presentation for 18th national award for excellence...
TRANSCRIPT
Presentation for 18th National Award for
Excellence in Energy Management-2017
KAWAS
31st August 2017
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Company Profile
Station Profile
Energy Conservation Projects
Roadmap For Energy Conservation
SEC Trend
Benchmarking
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GHG Inventorisation
9 SEC Monitoring Formats
Efforts Towards Green Company
10 Best Practices
Contents
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12 Awards & Accolades
Renewable and waste utilization
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Location Hazira, Surat (Gujarat, India)
Installed Capacity Stage-I 656.2MW (2 Identical blocks, each block consisting of 2 GTs and 1 ST)
Type Combined Cycle Gas Power Plant
Gas Turbines 4 Nos. of GE 9001-E of 106 MW each
Steam Turbines 2 Nos. of Alsthom Rateau 116.1 MW each
Fuels Natural Gas (GSPCL, GAIL), Naphtha, HSD
Source of Water River Tapti: Pump House at Variav
Power Evacuation Thru’ 8 Nos. of 220 KV Transmission lines: i) Haldarva-1,2 ii) Dastan-1&2 iii) Vav 1,2 iv) Ichapore 1,2
Beneficiaries Gujarat, MP, Maharashtra, DNH, Daman & Diu, Goa and J&K
Mah 31.14%
GUJARAT (28.5%)
MP 21.36%
DNH 12.38%
D&D 4.73%
GOA 1.89%
J&K 0.01%
MW Share % Share
656.2 MW
POWER ALLOCATION
Station Profile
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S.
No.
Title of Project Annual
Saving (Rs
Lakhs)
Investment
Made (Rs
Lakhs)
Payback
(Months)
Remarks
1 De-staging of HP BFP in Block-I
(Benefits as per one Pump).
6.98 5.55 9.45 02 No completed in 2016-17.
04 No planned in 2017-18.
2 Jet cleaning of Condenser Tubes in
Steam Turbine #1C & 2C.
9.88 4 4.85 ST#2C - Feb’ 2017
3 Online Compressor Washing of Gas
turbine.
72 91.75 15 Recovery of lost power output.
Prolonged sustained operation.
4 Replacement of 70 W HPMV Bollard
with 18 W Energy efficient
Bollard and LED tube light.
1.5 3.19 25 60 No. Bollard; 700 No. LED
Tubelights.
FY 17-18 – 4500 No
FY 18-19 – 10500 No.
Energy Conservation Projects in last 3 years
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S. No. Title of Project Annual
Saving (Rs
Lakh)
Investment
Made (Rs
Lakh)
Payback
(Months)
Remarks
5 Replacement of air filters cartridges
in all Gas Turbine
15 17.5 14 FY 16-17: 02 GT’s filters
replaced.
6 Application of Energy Efficient
Coating in Circulating Water Pump
10.45 9.4 10.8 CW Pumps – all 5
completed.
Make up water pumps – 2
No.
7 Retrofitting of VFDs in Raw Water
Pumps
5.16 15.58 36
Energy Conservation Projects in last 3 years
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25-30 % of the APC is consumed by Boiler Feed Pump.
2 working + 1 standby BFP’s in 1 block.
BFP Discharge Pressure – 98 Kg; Required Pressure – 87 Kg.
Hydraulic power requirement is low as compared to actual conditions.
Total stages in the BFP – 11 stages.
After De-staging – 10 stages
Yearly Electrical Savings – 2 Lakhs
Investment of INR 5.5 lakh gives simple payback of 9.45 Months.
De-staging of Boiler Feed Pump
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Description Before De-staging After De-staging
Discharge Pressure (Kg) 97.79 84
Discharge flow(T/hr) 175.95 179
Power consumption(kw) 751.68 kw 675.74 kw (@0.85p.f)
Power savings (kW) (10% power
savings) 75.94
Saving in kWh yearly (PLF=30%) 199570
Rs/kWh 2.58
Saving in Rs. (Lakhs) 6.98
Investment in Rs. (Lakhs) 5.5
Payback period in months 9.45
De-staging of Boiler Feed Pump
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The efficiency of the compressor depends on the inlet air temperature & fouling on the blades.
Gas turbine compressors consume approximately 60% of the overall cycle energy during operation.
Online washing is being performed while the gas turbine is in operation and at load.
The basic objectives of online cleaning are to maintain the cleanliness of a compressor after offline washing and to
extend the operating period between shutdowns required for offline (crank) washing.
Kawas has installed the GT Compressor
Online Washing System in all the 4 GTs and
simple payback period 15 Months. The
improvement in gas turbine power output after
utilization of compressor online water wash
system helps in restoring the lost power
and GT will run for prolonged duration.
Online Compressor Washing of Gas Turbines
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Test Results of Online Compressor Wash
Test period (GT#2B) 01.04.2016 to 31.03.2017
No. of Offline Wash Performed 6 No
No. of Online Wash Performed 40 No. Every 3rd Day
No. of Days operation 157 days
Average power output increase after an off line wash 1.325 MW Average=1.25%
Average power recovery during an online wash 0.93 MW
Production Profitability due to Online Wash 2.81232 MU's
In terms of Rs. (Lakhs) 72.557856
The operating and maintenance cost of the systems are not considered.
Online and offline cleaning are complementary.
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Energy Efficient Coatings on Pump Internals
The purpose of the circulating water system is to cool the condenser and condense the steam into water. Circulating
water is cooled in cooling towers.
There are 5 pumps which are driven by 6.6 KV, 930 kW motor.
Pump efficiency deteriorated due to scaling and corrosion.
Due to irregular surface area and resistance to flow, there may be
reduction in pump efficiency and increase in Power consumption.
Coating helps in gaining Pump efficiency by approximately 8%.
Energy Efficient Coating on Circulating Water Pumps
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Description Before Coating After Coating
Power consumption(kw) 845.67 kw 886.45 kw
Total Head Developed (m) 26.5 26.5
Measured Average Flow (m3/hr) 9000 10635.93
Pump Output (kW) 649.9 752.42
Motor Input (kW) 845.67 886.45
Calculated Pump Efficiency
(assumed motor efficiency as 95%) 80.89 89.34
Gain in Efficiency (%) 8
Saving in kWh yearly (PLF=30%) 495500
Rs/kWh 2.58
Saving in Rs. (Lakhs) 10.45
Investment in Rs. (Lakhs) 9.4
Payback period in months 10.8
Energy Efficient Coating on CW Pumps
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Replacement of Air Filters in Gas Turbines
Compressor sucks huge quantity of atmospheric air through paper filters.
These paper filters become clogged with dust, moisture and other impurities causing reduction in air flow and
high differential pressure.
The higher the clogging, lesser amount of air flow leading to low Gas Turbine power output.
Earlier filters were replaced when DP reaches at 1200 Pa.
Replacement being done at 700 Pa.
Losses due to high DP across filters is recovered as
improved GT output.
Simple Payback is 14 Months.
Replacement of Air Filters
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As per our efficiency reports, losses in generation due to clogged filters: 0.83 MW.
Operating Hours of GT = 24 X 365 X 0.3 (PLF = 30%) = 2628 Hours
Average Energy Saved = 0.83/2 X 2628 = 1.454 MU’s
Gain due to early replacement of filters (Earlier we were replacing it in 15 months but now every 9
months-6months early replacement)
= 40% period gain X 1.454 = 0.5816 MU’s
Energy Tariff = Rs 2.58 per KWhr
Energy saved in money terms = 2.58 X 0.5816 = Rs 1.50 Million
Investment Made = Rs 1.75 Million
Payback Period = (1.75 X 12)/1.5 = 14 Months
Gain through Replacement of Air Filters
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The hard scales which gets deposited on
condensers tubes of the Steam Turbines
affecting their heat transfer effectiveness
adversely and thus affecting the vacuum of
the system as well.
These hard scales are removed through jet
cleaning during Stream Turbine (ST) shutdown.
As per the capacity reports, after removal of
scales from the condensers, the vacuum
improved by 3.82/1.5 mbar in ST1C & ST2C
respectively resulting in corresponding saving of
0.382 MW/0.15MW power which remain effective
for minimum 60 days.
Total savings of INR 9.88 Lakhs
Jet Cleaning of Condensers
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As per our efficiency reports, average gain in generation due to improved vacuum: 0.382 MW (ST#1C) & 0.15 MW
(ST#2C)
Operating Hours of ST = 24 X 60 = 2880 Hours
Average Energy Saved = (0.382 +0.15)/2 X 1440 = 0.383 MU’s
Energy Tariff = Rs 2.58 per KWhr
Energy saved in money terms = 2.58 X 0.383 = Rs 0.988 Million
Investment Made = Rs 0.4 Million
Payback Period = (0.4 X 12)/0.988 = 4.86 Months
Gain through Jet Cleaning of Condensers
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Installation of Energy Efficient Lights
Total 60 nos of convention lights of 70 w replaced with EE light in reservoir area.
Energy Saved = (70 -18)/1000 X 60 No. X (12) hrs per day X 365 day = 18396 KWhr per year
Total 700 nos of 36W tube lights replaced with 18 W LED.
Energy Saved = (36 -18)/1000 X 700 No. X (12) hrs X 365 day = 40068 KWhr per year
Energy Tariff = Rs 2.58 per KWhr
Energy saved in money terms = 2.58 X (18396 + 40068) = Rs 150,837/-
Investment Made = Rs 119000 + 200000 = 319,000
Payback Period = (319000 X 12)/150837 = 25 Months
In year 2018-18 15000 no. conventional light(covering complete plant and township) will be replaced by EE
LED lighting.
Installation of Energy Efficient Lights
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VFD Installation in Raw Water Pumps
Gas plant operated at partial loading due to grid and gas availability constraints.
If, motor is allowed to continuous operate at full speed and uses electric energy at the full-load rate, even
though it was performing less useful work. In the process, it wasted a great deal of energy.
Incorporating variable frequency drives into applications such as fans, pumps, etc reduce energy use up to
50 percent at partial loads by matching motor speed to the changing load and system requirements.
Various drives have been converted to VFD’s like raw water pump, etc. On part loading operation of the
pump energy saving to the tune of 50 kW is achieved.
In 12 Month period, energy saved: 0.2008 MU’s
Energy Tariff: Rs 2.58
Energy saved in money terms = 2.58 X (0.2008) = Rs 0.516/- Million
Investment Made = Rs 1.558 Million
Payback Period = (1.558 X 12)/0.516 = 36 Months.
Retrofitting of Variable Frequency Drive’s
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Energy Efficient Coating of continuously running pumps
like ARCW pump, service water, DM water and potable
water pump. (Investment 60000; Savings-32000,
payback 23 months)
Switching off one of transformers and both sections
bus charging through tie breaker to reduce transformer
losses.
Increasing COC from present level of 5 to 5.5 keeping
LSI & RSI within limits. (Rs 2.2 lakh)
Hot blow down in place of cold blow down for NDCT to
decrease to reduce evaporation losses and heat load
to NDCT. (Rs 2.61 lakh)
Replacement of all the lights with energy efficient LEDs.
Replacement of chillers of central HVAC with new
chillers units.
Optimizing operation
Reducing open cycle generation during start-up. (Electrical
saving per start up – 23414 KWh)
GT configuration as per fuel and schedule availability.
Switching off one set of fin fans in both GT and Gen cooling
in winters. (Saving – INR 3.06 lakh)
Single CW pump with one unit. (Saving-Rs 17.27 Lakh/year)
Stopping T/G of ST after 72hours (Earlier we were not doing
this because of vibration hiccup issues) (88 KW saving)
Water makeup pump operations only during night hours ( off
peak hour tariff ) and capacitor bank to avoid P.F penalty.
All HPBFP de-staging. (Savings – INR 7 Lakh/year)
Stopping of ARCW Pumps (35 KW)
Roadmap for Energy conservations
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Year Thermal SEC
(Kcal/Kwh)
Electrical SEC (%) Target Gross Heat
Rate (Kcal/Kwh)
2014-15 2043 2.54 2050
2015-16 2064 2.9 2040
2016-17 2013 2.49 2020
Specific Energy Consumption-Trends
Target Electrical SEC: 2.5%
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Station Heat Rate
(Kcal/Kwh)
APC (%)
Kawas 2013 2.49
Dadri 2039 2.69
Faridabad 1993 2.8
Jhanor 2089 2.79
Road map to achieve benchmark
De-staging of all boiler feed pumps.
Energy Efficient Coating on high
consumption pumps.
Increasing COC from present level of 5 to
5.5 keeping LSI & RSI within limits
Replacement of all lights with energy
efficient LEDs.
Replacement of chillers of central HVAC
with new chillers units.
Benchmarking
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0
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'07-08 '08-09 '09-10 '10-11 '11-12 '12-13 '13-14 '14-15 '15-16 '16-17 17-18
Kawas
Performance Trend of Kawas in NTPC Gas Stations
Source: PEM ranking of NTPC
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GHG Inventorisation
Year Generation
(MU)
Scope1 CO2
(MT)
Scope2 CO2
(MT)
Total CO2 (MT)
2013-14 1388 557960 495 56291
2014-15 1741.2 696620 286 696906
2015-16 1212 485569 306.44 485875
2016-17 1717 686817 361 687178
1. NOx reduction through water spray system.
2. Replacement of Halon Fire fighting system with
Inergen based FF system.
3. Massive tree plantation.
4. Modification of Combustor components like
nozzles, liner, transition piece, etc.
5. Reduction in purchased electricity through
EE Coating on make-up water pumps.
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Energy Conservation projects and % investment
EnCon Project Budget allocation %
Total turnover of the company/plant FY 2016-17 (Rs. Million): 9734.6
Amount invested in EnCon Projects FY 2016-17 (Rs. Million): 39.1
Investment as % of turnover: 0.391
Status of Energy Conservation Projects of FY 2016-17
S. No. Description Status
1 HP BFP Destaging (02 No) Implemented
2 Energy Efficient Coating on CW Pump Implemented
3 Replacement of CFL & HPMV with LED Implemented
4 Online Compressor Washing Implemented
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Efforts towards Green Company
Projects Implemented
Procurement of Energy efficient Motors, LED Lights, solar lights, etc
Installation of RO Plant. Settling pit for conservation of water.
Jute Bag Distribution to Township.
Tree Plantation: 2016-17 – 1000 No. 2017-18* - 2025 No.
Green Vendors
Contract for collection of Bio medical waste is awarded to agency which is accredited and authorized by Gujarat
Pollution Control Board. Only valid licence holders from GPCB are considered for tendering/award.
Contract for collection of Electronic & Hazardous waste is awarded to agency which is accredited and
authorized by MSTC Ltd.
Benefits Achieved
Replacement of Halon Fire Fighting system with environmental friendly Inert gas based fire protection system.
Qty of Hazardous waste sold in last three years:
Resin: 3.99 MT
Used Lube Oil: 12.55 KL
Transformer Oil: 30KL
E-Waste free.
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SEC Monitoring and Reporting Formats
OLEMS Reports.
SAP generated reports for APC.
SMC
ORT
Mobile message
EMAP
Energy efficiency measures
implementation.
Monitoring of Auxiliary power consumption.
Coordinating & conducting Energy audits
of different systems.
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Best Practices
Air Scoring Line
Manual handling of chemical process has been removed.
Saving of time, APC & manpower.
Exact measuring of quantity leading to no wastage/over
usage of chemicals.
Investment of INR 45,000/- gives simple payback of 1
Months.
• Zero Investment project.
• Reduces evaporative & drift loss leading to
saving of Rs 2.61 Lakh per annum (Pumping cost &
water saving).
Hot Water Blow Down
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OPEN CYCLE TIME REDUCTION PLAN
• Typical efficiency of Brayton cycle is 32% in open cycle
mode and 49% in combined cycle mode.
• Open Cycle Thermal SEC- 3010 Kcal/Kwh whereas
Combined Cycle it is 2050 Kcal/KWh.
• Cold Start Up Time is 330 Minutes.
• By reducing open cycle time, thermal specific energy
consumption will decrease for the station.
• Electrical Saving – 23414 KWh per start-up.
• Saving in terms of Rs. 60000/- per start-up.
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Projects implemented through Kaizen
Air scoring Line for neutralization of De-Mineralization plant effluent. (Payback - 1 Months)
Replacement of old obsolete motorized actuators with new indigenous actuators. (INR 1.5 Lakh/actuator)
Steps towards zero discharge: Boiler drain pit water reuse, etc
Roof rain water harvesting.
Settling Pit for water conservation.
Energy conservation week is celebrated every year.
Various quizzes, competition and training are imparted to employees & their families on energy
conservation awareness.
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Renewable Energy Sources and Utilization of Waste
Presence in Renewables
30 KW SOLAR PV AT ITI OLPAD.
Solar lights in reservoir and Damka Village under CSR.
Future Projects in Renewables
35 KW ADMIN BUILING SOLAR PV ROOF TOP.
E-Vehicle charging point.
1 MW FLOATING SOLAR PV OVER RESERVOIR.
173 KW SOLAR PV FLOATING OVER POND IN SIMULAOR.
65 MW SOLAR PV PLANT BESIDE STAGE-II.
Utilization of Wastes: Around 216 MT/year of household waste have been used in Bio-methanation plant
which produces gas having GCV 1750 Kcal/Kg. The heat value of 378 Million kcal/year have been
generated in the bio-methanation plant. Vermicompost plant at Plant.
Installation and Supply of 30 MLD Tertiary treated water from SMC (Bhesan Sewage Treatment Plant of
Surat Municipal Corporation) to NTPC Kawas.
Settling pit to utilize water from Clarifier & cooling tower sludge.
Awards and Accolades
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National Energy Conservation Award – 2012 & 2015
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Station No of ESCerts Station No of Escerts
Singrauli 17610 Anta 1256
Rihand -16225 Auraiya 13931
Unchahar -7051 Dadri Gas 1112
Tanda -26086 Faridabad 7145
Dadri 33217 Kawas 24370
Badarpur -2610 Gandhar 8897
Korba -3395 Kayamkulam 1643
Vindhyachal 33729
Sipat 36443
Ramagundam 26947
Simhadri 11511
Farakka 24041
Kahalgaon 31197
Talcher Kaniha -49681
Talcher Thermal 1356
NTPC Coal Total 111003.23 NTPC Gas Total 58353
24370 ESCerts
issued to Kawas for
PAT CYCLE-1.
PAT Cycle-I performance
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SAFEE Global Energy Management Award for 2016
• Won SAFEE (South Asian Forum For
Energy Efficiency –World Energy
Council) First Global Energy
Management Award for 2016-17,in
the category Thermal Stations/Gas
Category for excellence in Energy
Efficient Performance dtd. 12/1/2017
.
Thank You
Address
NTPC Limited, KGPP,
Adityanagar, Surat – 394516 (India)
Phone
+91 261 2877000
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GT 1A synchronized 24.05.1992
GT 1B synchronized 22.03.1992
GT 2A synchronized 27.08.1992
GT 2B synchronized 30.06.1992
ST 1C synchronized 23.02.1993
ST 2C synchronized 19.03.1993
Renovation and
Modernisation Milestones
Commercial Operation
Milestones
GT 1A synchronized 21/01/2013
GT 1B synchronized 27/08/2013
GT 2B synchronized 05/03/2014
GT 2A synchronized 22/08/2014
ST 1C Minor O/H 24/08/2013
ST 2C Major O/H 04/07/2014
NTPC Kawas (Stage - I)
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Air Filters Replacement
SAVINGS DUE TO REPLACEMENT OF AIR FILTER CARTIDGES
SL.
NO. DATE
DIFFERENTIAL
PRESSURE IN
PASCALS
LOSS IN GENERATION DUE
TO HIGH DP AS PER
CAPACITY TEST in MW
REMARKS
1 06.04.2016 712 0.94 READINGS TAKEN BEFORE
REPLACEMENT OF AIR FILTERS
2 02.09.2016 219 0.16
READINGS TAKEN AFTER
REPLACEMENT OF AIR FILTERS IN JUL
2015
IMPROVEMENT 493 0.78 EXCESS GENERATION MADE POSSIBLE
WITH REPLACEMENT
SAVINGS in MU 1.097
SAVINGS Rs. (Lakhs) 28.30 AVG. RATE OF ENERGY IN KAWAS- @
RS. 2.58 PER UNIT
Note:- Replacement dates-
1A 01.05.2016
1B 01.06.2016
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Power /Operation Conditions
Before Offline Wash
After Offline
Wash
Before Online
Wash
After Online
Wash
Ambient Temperature °C 30.589 33.549 27 25.071
Ambient air Pressure BARA 1.0047 1.0070 1.0119 1.0120
Ambient RH % 34.721 26.92 35.341 33.554
GT Gross power (measured) MW 111.97 111.03 119.84 118.08
Corrected power
(corrected to site condition ) MW 115.10 117.09 115.77 116.88
The improvement in gas turbine power output after utilization of compressor online water wash system helps in
continuous prolonged operation and recovery of lost power output.
Performance Improvement thru Online Compressor Washing