mils DA (double amplitude) from their

normal ievels of 2 miis each. As attested in Table 10-1, the maximum vibra-

tion leveIs occurred in the rigid body modes during coast down.

Mount loads were estimated based on relative motion across the isolators

and on the isolator dynamic spring rates (from the Barry Qualification Test

231

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7-

_ < ---_

_ wo0_J

<

_ b

if)

m

0 °

0if)

0

o,r,,I

s__r,4e-'

4-4

4_

o

o

ooi

¢xl

o0o

x

7o

a0

232

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Report). Table 10-2 shows that these loads were well below the design loads.

The minimum margin of safety turned out to be 0.47, which was for the rear

mount along the axial axis at 460 rpm; the load it carried (40.9 kips) was the

maximum load for the system. The average margin of safety for the isolators

was 2.54.

Sensor

Front Mount Vertical

Front Mount Horizontal

Right Rear Vertical

Right Rear Horizontal

Right Rear Axial

Left Rear Vertical*

Left Rear Horizontal

Left Rear Axial*

Table I0-I. Vibration Response.

Displacement, mils DA

1370 rpm

8O

95

170

200

95

120

Idle (680 rpm)

200

50

200

105

330

130

Coast Down (rpm)

560 (460)

385 (280)

450 (200)

165 (200)

980 (460)

430 (200)

* Sensor Inoperable Before Event

The overall response of the isolators indicated that they functioned as

designed, significantly reducing the motion at the pylon/mount interface and

softening with increased loading. The resonant speeds of the system decreased

for the airfoil loss event. Further, the isolators reduced mount loads on the

engine and pylon. These loads were well within design limits.

Physically, the isolators performed as designed during the airfoil loss.

No wear or deformation of the isolator structure was incurred (or in any other

structure). The Met-L-Flex wire mesh showed some minor deformation in the aft

isolators. The mesh in the front isolator was undamaged. All isolators were

sent to the manufacturer, Barry Controls, for inspection and testing. Despite

the fact that all the load-deflection data for the isolators indicated little

233

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0

0u_

,.-6<

0

,._

0

0:E:

I

-r,4 _

0

0

;--..i

234

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change and were still within limits, the wire mesh in the aft isolators was

replaced. The front isolators were used "as is."

Predictions that maximumloads would occur in subidle modeswere veri-

fied. However, modes were not matched for the front mount (Tables 10-3 and

10-4). Also, as predicted, the highest load occurs on the aft mount in theaxial direction. Both magnitude and speed were in good agreementwith predic-

tion; however, the front mount loads measured were higher than predicted.

i0.2 STRAIN EVALUATION OF THE STRUT

Extensive strain tests were performed on various strut components during

ground testing. Corresponding stress levels were calculated and recorded. As

illustrated in Table I0-5, the greatest stress level recorded was in the upper

middle portion of the mount beam at a high pressure compressor speed of 7800

rpm. This stress level, 1.4 kpsi peak-to-peak, is well within the acceptable

levels and corresponds to a margin of safety of 80.4 (compared with the ulti-

mate shear strength of the material of which it is made - AMS 5528 stainless

steel). The minimum margin of safety occurs in the mid-fairing in the axial

direction at an intermediate pressure compressor. The recorded stress level

is 0.96 kpsi, peak-to-peak. This corresponds to a margin of safety of 2.7

with respect to the interlaminar shear strength.

Appendix B shows the range of data tested in terms of calculated stress

versus frequencies and speeds; figures contained therein (Figures B-I through

and B-40) illustrate the positioning of the strain gages used. Note that some

are arranged in rosettes; while others are uniaxial.

10.3 ACOUSTIC FATIGUE

A preliminary acoustic fatigue analysis of the strut fairing calculated a

response frequency of 174 Hz (the fundamental blade passing frequency range

for the engine operating range, 600 to 1400 rpm, is 80 to 187 Hz); however,

this figure is questionable due to the numerous assumptions and uncertainties

involved in the calculation. The operating conditions assumed were those of

cruise. Further, the panel was assumed flat; whereas, a slight panel curva-

ture or irregularity would increase the response frequency; finally, the damp-

ing ratio was estimated rather than known.

235

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Table 10-3. UDF TM Engine Comparison of Mount Loadsfor Airfoil-Out Event.

Maximum Load

Modified Nastran Model Test Results*

Location Load, ib rpm

FMV

FMB

RRMR

RRMA

LRMR

LRMA

8,800

7,500

10,500

44,000

12,000

31,000

228

528

228

444

228

420

Load, ib rpm

24,000 460

13,300 280

16,400 260

40,900 460

* Using Barry Mount Data and Relative Deflection,

Unbalance = 262,000 gm-inch

Table 10-4. UDF TM Engine Airfoil-Out Event Comparison

of Deflections (Absolute).

Maximum Displacement, mils DA

Location

FMV

FMH

RRI%R

RRMA

LRMR

LRMA

Note:

Modified Nastran Model

Deflection, mils

440

1120

6O0

II00

750

II00

rpm

228

540

450

420

228

420

Unbalance = 262,000 gm-inch

Measured Test Results

Deflection, mils

560

385

350

988

rpm

460

280

200

460

236

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Table 10-5. Stress Data - Strut.

• Y

: 6A4JDEi..F ...... •

:FMRING, VERT

',FMRINE, 0IA6

:FAIRIN6, AXIAL

:FHD [SOi .......

:RROF SPAR,VERTi .....................

:RR OF SPAR, OIA6i .....................

:RR Of SPAR, HORIZ

:SIDE OF SPAR, VERT

ISlOE OF SPAR, HORZ

:SIDE OF SPAR, 0IA6

:LT AFT ISO CLEVISi: ..................

',HT BIt,TOPAFT,VERT.....................

:HT M,TOP AFTvOIA6

',RT OIl,TOPAFT,HORZII .....................

'.HT DH,BTHAFT,HORZ

:fiT M,TOP HIO,HORZ

:lit PIt,TOP IllO, VERT

:HT OII,OTHFIID,VIE]IT

;:J:AFT HT Dll SUPTFTE,HOII

:RT AFT lSO CLEVIS

:RT RRHT, TAN

'.RROF OPAR,LIIRAFTtVER'.

:SME, HORIZ

:RR OF SPAR,UPRAFT,VER

:SAHE, DIA6

:SklqE,HORIZ

XH2w

2 tO._7)

3 (O.O_)

2 (0.96)

3 (0.72)

0

0

0

0

0

0

2 (0.5_)

3 (0.12)

0

3 (0.20)

(0.22)

(O.Ol)

3 (0.44)

3 (0.1.4)

2 (1.08)

2 tO.011)

0

(0.36)

3 (0.1.8)

0

0

0

XN2_

3 (0.1_)

3 (0.091)

2 (0.20)

(0.74)

0

0

0

0

0

0

2 (0.5)*

3 (0. lO)

0

3 10.L8)

2 (0.17)

2 (1.4)

;3 (0.42)

3 (0.02)

2 (0.21)

3 (0.94)

0

(0.41)

;3 (0.15)

0

0

0

ZN48 :I

I (O. LS) :

1 (0.54) :

2 (0.19)

1 (0.91) :

4 i0,057)*:

4 (O.Ol_)*:

4 (0)* :

4 (0.271* '

4 (0.22)t

4 (O.Z2)*

4 (0.:9) :

4 (0.12)

"l

3 (0.20)

3 (0.2;3)

2 {0.20) :

2 IO.2l) :

2 or 4 (0):1

2 I0.[0) :

3 (0.92) :

4 (0.66)t

3 (0.;36)..... I

2 (0.17)

4 (0)*

4 (0.50)t

4 (O. L2)t

CODES:

0: NODATAAVAILABLE

l: START/ACCELERATE

2: START/ACCELERATETO 700

_: ACCELERATETO 24,400 LOS.4: ACCELERATETO 24K F6

,: ONLYONEDATAPOINTAVAILABLE

FORflATIS: CODE| (IMiIHUH STRESS[N (PSI PP)

237

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For instance, if the curvature of the panel was as slight as 99 inches,

this frequency would then become383 Hz. What is known is that strain gage

data discussed in Section 10.2 and displayed in Appendix B, show that stressesare relatively low. Thus, there appears to be no resonant vibration within

the operating range of the engine and that acoustic fatigue is not a problem.

238

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11.0 RESULTS

The I00+ hour ground test program of the UDF TM engine demonstrated the

following :

• 25,000 ibf installed corrected thrust

High fuel efficiency: 0.232 ib/hr/Ibf installed corrected sfc

(specific fuel consumption)

• 15,000+ physical total shaft horsepower

• Full propulsor speed (1393+ rpm)

Advanced UDF TM aerodynamics that incorporates custom-tailored

composite fan blades over an inner titanium spar that serves as

the attachment mechanism to the engine for the fan blades

Individually replaceable propulsor fan blades with the engine

installed on the aircraft or test stand

DEC (digital electronic control) provides overall engine con-

trol by monitoring gas generator power and speed and propulsor

speeds and pitch angles; the engine utilizes the existing gas

generator control and a separate propulsor control to minimize

development costs without sacrificing control flexibility; this

control system drives a hydraulic/mechanical actuation system

that permits setting the fan blade pitch angle of the two fan

blade rotors either together or differentially

• Flawless operation of the F404 gas generator

• Counterrotation of structures, turbines, and fan blades

• Reverse thrust capability

Capability to withstand a fan blade airfoil loss with no struc-

tural or secondary damage

Failure of Stage I turbine blades and the subsequent damage to

following turbine blade rows; turbine structures withstood the

failures with little or no damage.

Also demonstrated were the following capabilities:

• Running at full power statically

• Data was repeatable statically

239

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Prediction of low speed, low pressure, counterrotating turbine

performance with accuracy comparable to that of the high speed,

conventional, low pressure turbines

Comparing data recorded early and late in the LCF testing, per-

formance deterioration was confined to a dirty IPC; there was

no evidence of mechanical deterioration

F404 gas generator provided repeatable and predictable perform-

ance and was better than predicted at lower powers (below 70%

takeoff power)

UDF TM blade performance sensitivity to rotational speed was much

greater than predicted

At power coefficient = 1.32, thrust coefficient was 4% better

than predicted (approximately 60% takeoff power)

At power coefficient = 1.95, thrust coefficient was 4% worse

than predicted (approximately 100% takeoff power)

Power turbine efficiency was approximately as predicted, being

within +1.5 points over the major portion of the operating

range; the flow function was within +0.5% of prediction at high

powers (above 80% takeoff thrust)

Overall performance was better than predicted up to 92% takeoff

power (23,000 ibf corrected installed thrust), and was poorer

than predicted beyond 92% takeoff power (23,000 ibf corrected

installed thrust) due to UDF TM speed sensitivity as noted above

At 60% takeoff thrust (15,000 ibf), sfc was approximately 5.50%

better than predicted

At 92% takeoff thrust (23,000 ibf), sfc was approximately as

predicted

At 100% takeoff thrust (25,000 Ibf), sfc was nearly 4.00% worse

than predicted.

240

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12.0 CONCLUSIONS

As a result of the I00+ hour UDF TM test program, it can be concluded that

all of the major objectives of this engine can be and have been met. Some of

these objectives are as follows:

The demonstrated feasibility of an unducted, ungeared, counter-

rotating ultra-high-bypass turbofan

Capability to produce at least 25,000 ibf and at least 15,000

shaft horsepower with an engine of this configuration

Exceptional fuel efficiency as compared to other turbofan or

turbojet engines

The capability to produce thrust with a new fan blade design

of composite materials over a titanium spar

The capability to control the engine and actuate the fan blades

with a digital electronic control

Capability to produce reverse thrust with the fan blades with-

out the use of a thrust reverser

• UDF TM propulsor capable of producing thrust as predicted

Current computer model cycle deck techniques can adequately

model a counterrotating turbofan

Propulsor deterioration (large seals, turbine, etc.) was not

encountered over the duration of testing, which exceeded I00

hours

Operation of the engine, and its performance, is stable at

takeoff power statically.

As expected in an engine program utilizing such new technologies and con-

cepts as the UDF TM, numerous problems have been discovered. However, it is

believed that none of these problems will present a major stumbling block to

future flight test of this engine or to the development of this concept into

an important new entry into the arena of subsonic commercial and military

transport aircraft. Every problem that has occurred during ground testing has

been addressed and adequately solved. Fine tuning may be necessary, and more

problems may be discovered of course, as the testing of this engine continues.

No significant fundamental aerodynamic or control problems were uncovered, and

241

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only two mechanical problems created significant setbacks to the test program.

Both of these problems were solved by rather simple, but successful means:

1 • Fan Blade Airfoil Loss - Although static component tests veri-

fied the integrity of the airfoil bonding to the titanium spar,

actual engine testing brought into effect additional factors

leading to the loss of one airfoil. At that time, only the

adhesive qualities of the composite to titanium bonding agent

held the airfoil to the spar. By adding positive retention

features to the design (by adding fasteners), airfoil retention

proved to be of no problem for the duration of testing and is

not expected to present a problem in the future.

° Turbine Blade Failure Stage 1 turbine blade dynamic response

was excessive due to insufficient damping, which eventually led

to their failure. Damping, in the form of friction, was intro-

duced to all blade rows by placing simple damper pins between

each blade; this satisfactorily reduced the dynamic response.

242

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13.0 SYMBOLS/ABBREVIATIONS

ALF

Beta Angle

BFM

BTAN91

BTAN92

BTWT

CV

DA

DEC

dia.

DMS

DOD

DTAMB

EB

EDM

EPR

F404 Fan

F404-GE-400

FHV

FMH

FMV

FNI IQA

FPI

Fsep

h

HCF

Hz

ID

IF

IGV

IPC

IT

LCF

Aft, Looking Forward

Fan Blade Pitch Angle, degrees

Backflow Margin, %

Front Rotor Pitch, degrees

Rear Rotor Pitch, degrees

Boeing Transonic Wind Tunnel

Convex

Double Amplitude

Digital Electronic Control

Diameter

Data Management System

Domestic Object Damage

AT from Standard Day/ISA Conditions

Electron Beam

Electrical Discharge Machining

Engine Pressure Ratio

Bypass Pressure Ratio

Low Bypass Turbofan Gas Generator

Fuel Heating Valve

Front Mount, Horizontal

Front Mount, Vertical

Installed Thrust, lb

Fluorescent Particle Inspection

Flow Separation Parameter

Coefficient of Heat Transfer (Btu/hr ft2, o F)

High Cycle Fatigue

Hertz, cycles/second

Inner Diameter

First-Flexural Frequency, cycles/second

Inlet Guide Vanes

Intermediate Pressure Compressor

First-Torsional Frequency, cycles/second

Low Cycle Fatigue

243

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244

LE

LPT

LRMA

LRHR

LRHV

LVDT

Max

Min

Mn

MPI

OGV

ON

P15/Pz

P46Q2

P48Q2

PLA

PO

PRS

PS

PS3

PT

PT8

PTO

PZ

RDGS

RRMA

RRMR

S/D

sfc

SFCIIR

SO

S/N

T46

T46Q2

TAmb

Leading Edge

Low Pressure Turbine

Left Rear Mount, Axial

Left Rear Mount, Radial

Left Rear Mount, Vertical

Linear Variable Differential Transducer

Maximum

Minimum

Mach Number

Magnetic Particle Inspection

Outlet Guide-Vanes

O-Nodal

F404 Fan Bypass Pressure Ratio

Gas Generator Pressure Ratio

Engine Pressure Ratio

Power Lever Angle, degrees

Ambient Pressure, psi

Stall Pressure Ratio

Static Pressure, psi

Gas Generator Compressor Discharge Pressure, psi

Total Pressure, psi ... (also Power Turbine)

Power Turbine Exhaust Pressure, psi

Peebles Test Operation

Compressor Inlet Pressure, psi

Readings

Right Rear Mount, Axial

Right Rear Mount, Radial

Shutdown

Specific Fuel Consumption, ib/hr/ib

Installed Specific Fuel Consumption, ib/ib

Strain Gage

Serial Number

Propulsor Exhaust Gas Temperature, o F

Gas Generator Temperature Ratio

Ambient Temperature, o F

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TAAP01

TAAP02

TAFC01TE

TT

2RUDFTM

W25

W48R

Xh

XV

XN48

XN49

ZN

Stage 1 Fan Telemetry Ring Cavity Thermocouple, o F

Stage 2 Fan Telemetry Ring Cavity Thermocouple, o F

Stage 1 Fan Telemetry Ring Cavity Thermocouple, o F

Trailing Edge

Total Temperature, o F

No. 2 Roller

GE36 Unducted Fan Engine

HPC Inlet Flow, ib/second

Power Turbine Flow Function, Corrected

Horizontal Displacement, inch

Vertical Displacement, inch

Stage 1Propulsor Fan Speed, rpm

Stage 2 Propulsor Fan Speed, rpm

Z-Nodal

245

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14.0 Ref_

i. Carlson, S.L., "Engine Damage Report," No. GE36-003, March 18, 1986.

2. Carlson, S.L., "Engine Damage Report," No. GE36-004, August 14, 1986.

3. Cote, M.J., "GE36 Nacelle Fairing Sonic Fatigue Analysis," Memo of July

24, 1986.

.

o

o

.

8_

Gaffney, E., Review of Airfoil Loss, "In Tne Unducted Fan Engine; GE

Quarterly Review No. 8," May 13, 1986.

General Electric, "Full-Scale Technology Demonstration of a Modern

Counterrotating Unducted Fan Engine Concept - Ccmponent Test," NASA

Contract No. NAS3-24210, CR-180868, _ 1987.

General Electric, "Full-Scale Technology Demonstration of a Modern

Counterrotating Unducted Fan Engine Concept - Design," NASA Contract

No. NAS3-24210, (_-180867, December 1987.

General Electric, "The U_ Fan Engine - Quarterly Review No. 6,

"NASA Contract No. NAS3-24210, August 16, 1985.

General Electric, '_[he Unducted Fan Engine - Quarterly Review No. 7,"

NASA Contract No. NAS3-24210, November 18, 1986.

9. General Electric, '_Fne Unducted Fan Engine - Quarterly Review No. 8,"

NASA Contract No. NAS3-24210, May 13, 1987.

i0. General Electric, "UDF TM Airworthiness Executive Review," NASA

Contract No. NAS3-24210, July 1986.

Ii.

12.

13.

14.

Kirkpatrick, R.A., "Failure Report: Engine S/N 082-001/A: High Power

Stall of October 2, 1985," December 13, 1985.

Kroger, J.P., "GE36 Seoond Ground Test," Test Project Sheet No. MA-004,

January 13, 1986.

Nelson, E. (Barry Controls), "Qualification Test Report for 94624

Engine Isolators: GE-36 Demonstrator Engine Program," Document No.

WD04624-I-005, Revision A, May 14, 1986.

Smith, R.E., "Engine Damage Report," No. GE36-002, Revision A, January

6, 1986.

246

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APPENDIX A

STEADY-STATE TEST DATA - BUILD 3

247

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DATA LEGEND

XN2

XN2R

PCN2R

XN25

XN25R

PCN25R

XN48

XN49

UT91R2

UT92R2

BTAN91

BTAN92

WI3

WI5

WF36

WF36R2

FNI IQA

SFC184

TAHB

TI0

PAMB

PIOM

HUHSER

RELHUM

WINVAV

WINAAV

XM0

P46Q2

CT46

T46X

IPC Physical Speed (rpm)

IPC Corrected Speed (rpm)

Percent IPC Corrected Speed (%)

HPC Physical Speed (rpm)

HPC Corrected Speed (rpm)

Percent HPC Corrected Speed (%)

Stage 1 Physical Speed (rpm)

Stage 2 Physical Speed (rpm)

Corrected Stage 1 Tip Speed (feet/second)

Corrected Stage 2 Tip Speed (feet/second)

Stage 1 Pitch Angle (degree)

Stage 2 Pitch Angle (degree)

Bypass Duct Inlet Flow (ib/second)

Bypass Duct Exit Flow (ib/second)

Fuel Flow (ib/hr)

Corrected Fuel Flow (ib/hr)

Corrected Installed Net Thrust (ib)

Corrected Installed Net Specific Fuel Consumption,

FHV = 18,400 (ibfuel/ibthrust hr)

Ambient Temperature (o R)

Inlet Total Temperature (o R)

Ambient Pressure (psia)

Inlet Total Pressure (psia)

Specific Humidity (grains/ib dry air)

Relative Humidity (%)

Average Wind Velocity (knots)

Average Wind Angle (degree)

Mach Number

Engine Pressure Ratio

Calculated T46 (o R)

Measured T46 (o R)

PRECEDING PAGE BLAi_j:-_,i'_OT glL,"AED

J

249

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APPENDIX B

STRAIN DATA FOR THE STRUT

Figures B-I and B-2 illustrate the locations of all the gages read except

KD FARI, KD FAR2, and KD FAR3. These three make up the vertical, diagonal,

and axial axes, respectively, of a gage rosette located centrally on the inner

surface of the mid-fairing.

The following graphs (Figures B-3 through B-40) contain maximum stress

locations calculated from strains read on gages located as shown in Figures

B-I and B-2. These are shown versus engine frequencies and speeds as read

from test diagrams. Each graph (with the exceptions of those combined because

only one situation for each was recorded) displays the maximum stress versus

speed or frequency for one gage only. Different situations are labeled for

each point. Note that almost all are labeled with either an XN2, an XN25, or

an XN48. These correspond to engine speeds as follows:

XN2 refers to the intermediate pressure compressor

XN25 refers to the high pressure compressor

XN48 refers to the Stage I propulsor.

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DISTRIBUTION

Government Aqencies

NASA Headquarters

600 Independence Avenue, SW

Washington, DC 20546

Attn: R/R.S. ColladayRJ/C.C. Rosen

RP/G.M. Reck

RP/J.R. Facey

NASA Lewis Research Center

21000 Brookpark RoadCleveland, Ohio

Attn: J.AR.J

P.G

G.KM.J

R.E

L.J

44135

ZiemianskiShaw

Batterton

SieversHartmann

Kielb

Kiraly

J.F. GroenewegJ.C. Williams

R.W. NiedzwieckiD.W. Drier

B.A. Miller

J.J. ReinmannL.J. Bober

A.G. Powers

J.J. CoyR.E. Coltrin

C.L. Ball

E.A. Willis

L. ReidE.T. Meleason

R.D. HagerLibrary

Report Control OfficeTech. Utilization Office

D.C. MikkelsonAFSC Liaison Office

Army R & T Propulsion Lab

NASA Ames Research Center

Moffett Field, CA 94035

Attn: R.P. BenczeR.C. Smith

MS 86-I

MS 86-IMS 86-I

MS 100-5

MS 3-7

MS 23-3MS 23-3

MS 86-7MS 500-211

MS 77-6 (2 copies)MS 86-2MS 5-3

MS 77-10

MS 86-7

MS 86-4MS 86-4

MS 77-10

MS 77-6MS 86-I

MS 77-10

MS 77-10

MS 86-7 (3 copies)

MS 60-3 (2 copies)MS 60-IMS 7-3

MS 6-12 (2 copies)MS 501-3MS 77-12

MS 227-6

MS 227-6

320

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NASA Langley Research Center

Hampton, VA 23665

Attn: D.G. StephensResearch Information Center

MS 462

MS 151A

NASA Scientific and Technical Information FacilityP.O. Box 8757

B.W.I. Airport, MDE 21240

Attn: Accession Dept. (20 copies)

NASA Dryden Flight Research CenterP.O. Box 273

Edwards, CA 93523

Attn: D-OP/R.S. Baron (2 copies)

Department of Defense

Washington, DC 20301Attn: R. Standahar, 3DI089 Pentagon

Wright-Patterson Air Force Base

Dayton, OH 45433Attn: AFWAL/PO/Co]. J. Radloff

AFWAL/POTA/M.F. SchmidtAFWAL/POT/H.I. Bush

ASD/EN/CoI. L.G. vanPelt

ADS/SR/K.I. Collier

Eustis Directorate

U.S. Army Air Mobility

R & D LaboratoryFort Eustis, VA 23604

Attn: J. White

J. Gomez, Jr.

Navy Department

Naval Air Systems Command

Arlington, VA 20360Attn: G. Derderian, AIR-310-E

Naval Air Propulsion Test CenterTrenton, NJ 08628

Attn: P.J. Mangione, MSPE-32R. Valeri, MSPE-34

U.S. Naval Air Test Center

Code SY-53

Patuxent River, MD 20670

Attn: E.A. Lynch

321

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USAVRAD Command

P.O. Box 209

St. Louis, MO 63166Attn: R.M. Titus

Department of TransportationNASA/DOT Joint Office of Noise Abatement

Washington, DC 20590Attn: C. Foster

Federal Aviation Administration

New England Region12 New England Executive Park

Burlington, MA 01803Attn: D.P. Salvano

Enqine Manufacturers

AVCO Lycoming550 S. Main Street

Stratford, CT 06497Attn: H. Moellmann

Detroit Diesel/Allison DivisionP.O. Box 894

Indianapolis, IN 46206Attn: B. Wallace

Garrett Turbine Engine Company111 South 34th StreetP.O. Box 5217

Phoenix, AZ 85010Attn: R. Heldenbrand

Garrett Turbine Engine CompanyTorrance, CA 90509

Attn: F.E. Faulkner

General Electric Company/AEGI Neumann WayEvendale, Ohio 45215

Attn: T.F. Donohue

General Electric Company/AEG1000 Western Avenue

Lynn, MA 01910Attn: B. Weinstein

322

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General Electric CompanyP.O. Box 88186

Cleveland, OH 44181Attn: M.H. Rudasill

Pratt & Whitney Aircraft Group

United Technologies Corporation

Engineering Division400 Main Street

East Hartford, CT 06108Attn: R.W. Hines

G.L. Brines

G.L. Bywaters

Pratt & Whitney Aircraft Group

United Technologies CorporationMilitary Products DivisionP.O. Box 2691

West Palm Beach, FL 33402Attn: R.E. Davis

T.R. Hampton

Pratt & Whitney Aircraft Group

United Technologies Corporation

24500 Center Ridge RoadSuite 280

Westlake, OH 44145Attn: A. Leiser

Teledyne CAE, Turbine Engines

1330 Laskey RoadToledo, OH 43612

Attn: R.H. Gaylord

Williams International

2280 West Maple Road

Walled Lake, MI 48088

Attn: R. vanNimwegenR. Horn

Airframe Manufacturers

Boeing Commercial Airplane CompanyP.O. Box 3707

Seattle, WA 98124

Attn: Dr. C.G. Hodge

F. DavenportJ. Farrell

161-04

162-25162-23

713-11713-07

323

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Boeing CompanyWichita DivisionP.O. Box 7730Wichita, KS 67277

Attn: D. TarkelsonC.T. Havey

Cessna Aircraft CompanyP.O. Box 154

Wichita, KS 67201

Attn: D. Ellis Dept 178

Douglas Aircraft CompanyMcDonnell Douglas Corporation3855 Lakewood Boulevard

Long Beach, CA 90846Attn: M. K1otzsche

W. Orlowski

Gates Learjet CorporationP.O. Box 7707

Wichita, KS 67277Attn: E. Schiller

General Dynamics ConvairP.O. Box 80844

San Diego, CA 92138

Attn: S. Campbell

Grumman Aerospace CorporationSouth Oyster Bay Road

Bethpage, NY 11714Attn: N.F. Dannenhoffer

Gulfstream Aerospace CorporationP.O. Box 2206

Savannah, GA 31402-2206Attn: R. Wodkowski

Lockheed-California CompanyBurbank, CA 91502

Attn: J.F. Stroud

R. Tullis

Lockheed-Georgia Company86 S. Cobb Drive

Marietta, GA 30063Attn: W.E. Arndt

324

D/75-42

D/75-21

D/71-01, Zone 13

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McDonnell Aircraft CompanyMcDonnell Douglas CorporationP.O. Box 516St. Louis, MO 63166

Attn: G. Phariss

Rockwell International

International Airport

Los Angeles DivisionLos Angeles, CA 90009

Attn: A.W. Martin

Airlines

American Airlines

Maintenance and Engineering Center

Tulsa, OK 74151Attn: C. Wellmershauser

Continental Airlines, Inc.

2929 Allen ParkwayHouston, TX 77019

Attn: Jo Arpey

Delta Airlines, Inc.

Hartsfield-Atlanta International AirportAtlanta, GA 30320

Attn: J.T. Davis

Eastern Airlines

International AirportMiami, FL 33148

Attn: E. Upton

Federal Express CorporationBox 727

Memphis, TN 38194

Attn: J. Riedmeyer

Pan American World Airways, Inc.

JFK International AirportJamaica, NY 11430

Attn: R. Valeika

Trans World Airlines

605 Third Avenue

New York, NY 10016Attn: K. Johnson

325

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United Airlines

Maintenance Operations CenterSan Francisco International Airport

San Francisco, CA 94128Attn: J. Goodwine

Hamilton Standard

United Aircraft CorporationWindsor Locks, CT 06096

Attn: B. GatzenS. Ludemann

Massachusetts Institute of Technology

Department of Astronautics and Aeronautics

Cambridge, MA 02139Attn: Library

Penn State University

Department of Aerospace Engineering233 Hammond Building

University Park, PA 16802Attn: Dr. B. Lakshminarayana

Rohr CorporationP.O. Box 878

Foot and H Street

Chula Vista, CA 92012

Attn: Library

TRW, Inc.

TRW Equipment Group23555 Euclid Avenue

Cleveland, OH 44117Attn: I. Toth

University of Michigan

Gas Dynamics LaboratoriesAerospace Engineering Building

Ann Arbor, MI 48109Attn: Dr. C.W. Kaufmann

University of Tennessee Space Institute

Tullahoma, TN 37388Attn: Dr. V. Smith

MS 1-2-11MS I-2-11

326

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Cessna Aircraft Company

McCauley Accessory Division3535 McCauley DriveVandalia, OH 45377

Attn: H.G. Starnes

Hartzell Propeller ProductsP.O. Box 1458

1800 Covington AvenuePiqua, OH 45356

Attn: D. Edinger

University of WashingtonSeattle, WA 98195

Attn: Dr. R. Decher

32 7

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"1 Report NOCR-180869

4 Tree and Subtitle

2 Government Accession No 3 Recipient s Catalog No

5 Report DateDecember 1987

Full-Scale Technology Demonstration of a Modern Counterrotating

Unducted Fan Engine Concept - Engine Test

7 Author(s)

GE36 Design and Systems Engineering

9 Performing Orgamzatlon Name and Address

GE Aircraft Engines

One Neumann Way

Cincinnati, Ohio 45215

12 Sponsonng Agency Nameand Address

NASA Lewis Research Center

2]000 Brookpark Road

Cleveland, Ohio 44135

6 Performmg OrgamzaUon Code535-03-01

8 Performing Organization Report No

10 Work Umt No

11 Contract or Grant No

NAS3-24210

13 TypeofReportand Period Covered

Topical

14 Sponsormg Agency Code

5 Supplementary Notes

ii6 Abstract

The UDF TM (unducted fan) engine is an innovative aircraft engine concept that is based on an

ungeared, counterrotating, unducted, ultra-high-bypass turbofan configuration. This engine is

being developed by GE Aircraft Engines to provide a high thrust-to-weight ratio power plant with

exceptional fuel efficiency for subsonic aircraft application.

This report covers the successful ground testing of this engine. A test program exceeding

lO0-hours duration was completed, in which all of the major goals were achieved. The following

accomplishments were successfully demonstrated: full thrust (25,000 ib); full counterrotating

rotor speeds (1393+ rpm); low specific fuel consumption (< 0.24/Ib/hr/ib); new composite fan

blade design; counterrotation of structures, turbines, and fan blades; control system; actuation

system; and reverse thrust.

17 Key Words tSuggesleC by Authorls))

Unducted Fan (UDF_); Counterrotation;

Ultra-High-Bypass Fan; Propfan

18 DlstriOubonStatement

19 SecJrd_ ClasS_ ,Of this reporti

Unclassified

20 Security Class_f !of this page)

Unclassified

2! No of Pages

326

22 Price

I

_1 i