reporte fallas 09-30-04

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    Doble Engineering Company

    Troubles & Failures Report8/1/2004 To 9/30/2004

     Arrester - TroubleIncident # Incident Date Report Date Photo File Name

    43921 4/29/2003 10/14/2004 IID200401,02,03

    Manufacturer Model Number KV Mfgr Year  

    Joslyn 8110D0001J096 51-100 kV

    Method of Detection

    Cause of Failure

    No apparent trouble in the system.

    Comments

    (Photo was unavailable for release in this report.)

     Arrester - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43922 11/15/2003 10/14/2004

    Manufacturer Model Number KV Mfgr Year  Joslyn ZE 51-100 kV NONE

    Method of Detection

    Cause of Failure

    Line down.

    Comments

    B/O lightning arrester on RNO breaker.

     Arrester - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43961 12/25/2003 2/23/2004 SNPD2004_Rept04

    Manufacturer Model Number KV Mfgr Year  

    Ohio Brass 219576 101-150 kV 2001

    Method of Detection

    Cause of Failure

    Unknown - clear day, no moisture found internally.

    Knowledge Is PowerSM

     Apparatus Maintenance and Power Management For Energy Delivery

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    Comments

     Arrester failed only about 3 months after it was installed as a replacement to an old SiC

    arrester. O.B. had identified arresters that had a problem with moisture ingress,

    but this S/N was not part of their recall. O.B. performed an analysis, but no cause

    was identified. (Photo was unavailable for release in this report.)

    Bushing-Condenser (oip) - TroubleIncident # Incident Date Report Date Photo File Name

    43924 5/2/2003 10/14/2004

    Manufacturer Model Number KV Mfgr Year  

    General Electric PVDB1155202 11-15 kV 2002

    Method of Detection

    Cause of Failure

    Comments

    Bushing-Condenser (oip) - TroubleIncident # Incident Date Report Date Photo File Name

    43969 8/19/2003 3/25/2004

    Manufacturer Model Number KV Mfgr Year  

    General Electric 550W1600UG 451-500 kV 1981

    Method of Detection

    Failed Doble power factor test.

    Cause of Failure

    Comments

    Type U 500KV Bushing - evidence of water entering at top terminal gasket.

    Bushing-Condenser (oip) - TroubleIncident # Incident Date Report Date Photo File Name

    43942 3/8/2004 3/23/2004 sce2004_rept01a,b

    Manufacturer Model Number KV Mfgr Year  

    General Electric FK69-3500-1 51-100 kV 1962

    Method of Detection

    Cause of Failure

    Comments

    Type U bushing on circuit breaker failed. (Picture was unavailable for release in this report.)

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    Bushing-Condenser (oip) - Failure at TestIncident # Incident Date Report Date Photo File Name

    43891 8/13/2004 8/16/2004

    Manufacturer Model Number KV Mfgr Year  

    Lapp POC 101-150 kV

    Method of Detection

    Bushings: C1 Power Factor 

    Cause of Failure

    Bushing

    Comments

    Cable - TroubleIncident # Incident Date Report Date Photo File Name

    43934 6/4/2003 3/18/2004 MWD2004_Rept01A(thru C).JPGManufacturer Model Number KV Mfgr Year  

    Rome 0-5 kV 1982

    Method of Detection

    Cause of Failure

    Insulation failure due to old manufacturing formulation.

    Comments

    The hydro plant tripped due to utility excursion. After receiving permission from the utility for

    restart, the unit tripped as soon as the breaker closed. A Megger test revealed a problem

    with one of the conductors from the unit circuit breaker to transformer. A hole slightly larger

    than a quarter was found in the failed cable. (Photos were unavailable for release in this

    report.) As preventative measures, the asset owner will survey other 14 hydro plants

    for similar old XLP cables and continue cable testing every 5 years; they may also consider

    a shorter interval between cable tests, particularly for older cables.

    Capacitor - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43926 1/5/2004 4/1/2004

    Manufacturer Model Number KV Mfgr Year  

    Westinghouse Electric series caps 201-250 kV 1966

    Method of Detection

    Cause of Failure

    Comments

    Cap bank was called to bypass. Bypass switch got part way closed causing extended arcing (blowing

    up glass & burning up contacts). Bank was installed in 1966. Parts are wearing out and getting hard to get.

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    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43947 8/15/2001 4/15/2004

    Manufacturer Model Number KV Mfgr Year  

    Westinghouse Electric 242-SP-50 251-300 kV 1980

    Method of Detection

    Cause of Failure

    Failed air compressor.

    Comments

     AØ DID NOT CLOSE. BREAKER USED UP ENOUGH AR TO LOCK OUT AIR COMPRESSOR. BROUGHT

    IN LOW AIR ALARM, AND LOCKED OUT. CLOSING CIRCUIT TO GCB. FOUND BROKEN RINGS ON

    PISTON AØ MECH; ALSO FOUND BROKEN 1" ROLL PIN IN PISTON ROD. BOLTS IN OPENING

    VALVE ASEMB.

    Circuit Breaker - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43962 1/7/2003 2/23/2004

    Manufacturer Model Number KV Mfgr Year  

    Siemens FCV-500 11-15 kV 1979

    Method of Detection

    Cause of Failure

    Trip coil failure.

    Comments

    Circuit switcher operated to clear fault, interrupting service to approx 5,000 customers.

    However, circuit switcher would not close again, and motor operator had to be repaired.

    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43952 1/17/2003 4/15/2004

    Manufacturer Model Number KV Mfgr Year  

    McGraw Edison AHJ-60-138-10000 151-200 kV 1973

    Method of Detection

    Cause of Failure

    Mechanism lubrication dried up.

    Comments

    FOUND ALL BEARING STIFF, OR NOT MOVING AT ALL IN MECH. R & R TRIP ASS.

    REMOVE AND DISASSEMBLE STIFF TRIP LINKAGE, LUBE PINS

     AND FREE UP STIFF BEARINGS. NOW THE BREAKER LATCHES EVERY TIME.

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    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43946 1/22/2003 4/16/2004

    Manufacturer Model Number KV Mfgr Year  

    Siemens SPS2-245-40-1 201-250 kV 2001

    Method of Detection

    Cause of Failure

    While being energized, pole 3 went phase to ground.

    Comments

    Removed SF6 gas & removed pole 3 cover. Found that pole 3 did flash to ground.

    Looks like it flashed from the corona ring to the tank. 7 of the same voltage level

    and model in the 2000/2001 mfg year were internally inspected.

    Circuit Breaker - Trouble

    Incident # Incident Date Report Date Photo File Name43951 2/5/2003 4/15/2004

    Manufacturer Model Number KV Mfgr Year  

    Westinghouse Electric GO-3D 51-100 kV 1950

    Method of Detection

    Cause of Failure

    Exhaust piston stuck.

    Comments

    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43916 2/24/2003 4/4/2004 BPAT200414-19

    Manufacturer Model Number KV Mfgr Year  

     ABB 550PM 50-30 > 500 kV 2003

    Method of Detection

    Cause of Failure

    Restrike

    Comments

    Breaker sent a trip command via SCADA. A & B phases interrupted approximately 320

     Amps. C-phase continued to carry load current for approximately 16 cycles. Breaker

    Failure Relay operated and cleared the bus. Breaker was commission tested and in

    service less than 6 weeks. (Photo was unavailable for release in this report.)

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    Circuit Breaker - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43953 3/24/2003 4/15/2004

    Manufacturer Model Number KV Mfgr Year  

    McGraw Edison CH-60A-69-3500 51-100 kV 1974

    Method of Detection

    Cause of Failure

    Comments

    FOUND CLOSE COIL OPERATOR IN PIECES AND CLOSE COIL BO, REBUILT CLOSING MEC. AND REPLACED COIL.

    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43968 4/2/2003 3/25/2004

    Manufacturer Model Number KV Mfgr Year   Alsthom HGF-1014 201-250 kV 2002

    Method of Detection

    Cause of Failure

    Internal contamination from factory

    Comments

    Internal fault B Phase to ground 15000amps

    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name43950 4/15/2003 4/15/2004

    Manufacturer Model Number KV Mfgr Year  

    Mitsubishi 101-150 kV 2001

    Method of Detection

    Cause of Failure

    B/O closing coil.

    Comments

    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43954 5/22/2003 4/15/2004

    Manufacturer Model Number KV Mfgr Year  

    McGraw Edison AHJ-60-138-1000 101-150 kV 1973

    Method of Detection

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    Cause of Failure

    Mechanism lubricants dried out.

    Comments

    Breaker had problems closing.

    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43939 7/1/2003 10/14/2004 PAC200402

    Manufacturer Model Number KV Mfgr Year  

     ABB 145PMI 101-150 kV

    Method of Detection

    Cause of Failure

    Broken stud that mounts the stationary arcing contact inside the stationary contact assem

    CommentsThis was likely caused by a stress concentration due to a surface defect such as a crack at

    the root of the threads. (Photo was unavailable for release in this report.)

    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43948 7/7/2003 4/15/2004

    Manufacturer Model Number KV Mfgr Year  

    Westinghouse Electric 242-SP-50 251-300 kV 1980

    Method of Detection

    Cause of Failure

    Comments

    07/07/03 Breaker timing problem. Timed breaker, found out by 15 ms, will need to come

    back to adjust. 07/10/03 Adjusted phase-to-phase timing on breaker. Turned

    screw on close pilot valve out to speed up tank 3; it is still slower than factory spec.

    Circuit Breaker - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43973 8/2/2003 4/6/2004

    Manufacturer Model Number KV Mfgr Year  

    General Electric FK-144-250Y 11-15 kV 1956

    Method of Detection

    Cause of Failure

    Fault started at line arrester, breaker did not clear fault.

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    Comments

    Breaker tank ruptured. Breaker was a total loss. (Lightning in area.)

    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43937 8/10/2003 5/18/2004 MWD2004_Rept04A(and B).jpgManufacturer Model Number KV Mfgr Year  

    Siemens SPS-38-23-1 36-50 kV 1995

    Method of Detection

    Cause of Failure

    Comments

    This CB has been leaking since installation. Utility personnel spent a couple of days

    troubleshooting this CB using conventional gas detection methods but were not successful.

    The amount of leak was very minimal; about 5 pounds of SF6 gas was added once a yr.GIS came to the power plant on 10/27/03 to perform laser imaging on the breaker. The

    camera detected a leak on the supply line fitting of A-Phase; no other leaks were found.

    Utility personnel performed soap bubble test to confirm the leak and then adjusted the fitting.

    Re-shot of the fitting showed no more SF6 leak. (Photo unavailable for release in this report.)

    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43949 8/17/2003 4/15/2004

    Manufacturer Model Number KV Mfgr Year  

    Westinghouse Electric 242-SP-50 251-300 kV 1980

    Method of Detection

    Cause of Failure

    Comments

    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43923 9/10/2003 10/14/2004 IID200304,05,06,07,08,09

    Manufacturer Model Number KV Mfgr Year  

    Siemens BZO121406 151-200 kV 1984

    Method of Detection

    Tested the bushings and found variable capacitance.

    Cause of Failure

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    Comments

    Replaced the breaker. (Photos unavailable for release in this report.)

    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43966 10/2/2003 2/16/2004Manufacturer Model Number KV Mfgr Year  

    I.T.E. 242-GA63-30C 201-250 kV 1981

    Method of Detection

    Cause of Failure

    Deterioration of capacitor.

    Comments

    Replacement Capacitors not available-Pole 2 destroyed.

    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43915 10/18/2003 4/4/2004 BPAT200412,13

    Manufacturer Model Number KV Mfgr Year  

     ABB 550PM 40-30 > 500 kV 2003

    Method of Detection

    Cause of Failure

    Comments

    Breaker sent a trip command via SCADA. A & B phases interrupted approximately 250

     Amps. C-phase continued to carry load current for approximately 16 cycles. Breaker

    Failure Relay operated and cleared the bus. (Photos were unavailable for release in this report.)

    Circuit Breaker - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43960 10/28/2003 2/23/2004

    Manufacturer Model Number KV Mfgr Year  

    Siemens FCV500 11-15 kV 1979

    Method of Detection

    Cause of Failure

    Trip coil burned, breaker did not operate, took substation off line.

    Comments

    Failure caused interruption of service to approx. 5000 customers.

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    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43943 11/10/2003 3/23/2004 sce2004rept_02

    Manufacturer Model Number KV Mfgr Year  

     ABB 72PMI31-12 51-100 kV 2000

    Method of Detection

    Cause of Failure

    Shorted B-phase close coil causing.

    Comments

    Close signal was initiated via automatic capacitor controls, B phase close coil

    leads were shorted. X relay contacts welded closed causing cb to pump until A phase

    interrupter failed. It appears the cb close-opened. (Photo unavailable.)

    Circuit Breaker - In-Service Failure

    Incident # Incident Date Report Date Photo File Name43909 11/16/2003 4/4/2004 BPAT200401, BPAT200420

    Manufacturer Model Number KV Mfgr Year  

    Brown Boveri Company 72 PM 51-100 kV 1988

    Method of Detection

    Cause of Failure

    Bird droppings from an overhead structure washed down onto the bushings by the rain.

    Comments

    2 entrance bushings failed. Repair of the breaker required an internal inspection, replacement bushings and

    unknown internally damaged parts to be replaced. Time to repair was longer than replacing the breaker

    from stock so bkr was replaced. Additionally, the load lost needed to be restored. (Photos unavailable.)

    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43940 11/26/2003 12/1/2003

    Manufacturer Model Number KV Mfgr Year  

    High Voltage Breakers HVB362 301-350 kV 2003

    Method of Detection

    Cause of Failure

    Defective material in the dashpot piston.

    Comments

    New breaker not in service. Relay doing final trip testing. Got pole disagreement

    alarm. Found bent linkages in the mechanism of one phase. HVB sent factory people

    to investigate. Found damage to linkages in mechanism, the aluminum cast support

    conductor that holds the puffer piston, the puffer piston, the Teflon nozzle, and

    the stationary contacts. HVB removed and replaced the whole phase. Took damaged

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    phase to factory for investigation. HVB acted quickly and performed all repairs

    at no cost to utility. Report available.

    Circuit Breaker - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43925 12/20/2003 4/1/2004Manufacturer Model Number KV Mfgr Year  

    I.T.E. VRK-15-12 11-15 kV 1972

    Method of Detection

    Cause of Failure

    Failure of mag latch and mech to keep breaker in the tripped position.

    Comments

    ITE VRKs have a history of mag latch failures and parts are no longer available.

    Circuit Breaker - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43913 1/6/2004 4/4/2004

    Manufacturer Model Number KV Mfgr Year  

    Pennsylvania Transformer RHE-84L 201-250 kV 1965

    Method of Detection

    Cause of Failure

    Latch valve failed due to lack of lubrication.

    Comments

    Trouble: OCB failed to reclose. Temperature -32 degrees. Mechanism does not move.

    Corrective action - Removed and cleaned latch valve. Cleaned and lubed mechanism.

    Circuit Breaker - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43912 1/6/2004 4/4/2004

    Manufacturer Model Number KV Mfgr Year  

    Pennsylvania Transformer RHE-84-230-15000 201-250 kV 1965

    Method of Detection

    Cause of Failure

    Comments

    Trouble: OCB failed to reclose. Temperature -32 degrees. Mechanism does not move.

    Corrective action - Removed and cleaned latch valve. Cleaned and lubed mechanism.

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    Circuit Breaker - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43964 1/29/2004 2/23/2004

    Manufacturer Model Number KV Mfgr Year  

    Siemens FCV500 11-15 kV 1979

    Method of Detection

    Cause of Failure

    Trip coil burned, circuit breaker failed to operate on distribution circuit fault.

    Comments

    When the 12 kV circuit breaker failed to operate, backup relaying sensed the fault

    and opened the 115 kV circuit switcher, interrupting service to approximately 5000

    customers. This was the 3rd incident in 4 months where failure of a FCV-500 trip

    coil caused a station to trip off line.

    Circuit Breaker - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43956 3/19/2004 4/15/2004

    Manufacturer Model Number KV Mfgr Year  

     Allis-Chalmers FC-500-A1 11-15 kV 1974

    Method of Detection

    Cause of Failure

    Trip mechanism frozen; lubrication dried up.

    Comments

     ACB WAS OVERHAULED 2 YRS AGO. PLAN TO REVISE LUBRICATION PROCEDURES ON BREAKER

    MECHANISMS. THIS ACB FAILED TO OPEN ON A FEEDER FAULT CAUSING THE

    BUS OVERCURRENTS TO CLEAR AN ENTIRE BUS SECTION (5 ADDITIONAL CIRCUITS)

    Circuit Breaker - TroubleIncident # Incident Date Report Date Photo File Name

    43888 7/6/2004 8/4/2004 3449164710432161.JPG

    Manufacturer Model Number KV Mfgr Year  

     ASEA-Brown Boveri 242PMG50-30 201-250 kV 2000

    Method of Detection

    Visual Inspection

    Cause of Failure

    Leak/Gasket

    Comments

    Moisture trapped in the mechanism housing caused massive corrosion damage and multiple

    breaks on the disc springs on this AHMA-11 mechanism. The mechanism is not repairable

    and is a total loss. Some water found an access into the mechanism housing, apparently

    through some inadequate sealing procedures during installation. The drain hole

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    was removed and over one quart of water poured out from the mechanism. A new mechanism

    was installed and proper installation and sealing procedures were followed.

    Circuit Switcher - TroubleIncident # Incident Date Report Date Photo File Name

    43971 7/3/2003 3/25/2004

    Manufacturer Model Number KV Mfgr Year  

    S&C Electric 2040 51-100 kV 1988

    Method of Detection

    Cause of Failure

    Voids & unmelted plastic in Delrin Spring Carrier allowing Red Target to actuate even though there was no SF6 leak.

    Comments

    We have had 30 or so of these Red Target-Low Gas problems and have been sending

    back the Interrupters for a porcelain credit. We were told by the factory that units

    between 1988 and 1991 did have manufacturing problems with the carrier, but, notrouble since 1991. Then we had several 1992 and 1995 failures and contacted them

    again. Recently we had the S&C Factory research this problem thoroughly and they

    have a new repair kit that we can install in the field.

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    Circuit Switcher - TroubleIncident # Incident Date Report Date Photo File Name

    43928 7/31/2003 4/1/2004

    Manufacturer Model Number KV Mfgr Year  

    S&C Electric Mark IV 301-350 kV 1978

    Method of Detection

    Cause of Failure

    Unknown. Shipped failed interrupters back to S&C.

    Comments

    Interrupters on south pole failed to interrupt. Opened circuit with air break arms.

    Circuit Switcher - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43927 11/1/2003 11/1/2003 IPC2004_Rept03

    Manufacturer Model Number KV Mfgr Year  S&C Electric S&C 2020 51-100 kV 1994

    Method of Detection

    Cause of Failure

    Comments

    Problem with this design, if the circuit switcher fails to trip, (trip coil failure)

    the agastat times out and the disconnects open even though the SF6 bottles do

    not. The clearances on the open 69 kv disconnects are too close and the energized

    line was flashing over phase to phase. This C/S needs a redesign, or we could roll

    the C/S 180 so the open disconnects would not be energized when the gas bottles

    were closed. (Photo not available for release in this report.)

    Circuit Switcher - TroubleIncident # Incident Date Report Date Photo File Name

    43914 2/3/2004 4/4/2004 BPAT200403,04,05,

    Manufacturer Model Number KV Mfgr Year  

    S&C Electric Mark IV > 500 kV 1979

    Method of Detection

    Cause of Failure

    Mechanical failure of the interphase linkage.

    Comments

    While attempting to close circuit switcher via SCADA, the reactor and bus LOR's

    operated. South bus LOR reset. Operator reported only two phases closed and linkage

    between phases on the ground. (Photo unavailable.)

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    CT - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43967 11/27/2003 2/15/2004

    Manufacturer Model Number KV Mfgr Year  

    Haefely IOSK-245 201-250 kV 1985

    Method of Detection

    Cause of Failure

    Internal fault

    Comments

    CT Column caught on fire & failed due to A Phase to Ground fault. This is a free-standing

    oil-filled CT.

    CT - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43890 11/27/2003 8/16/2004 27131316710412281.ppt

    Manufacturer Model Number KV Mfgr Year  Trench Electric IOSK-245 201-250 kV 1984

    Method of Detection

    Other (See Comments), Relay Operation

    Cause of Failure

    Deteriorated Insulation

    Comments

    This is for a 230kV free standing CT that failed catastrophically while in service.

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    Insulator - Trouble

    Incident # Incident Date Report Date Photo File Name

    43936 10/21/2003 3/18/2004 MWD2004_Rept03A(thru H).JPG

    Manufacturer Model Number KV Mfgr Year  

    Other 201-250 kV 1933

    Method of Detection

    Cause of Failure

    Unknown cause but note age of equipment.

    Comments

    One insulator stack pulled completely away, littering the station floor with insulator

    material. (Photo unavailable.)

    PT - TroubleIncident # Incident Date Report Date Photo File Name

    43935 6/10/2003 3/18/2004

    Manufacturer Model Number KV Mfgr Year  

    General Electric JVM 0-5 kV 1979

    Method of Detection

    Cause of Failure

    Failure attributed to age of the equipment.

    Comments

    Both units tripped offline. From investigation, both fuses on the primary side

    were found blown. TTR revealed shorted turns in the faulty P.T. The P.T. was replaced

    with an old spare; new P.T.'s were ordered and will be changed-out at the next scheduled

    maintenance. As preventive measures, other hydro plants will be surveyed for

    the same type and manufacture P.T., of the same vintage, and consideration given to

    performing insulation resistance tests on older P.T.'s during annual shutdowns.

    Reactor - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43899 2/21/2004 9/14/2004

    Manufacturer Model Number KV Mfgr Year  

    Trench Electric Shunt 26-35 kV 1981

    Method of Detection

    Other (See Comments)

    Cause of Failure

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    Deteriorated Insulation

    Comments

     After the reactor circuit breaker tripped, a lockout alarm indication was given.

     A turn-to-turn failure occurred on the inside package of the reactor. Trench stated

    that switching surges over long term operation can cause a shorted turn that creates

    a high circulating current blowing out the winding. At 23 years old Trench stated

    that it served its useful life. Inspection of other units was suggested. Reactorsof this age don't have arresters. New ones do to protect from TOVs during switching.

    Consequently, we will be adding arresters to the other reactors in service.

    Regulator - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43938 6/3/2004 3/25/2004 PAC200401a,b,c

    Manufacturer Model Number KV Mfgr Year  

    Siemens JFR 16-20 kV 2002

    Method of Detection

    Cause of Failure

    Spring failure - Siemens has redesigned the spring to a compression type.

    Comments

    We have seen several new model JFR regulators with this problem. Usually when a

    drive spring breaks the operating mech jams. However this regulator tried to go

    through the neutral position with only motor drive and caused an open circuit at the

    reversing switch. (Photo was not available for release in this report.)

    Relay - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43963 1/28/2004 2/23/2004

    Manufacturer Model Number KV Mfgr Year  

    Basler BE1-51 N/A 1996

    Method of Detection

    Cause of Failure

    Relay housing did not short CT circuit when relay was pulled for maintenance.

    Comments

    When the relay technician was removing a Basler BE1-51 relay for maintenance, theshorting device did not make a connection to the CT circuit. When the paddle was

    removed, technician heard buzzing noise (from CT opening), then differential relay

    operated, opening circuit switcher. Service interrupted to about 5000 customers

    for several minutes until relay re-installed and station put back on line.

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    Switch - TroubleIncident # Incident Date Report Date Photo File Name

    43911 5/14/2003 4/4/2004 BPAT200402

    Manufacturer Model Number KV Mfgr Year  

    (No MFR Listed) TA-3A 251-300 kV 1964

    Method of Detection

    Cause of Failure

    C-phase of the disconnect mechanically failed & stayed in the harp while operating the

    disconnect switch. A-phase and B-phase opened normally.

    Comments

    This Schwager-Wood disconnect had a history of problems, likely associated to the

    instability of the ground conditions at the site. The C-phase blade was found loose,

    in the harp, in a rotated position. The crank arm at the hinge end was fully rotated

    in the full open position. It does not appear that the blade left the harp during

    operation. (Photo unavailable for release in this report.)

    Switch - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43910 5/16/2003 4/4/2004

    Manufacturer Model Number KV Mfgr Year  

     Allis-Chalmers Pantograph > 500 kV 1968

    Method of Detection

    Cause of Failure

    Mechanical failure of pantograph-type blade on the disconnect.

    Comments

    It has been determined that this disconnect is not needed on the system anymore due

    to system configuration changes. It is scheduled to be removed. Removal of this

    disconnect will allow us to have spare parts for the remaining 8 pantograph disconnects

    on our system pending replacement.

    Switch - Failure at TestIncident # Incident Date Report Date Photo File Name

    43894 7/20/2004 8/30/2004

    Manufacturer Model Number KV Mfgr Year  

    (No MFR Listed) EV-1 > 500 kV

    Method of Detection

    Other (See Comments)

    Cause of Failure

    Other (See Comments)

    Comments

    The equipment was a Southern States EV-1 500-kV disconnect switch. The part that

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    failed was the VM-1, slave, motor operator on A-phase. When the

    MOD (Motor Operated Disconnect) was operated, A-phase motor operator continued

    to turn after the blade was fully open. This caused the coupling between the gear

    box and the shaft connected to the rotating stack to fail. After this occurred,

    the motor operator continued to spin, breaking off all open and close stops on the

    motor operator. The motor operator was finally stopped when the DC control knife

    switch was pulled. It was found that the 1" stainless steel gear shaft was crackedvertically.

    The entire motor operator was replaced.

    Transformer - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43917 5/17/2003 4/4/2004

    Manufacturer Model Number KV Mfgr Year  

    Wagner Electric HAL 24 101-150 kV 1951

    Method of Detection

    Cause of Failure

    Winding failure due to lightning.

    Comments

    Through Fault

    Transformer - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43958 6/6/2003 2/23/2004

    Manufacturer Model Number KV Mfgr Year  

    Federal Pacific Electric Transformer, LTC 101-150 kV 1968

    Method of Detection

    Cause of Failure

     A high-current, three phase, through fault occurred and the transformer failed.

    Comments

    Failure caused interruption of service to 3000 customers including several large

    industrials. This vintage of FPE transformer is prone to failure. We purchased

    5 of these in 1968 and all five have now failed. Most of them failed during a through-fault.

    Transformer - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43929 6/19/2003 4/1/2004

    Manufacturer Model Number KV Mfgr Year  

    Wagner Electric 101-150 kV 1970

    Method of Detection

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    Cause of Failure

    Poor design.

    Comments

    Through-fault during lightning storm (windings failed).

    Transformer - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43908 6/20/2003 4/23/2004

    Manufacturer Model Number KV Mfgr Year  

    Westinghouse Electric 101-150 kV 1964

    Method of Detection

    Cause of Failure

    Possibly Lightning

    CommentsHoop failure (progressive turn-to-turn fault); replaced the transformer.

    Transformer - TroubleIncident # Incident Date Report Date Photo File Name

    43944 7/3/2003 3/23/2004 sce2004_Rept03

    Manufacturer Model Number KV Mfgr Year  

    Westinghouse Electric Unknown 1954

    Method of Detection

    Cause of Failure

    Probably age related.

    Comments

    Contact leaf spring failed. (Photo unavailable.)

    Transformer - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43959 7/5/2003 2/23/2004 SNPD2004_Rept02a,b,c

    Manufacturer Model Number KV Mfgr Year  

    General Electric Transf, w LTC 101-150 kV 1975

    Method of Detection

    Cause of Failure

    Squirrel contacted 12 kV bus on source side of circuit breaker. Corroded wiring prevented

    circuit switcher from tripping. Sustained fault caused much damage

    Comments

    Fault started when a squirrel contacted the source side of an outdoor 12 kV breaker.

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     The fault grew and involved all three-phases. Relays saw the fault properly, and

    provided signal to circuit switcher to trip. Circuit switcher did not trip due

    to corroded wiring inside conduit (not visible from ends). Fault and fire damage

    was extensive. Two breakers and bus support structure were burned. Transformer

    failed during the through-fault. Service interrupted to 5000 customers. (Photo unavailable.)

    Transformer - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43972 7/10/2003 4/22/2004

    Manufacturer Model Number KV Mfgr Year  

    Virginia Transformer 51-100 kV 1993

    Method of Detection

    Cause of Failure

    Unknown

    CommentsTurn to turn failure on the secondary winding. Performed complete rewinding of all coils,

    testing and tank refurbishment, repair of load tap changer, installation of new remote

    temperature gauges, new insulating oil, install tap changer filter unit, desiccant drier breather.

    Transformer - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43931 8/4/2003 4/2/2004

    Manufacturer Model Number KV Mfgr Year  

    General Electric 451-500 kV

    Method of Detection

    Cause of Failure

    Comments

    This transformer has Trench 287 kV high-voltage composite bushings.

     A flashover occurred between the bottom plate and the tank wall of the transformer 

    and another fault between the upper part of the oil impregnated paper winding and

    the flange of the composite insulator. All high-voltage bushings were replaced.

    Transformer - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43970 8/19/2003 3/25/2004

    Manufacturer Model Number KV Mfgr Year  

    General Electric 367 MVA 451-500 kV 1981

    Method of Detection

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    Cause of Failure

    Lightning strike to bushing (H S bushing)

    Comments

    Bushing failed due to low oil level resulting in lower BIL, water had entered bushing

    on top terminal gasket. Due to internal damage, replaced transformer.

    Transformer - TroubleIncident # Incident Date Report Date Photo File Name

    43965 9/10/2003 3/2/2004

    Manufacturer Model Number KV Mfgr Year  

    Ferranti, Ltd. Transformer LTC 101-150 kV 1995

    Method of Detection

    LTC was severely coked and producing high levels of ethylene.

    Cause of Failure

    Poor design and/or quality of LTC

    CommentsProblems were uncovered during routine DGA of the tap changer oil. The first test

    showed extremely high levels of ethylene, about 100 times normal. We suspected

    the test was faulty, so a second sample was drawn, and it had 145,000 ppm ethylene.

    The Doble lab reported this ethylene level was the highest they have ever recorded

    in a DGA sample. The tap changer was maintained less than 2 years ago and has an

    oil filtration unit installed. When opened up, the reversing switch had severe

    coking. Movable and stationary contacts also required replacement.

    Transformer - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43941 10/1/2003 10/22/2003

    Manufacturer Model Number KV Mfgr Year  

    General Electric LRT-200-2 Unknown

    Method of Detection

    Cause of Failure

    Bypass switch assembly misalignment on phase 3.

    Comments

    Transformer failed due to tap changer failure. Report available.

    Transformer - TroubleIncident # Incident Date Report Date Photo File Name

    43957 10/14/2003 4/15/2004

    Manufacturer Model Number KV Mfgr Year  

    Federal Pacific Electric 51-100 1974

    Method of Detection

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    Cause of Failure

    Low side turn-to-turn failure.

    Comments

    DGA RESULTS - * The equipment condition code has been abnormal (2-3) since 08/13/2003.

    The high CO2/CO ratio may indicate thermal decomposition of cellulose. Exercise

    caution. Determine load dependence.

    Transformer - TroubleIncident # Incident Date Report Date Photo File Name

    43920 11/29/2003 4/4/2004 BPAT200406

    Manufacturer Model Number KV Mfgr Year  

    Hyundai BPA001000891 101-150 kV

    Method of Detection

    Cause of FailureLow voltage leads flashed over to the core.

    Comments

    The transformer tripped by two sets of differential, the Buchholz and the pressure relief 

    device operated. The 115 KV breaker at Drummond and the 161 KV breaker at Goshen

    (72 miles) isolated the failed transformer within 4 cycles. The quick response from the

    relays and breaker may have prevented further damage to the transformer. There were

    of combustible gasses in the oil including acetylene, but the transformer tested OK

    electrically. The manufacturer reported to the site within one week after the failure,

     inspected the transformer and found that there was a dielectric breakdown between the

    X1 C-phase and X2 B-phase leads and the core clamping structure through a lead

    supporting board for X1, X2 and X3 leads. The failure occurred close to the X1 bushing

    after the lead makes a 90 degrees angle from vertical to horizontal. (Photo unavailable.)

    Transformer - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43930 1/13/2004 4/2/2004

    Manufacturer Model Number KV Mfgr Year  

    General Electric FOA 451-500 kV

    Method of Detection

    Cause of Failure

    Bushing Failure

    Comments

    Trench 230kv bushing failure caused total loss of transformer. We are replacing

    all of these type composite bushings.

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    Transformer - TroubleIncident # Incident Date Report Date Photo File Name

    43907 1/15/2004 4/23/2004 AVA2004_01

    Manufacturer Model Number KV Mfgr Year  

     Alsthom > 500 kV 2002

    Method of Detection

    Cause of Failure

    Comments

    High voltage winding insulation failed. (Photo unavailable.)

    Transformer - TroubleIncident # Incident Date Report Date Photo File Name

    43918 1/16/2004 4/4/2004 BPAT200407,08,09,10,11

    Manufacturer Model Number KV Mfgr Year   Allis-Chalmers 301-350 kV 1963

    Method of Detection

    Cause of Failure

    Internal fault leading to winding failure.

    Comments

    (Photos unavailable.)

    Transformer - TroubleIncident # Incident Date Report Date Photo File Name43932 2/16/2004 4/2/2004

    Manufacturer Model Number KV Mfgr Year  

     ASEA Inc. TFTY1000 201-250 kV

    Method of Detection

    Cause of Failure

    Internal fault caused can to split a welded seam along the lid on low-voltage side of transformer.

    Comments

    Unit was 8 years beyond design life, paper insulation degradation, 2300 piles driven

    into ground in area for new construction, and decrease in insulation distance between

    18kv internal delta bus at bottom of transformer tank.

    Transformer - TroubleIncident # Incident Date Report Date Photo File Name

    43933 2/17/2004 4/26/2004 MID200401,02,03

    Manufacturer Model Number KV Mfgr Year  

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    Kuhlman Electric 51-100 kV 1979

    Method of Detection

    Cause of Failure

    Possibly due to previous over tightening of wire connection to collection ring stud.

    Comments

     An inspection of the LTC was made as part of the regular maintenance when the electriciannoticed the phenolic collector ring panel was burnt. The two studs passing through

    the phenolic collector ring panel from the collector ring overheated causing the

    board and studs to deteriorate. The 3/4" studs are reduced to 1/2" on the end connecting

    to the collector ring. Solder is then sweat into the threads from the other side

    (penetrating approx. 1/4"). I suspect the stud had loosened from the collector ring

    (possibly due to previous over tightening) and overheated to the point the cable,

    with the studs attached, came loose in the electricians hand. (Photo unavailable.)

    Transformer - TroubleIncident # Incident Date Report Date Photo File Name43919 2/20/2004 4/4/2004 BPAT200421, 22

    Manufacturer Model Number KV Mfgr Year  

     Allis-Chalmers 301-350 kV 1963

    Method of Detection

    Cause of Failure

    Internal Fault

    Comments

    Winding failure. (Photo unavailable.)

    Transformer - TroubleIncident # Incident Date Report Date Photo File Name

    43945 3/19/2004 3/23/2004 sce2004_Rept04a,b

    Manufacturer Model Number KV Mfgr Year  

    General Electric Unknown 1951

    Method of Detection

    Cause of Failure

    Tracking and burning of the insulating drum on NLTC allowed the conductor contact pointsto be misaligned and become loose. Severe arcing occurred.

    Comments

    Uneconomical to repair unit. This station is isolated load

    so a generator had to be installed to off load transformer. (Photo unavailable.)

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    Transformer - TroubleIncident # Incident Date Report Date Photo File Name

    43955 3/30/2004 4/15/2004 Sdge2004Rept10A-G.JPG

    Manufacturer Model Number KV Mfgr Year  

    Waukesha LTC PWR XFMR 2002

    Method of Detection

    Cause of Failure

    High moisture.

    Comments

    Before we put the bank in service in April of 2003 , it failed the Doble test. When

    we opened it up we found severe rust all over the core. Waukesha came out and cleaned

    it up and called it good. It still Doble tested bad. It started gassing so it

    was taken out of service. We Doble tested it before Waukesha reps got here to see

    if it was worse than the initial test; it was. The CL watts went from 1.543 to 6.619 and the

    CHL watts went up to 8.250 from 1.895. We also megger tested it again to see if that

    had gotten worse and it did. Low to ground was 10.7 gig ohms and now it only got89.7 meg ohms. When Waukesha drained it and opened it up on 3-21-04, the rust and

    contamination looked worse than it did back in March of 2003. In March of 2003,

    Waukesha drained and processed the oil for 24 hours. This was after they got inside

    and cleaned up the rust off of the top of the core. The transformer came to us from

    Waukesha with oil in it. The only time it was opened up when it was originally put in

    service was when the factory rep was here to supervise the installation of the bushings.

    Two-Winding Transformer - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43898 1/4/2004 9/14/2004

    Manufacturer Model Number KV Mfgr Year  

    General Electric L252778A 1981

    Method of Detection

    Relay Operation

    Cause of Failure

    Other (See Comments)

    Comments

    B phase (center) failure - could have been the winding insulation (most likely)

    and/or the B phase HV bushing.

    Two-Winding Transformer - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43889 2/4/2004 8/16/2004

    Manufacturer Model Number KV Mfgr Year  

    General Electric GE 12/16/20 @55degC 51-100 kV 1981

    Method of Detection

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    Power Factor, TCG

    Cause of Failure

    Winding

    Comments

    Two-Winding Transformer - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43895 7/2/2004 9/2/2004 5230132810442451.jpg

    Manufacturer Model Number KV Mfgr Year  

    General Electric D

    Method of Detection

    Exciting Current

    Cause of Failure

    Through-Fault

    Comments

    This unit has X1-X0 winding damage that showed up in TTR and excitation tests.

    INTERNAL INSPECTION RESULTS

    The coil structure that contains the H1-H3/X1-XO windings shows subtle evidence

    that movement occurred in the structure. There are spacers in multiple areas of

    the winding that have shifted out of their normal position. The LV leads that exit

    the coil structure had ripped the cloth that originally tied some bracing blocks

    to the leads. On one location at the bottom of the coil structure the blocking

    was out of alignment. No tipping of the HV conductors or core damage could be observed.

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    Two-Winding Transformer - Failure at TestIncident # Incident Date Report Date Photo File Name

    43897 8/24/2004 9/9/2004

    Manufacturer Model Number KV Mfgr Year  

    Westinghouse SL 1984

    Method of Detection

    Partial Discharge

    Cause of Failure

    Winding

    Comments

    Two-Winding Transformer - In-Service FailureIncident # Incident Date Report Date Photo File Name

    43896 8/30/2004 9/9/2004Manufacturer Model Number KV Mfgr Year  

     ASEA-Brown Boveri SL 1997

    Method of Detection

    Relay Operation

    Cause of Failure

    Winding

    Comments