presented by m/s dalmia cement (bharat) ltd,...
TRANSCRIPT
Hearty welcome to
KEP - Small Group Activity
Presented by M/s DALMIA CEMENT (BHARAT) LTD, DALMIAPURAM
Building Young India since 1939
Pan India Player • Operating 13 Cement Plants with a total
capacity of 30 MTPA
Plant Profile - Dalmiapuram: • Installed Capacity (Clinker) - 2.3 MTPA • Installed Capacity (Cement) - 3.4 MTPA • Captive power plant (CPP – 1) - 27 MW • Captive power plant (CPP – 2) - 18 MW
Uniqueness: • Producing 16 varieties of cement in one
location • Operating 7 Management Systems • First in India to produce High strength cement
(Since 1976) • First in India to produce Oil well cement (Since 1986)
Energy to Monetary (ETM)
S.NO SGA PROJECTS QTY ONE TIME INVESTMENT
(LACS)
SAVINGS (KW/HR)
SAVINGS (LACS/YR)
1 IMPLEMENTED
5 7.5 185 56
2 UNDER PROGRESS
3 13.5 32 9
3 UNDER APPROVAL
4 16 65 15
4 UNDER STUDY
6 32.5 120 17
TOTAL 18 69.5 402 97
Our SGA journey started from Dec'17
Conversion Of Bag Filter Purging system
Team Victory
Background
To reduce the Compressor air leakage in Pyro section
Observation made
Leakage from Aux Bag filter purging system was on higher side due to
Old system - Piston operated purging type
Frequent failure of internal spare parts
Online maintenance not possible
Action Taken
Purging system upgraded to diaphragm type.
This modification was implemented in 5 number of Aux Bag filters
Piston Operated Purging
Piston in Receiver tank
Project 1
Conversion Of Bag Filter Purging system
Benefits
Compressed air leakage arrested completely
Online maintenance possible.
Minimum Spares & Maintenance cost
Investment made
One Time - 2.4 lacs
Savings Achieved
Energy : 15 kWh
Monetary : 3.62 lacs/annum
Payback : 8 months
Diaphragm Operated Purging
Installation of VFD for Packing House Bagfilter Fan
Team DSP
Background
To improve the efficiency of the bag filter, thereby controlling the dust and to save energy
Observation made
Bag Filter Fan was operated in DOL mode at full speed of 1450 rpm resulting in
Optimisation of Suction line dampers to avoid fan overload tripping
Insufficient suction leading to more dust pollution
Frequent choking of bags leading to reduced life and more maintenance hours
Action Taken
VFD drive installed for one of the Auxillary bag filter fan
Variable Frequency Drive
Project 2
Benefits
Fan running at a speed of 800 rpm, which is sufficient
Suction line dampers were removed.
Better suction with effective dust control.
Investment made
One Time - 5.05 lacs
Savings Achieved
Energy : 15 kWh
Monetary : 3.27 lacs/annum
Payback : 19 months
Installation of VFD for Packing House Bagfilter Fan
Nuisance Dust Collector
Team Spartans
Background
To optimize Raw meal silo circuit to save energy
Observation made
Both Raw meal silos were simultaneously operated for infeed and extraction
Auxiliary Power consumption was higher
All the drives in the circuit were running
Action Taken
Single silo operation logic was implemented without affecting product quality
Variable Field Drive
Optimisation of Power in Rawmeal silo group equipments
Project 3
Benefits
Six drives were stopped in the circuit
Ready standby circuit available to avoid breakdowns
Reduction in spares and maintenance cost
Investment made
Nil
Savings Achieved
Energy : 40 kWh
Monetary : 9.5 lacs/annum
Payback : NA
Optimisation of Power in Rawmeal silo group equipment's
10
DALMIA CEMENT (BHARAT) LIMITED - ARIYALUR
Installed Capacity (Clinker) - 2 MTPA Installed Capacity (Cement) - 3 MTPA Captive Power Plant (CPP) - 27MW Product Type - OPC, PPC
Overall Summary
S.NO SGA PROJECTS QTY ONE TIME
INVESTMENT (LACS)
SAVINGS (KW/HR)
SAVINGS (LACS/YR)
1 IMPLEMENTED 6 2.72 145.5 16.12
2 UNDER PROGRESS 3 4.3 9.96 3.14
3 UNDER APPROVAL 3 52.5 134 22.83
4 UNDER STUDY 2 6 20.3 3.61
TOTAL 14 65.52 309.76 45.7
Optimization of Compressed air in Rawmill HAG
Team ADSS Background: Compressor power consumption was more in Rawmill HAG.
Observation Made: More pressure drop in Raw mill HAG due to Non uniformity of compressor pipeline between coal mill to HAG
Action Taken: Compressor air pipe line size was modified from 1” to 2” (Coal mill to HAG).
Savings Achieved: Energy : 241 KW/Day
Cost : 1.27 Lakhs/Annum
Project 1
Optimization of Compressed air in Rawmill HAG
Receiver tank
Coal mill
HAG
2” pipeline
Friction loss -
0.39 bar
1” pipeline
Friction loss -
1.32 bar
Receiver tank
Coal mill
HAG
2” pipeline
Friction loss -
0.39 bar
2” pipeline
Friction loss -
0.39 bar
Before After
Reduction of 1 bar = 7% of Power Reduction
Raw mill productivity enhancement
Team ADSS Background: We are not able to achieve the desired production of 440 TPH, due to raw meal
residue was around 2 % on 212 microns even at full speed of Raw mill fan.
Observation Made: Raw mill classifier seal gap was found 12 mm which leads to higher raw meal
residue
Action Taken: Classifier seal gap was reduced from 12 to 6 mm by providing the felt seal
Savings Achieved: Energy : 2112 KW/Day Cost : 10 Lakhs/Annum
Project 2
Raw mill Classifier seal gap reduced from 12 to 6mm by
providing the felt seal
Raw Mill Classifier Seal Gap
Reduction of False air in Cement mill
Team 2.0 Background: Cement mill false air was more which leads to increase the sp. power
consumption of fan
Observation Made: Cement mill bag house rotary air lock bottom false air enriching was more
because of gap in both rotor end
Action Taken: Bag house RAL rotor end opening was fully closed and false air was reduced
from 11 to 9.8 %
Savings Achieved: Energy : 240 KW/Day Cost : 1.7 Lakhs/Annum
Project 3
Cement Mill Bag House RAL
Cement mill bag house rotary air lock - rotor both end
opening was closed and false air was reduced from
11% to 9.8%
THANK YOU