safety investigation report - mtip.gov.mt repository/msiu documents... · out the periodical survey...
TRANSCRIPT
MV Hellenic Sea 201204/018 1
Marine Safety Investigation Unit
MV Hellenic Sea
SAFETY INVESTIGATION REPORT
201204/018 REPORT NO.: 07/2013 April 2013
MV Hellenic Sea Serious injuries to five crew members
following a boiler explosion
In the port of Inchon
26 April 2012
SUMMARY
The vessel arrived alongside at
Incheon on 24 April 2012. Cargo
discharge operations commenced
at 0840 on the same day.
At the request of the managers, a
surveyor from the vessel‟s
classification society attended on
board on 25 April in order to carry
out the periodical survey on the
auxiliary oil fired and exhaust gas
boilers.
Following the survey, the class
surveyor issued a list of pending
items to be completed by 27 April
2012. These included the
adjustment of the safety valves to
an opening pressure of 7.5 bar.
The repairs were completed on 26
April and the boiler started.
At approximately 2025, when the
steam drum pressure on the
pressure gauge was reported to
read approximately 1.60 bar, the
boiler steam drum collapsed.
The escaping drum contents
seriously injured some of the
engine-room personnel, who
were testing the boiler.
The safety investigation
concluded that although the
safety valves opened at 7.2 bar,
the engine-room personnel
testing the boiler tightened them
further, wrongly basing their
decision on the readings of the
pressure gauge.
MSIU has issued one
recommendation to the mangers,
aimed to address risk assessment.
The Merchant Shipping (Accident and Incident Safety Investigation) Regulations, 2011 prescribe that the sole objective of marine safety investigations carried out in accordance with the regulations, including analysis, conclusions, and recommendations, which either result from them or are part of the process thereof, shall be the prevention of future marine accidents and incidents through the ascertainment of causes, contributing factors and circumstances.
Moreover, it is not the purpose of marine safety investigations carried out in accordance with these regulations to apportion blame or determine civil and criminal liabilities. NOTE
This report is not written with litigation in mind and pursuant to Regulation 13(7) of the Merchant Shipping (Accident and Incident Safety Investigation) Regulations, 2011, shall be inadmissible in any judicial proceedings whose purpose or one of whose purposes is to attribute or apportion liability or blame, unless, under prescribed conditions, a Court determines otherwise.
The report may therefore be misleading if used for purposes other than the promulgation of safety lessons.
© Copyright TM, 2013
This document/publication (excluding the logos) may be re-used free of charge in any format or medium for education purposes. It may be only re-used accurately and not in a misleading context. The material must be acknowledged as TM copyright. The document/publication shall be cited and properly referenced. Where the MSIU would have identified any third party copyright, permission must be obtained from the copyright holders concerned.
MV Hellenic Sea 201204/018 2
FACTUAL INFORMATION
Vessel
Hellenic Sea is a bulk carrier built in 1991 at
Jiangnan Shipyard, Shanghai, China. The ship
has an overall length of
225.00 m, a beam of 32.20 m, and a depth of
18.00 m. Her deadweight of
65,433.70 mt corresponded to a summer draft
of about 13.13 m.
Propulsive power is provided by one HD
MAN B&W 5L70MCE low speed diesel
engine, delivering 9451 kW at 100 rpm. Low
pressure steam is supplied by an oil-fired
boiler type Gadelius / Sunrod CPDB-15 and an
exhaust gas boiler type Aalborg AQ-2. The
vessel had a valid UMS notification
At the time of the accident, Hellenic Sea was
registered in Malta and classed with Bureau
Veritas1. It was owned by Patmos Shipping
Co. Ltd., operated by Mantinia Shipping Co.
Ltd., and managed by Hellenic Ship
Management Corporation.
The Injured Crew
The ship had a crew of 27, comprising 26
Filipino and the master of Greek nationality.
All the crew members were appropriately
qualified to hold their positions on board. The
vessel‟s manning was in accordance with the
Minimum Safe Manning Certificate.
The chief engineer had joined the vessel at
Port Said, Egypt on 23 February 2012. He had
been at sea for about 10 years and had served
as a chief engineer for just over four years. He
had already served for six months as a chief
engineer on another vessel under the
management of the company.
The second engineer had joined the vessel in
Singapore on 14 April 2012. He had been at
sea for about 15 years and had served as a
second engineer for about 5.5 years. This was
1 On owners‟ request, the vessel‟s Registry was closed
on 23 August 2012 in terms of
Article 28(1) of the Merchant Shipping Act.
the second engineer‟s first contract on a vessel
under the management of the company.
The third engineer had joined the vessel in
Jeddah, Saudi Arabia on 07 February 2012.
He had been at sea for about 13 years and had
served as a third engineer for about 7.5 years.
This was not the first contract for the third
engineer on a vessel under the management of
the company, having also served for about 19
months in this rank with them.
The fourth engineer had joined the vessel in
Singapore together with the second engineer.
He had been at sea for about 9 years and had
served as a fourth engineer for about 2.5 years.
This was the second engineer‟s first contract
with the company.
The oiler had joined the vessel in Singapore
with the second and fourth engineers. He had
been at sea for about 12 years in this rank.
This was not the first contract for the oiler
with other vessels under the same
management, as he had already served on
vessels under the same management for about
14 months.
The Auxiliary Oil-fired Boiler
Small in size and light in weight, the boiler is
designed to be suitable for use as a marine
boiler.
The Sunrod boiler (Figure 1) has pin tubes
with extended heating surfaces and is
considered as a hybrid between fire tube
boilers and water tube boilers.
MV Hellenic Sea 201204/018 3
Figure 1: Sunrod boiler Adopted from: www.aalborgindutries.com
The vertical welded cylindrical body consists
of a furnace and a convection part integrated
with the drum. The furnace consists of a gas
tight membrane wall from which the flue gases
pass through the pin tube elements to the
smoke-box on the top of the boiler. A number
of downcomer tubes connecting the drum to
the ring header ensure a good natural
circulation at all loads through the furnace
tubes (Figure 2).
The boiler is side-fired, which makes the
boiler very easy to ventilate and gives an
operation and maintenance friendly location of
the burner and its controls. The incoming
system water is mixed into the boiler drum by
means of a spreader with nozzles. The hot
water generation is practically instant. The
response from load variation is very fast.
Figure 2: Water and steam flow diagram
The boiler can be inspected on the water side
through the manhole in the pressure vessel and
through the hand holes in the ring header. On
the gas side, the boiler can be inspected from
the flue gas box at the top of the boiler and
from the furnace.
Calibration of Engine-room’s Pressure and
Temperature Gauges
The verification of boiler pressure gauges was
mandatory. It is a class requirement that in
those circumstances where the calibration of
the gauge could not be readily verified, a
written statement had to be obtained from the
master/chief engineer, confirming that the
gauges had been calibrated. Another option
was to have a second gauge for the verification
of the primary gauge.
Documentary evidence indicated that the
vessel‟s pressure and temperature gauges had
last been calibrated (by a pressure gauge
calibration instrument available on board) on
19 March 2012, i.e. about five weeks prior to
the accident happened. This was within the
time frame stipulated in the company‟s safety
management procedures. Spare gauges were
MV Hellenic Sea 201204/018 4
also available on board. The calibration of the
instruments was included in Chapter VII –
Maintenance Manual, Chapter 02, Procedure 4
of the Company‟s safety management system
manual.
Environment
The wind was calm and the sea state was calm
glassy inside the port area. The light intensity
in the engine-room was adequate and not
considered to be contributory to the accident.
NARRATIVE2
Hellenic Sea departed from the port of
Yuzhny, Ukraine on 23 March 2012 at 0400
bound for Incheon, Republic of Korea,
carrying corn in bulk. The vessel arrived at
Incheon on 22 April at 2200 and berthed
alongside berth no. 51 on 24 April. Until then,
the voyage was uneventful. Cargo discharge
operations commenced at 0840 on the same
day.
At the request of the managers, a surveyor
from the vessel‟s classification society
attended on board on 25 April in order to carry
out the periodical survey on the auxiliary oil-
fired and exhaust gas boilers. The periodic
survey was due on 05 May 2012.
As part of the survey, the safety valves on the
oil-fired boiler were tested in the presence of
the attending class surveyor and both were
reported to have opened at 7.2 bar. Following
the survey, the class surveyor issued a list of
pending items to be rectified by 27 April 2012.
The pending items included (but were not
limited to) the rectification of water leaks on
the water level gauge, leaks on various valves
and piping and the adjustment of the safety
valves to an opening pressure of 7.5 bar.
2 Unless otherwise stated time is local (LT).
The repairs on the boiler were carried out by
the third engineer, who was in charge of the
boiler operation and related maintenance. The
third engineer was assisted by the second
engineer. The repairs were completed on 26
April at approximately 2015.
The oil-fired boiler was prepared for start-up
as soon as the repairs were completed. The
chief engineer, second, third and fourth
engineers were monitoring the process. One
of the oilers was also in close proximity,
cleaning in way of the boiler furnace. The
steam pressure on the boiler pressure gauge
prior to the starting was reported to be about
1.3 bar.
The third engineer carried out an initial
ignition test on the boiler burner unit under
manual control and subsequently started the
boiler on the automatic control mode. The
third engineer reported that the burner starting
sequence, including the purging of the boiler
furnace, was completed without any problems.
He also reported that the burner flame was
checked repeatedly through the sight glass and
no abnormalities were observed.
The boiler mountings and piping, which had
just been repaired, were also inspected for any
visible leaks. No leaks were reported.
Tightening of the safety valves was apparently
carried by the engine-room personnel during
the verification of the auxiliary boiler‟s
operation.
At approximately 2025, when the steam drum
pressure was reported to be 1.60 bar, the boiler
steam drum collapsed, releasing its contents in
the surrounding area within the engine-room
and seriously injuring all the engine-room
personnel around the boiler. The third
engineer managed to leave the site and raise
the initial alarm.
The master instructed the chief mate and other
crew members to administer first aid treatment
to the injured crew members and secure the
area. At the same time, the third mate
MV Hellenic Sea 201204/018 5
contacted the local authorities and reported the
accident.
At 2050, an ambulance arrived and transferred
the second, third and fourth engineers and the
oiler to the local hospital. In the meantime,
the master inspected the engine-room and
verified that the affected area was secured
from potential fire and pollution threats.
It was concluded that the engine-room could
be safely accessed. In view of the number of
injured crew members, the electrician and
remaining engine-room crew members
assumed the responsibility for the engine-room
watches.
At 2115, the chief engineer was also landed
ashore and transferred to the hospital to
receive treatment for minor injuries. He
returned on board on 28 April. The second,
third and fourth engineers remained in hospital
to receive treatment for burn injuries.
Boiler Damage
The boiler (Figure 3) sustained considerable
damage.
Figure 3: Boiler condition after the accident
An inspection of the boiler revealed that the
boiler furnace top plating had collapsed into
the furnace. The damage was attributed to an
overpressure condition inside the steam drum
(Figure 4).
Figure 4: Boiler furnace roof after it collapsed into
the furnace as a result of an overpressure condition
The steam generating tubes (Figures 5 and 6),
furnace supports, and burner guide ring
(Figures 7) had also sustained severe damage.
Figure 5: Steam generating tubes and partly
detached furnace roof
Figure 6: Damaged steam generating tube detail
MV Hellenic Sea 201204/018 6
Figure 7: Damaged burner guide ring
As a result of the explosion, the burner
assembly was found about 20 m away from the
boiler (Figure 8).
Figure 8: Damaged burner assembly
A section of the exhaust uptake and expansion
bellows mounted between the flue gas box and
exhaust ducting had been dislodged, damaging
a nearby steel ladder (Figures 9 and 10).
Figure 9: Damaged exhaust uptake and expansion
bellows
Figure 10: Damaged ladder
ANALYSIS
Aim
The purpose of a marine safety investigation is
to determine the circumstances and safety
factors of the accident as a basis for making
recommendations, to prevent further marine
casualties or incidents from occurring in the
future.
The Source of the Boiler Damage
On the basis of the available evidence, the
safety investigation excluded the possibility of
an explosion inside the furnace. The boiler
was started in accordance with the
manufacturer‟s instructions and established
safety management system procedures.
MV Hellenic Sea 201204/018 7
The chief and third engineers reported that the
boiler start sequence, including the purging of
the furnace, was carried out without any
issues. The flame was also monitored and
observed to be healthy whilst the burner was in
operation. It was therefore evident that the
occurrence had initiated from the water side.
De-activated Defences
During the examination of the damaged boiler,
it was noticed that a steam valve, designated
OV15, and mounted on top of the boiler, was
found closed (Figure 11). The steam valve in
question supplied steam to the boiler pressure
gauge.
Furthermore, valve OV15 supplied steam both
to the pressure transmitter which controlled the
starting and stopping of the burner unit, and to
pressure switches, which activate the high and
low pressure alarms and the high pressure
boiler shutdown.
Figure 11: Part of the water feed and steam system
showing steam valve OV 15
The steam valve was closed prior to the
commencement of the repairs on the boiler on
26 April. Following the completion of the
repairs and prior to the boiler start-up, the
engine-room personnel did not open the steam
valve OV15.
When the boiler was started on 26 April at
about 2025, the boiler pressure gauge was
showing the residual pressure in the length of
pipe between the closed steam valve and the
pressure gauge. The actual pressure in the
boiler after the start-up was higher than that
shown on the pressure gauge. The pressure
transmitter and pressure switches, isolated
from the actual conditions inside the steam
drum, failed to stop the burner and activate
both the alarms and other fitted safety
defences.
Testing of the Safety Valves
It was established that following the survey,
the engineers had adjusted the safety valves
with the intention to test their opening
pressure.
The engineers started the boiler with no
indication of the working pressure (given that
the pressure gauge was isolated from the
system). Unaware of this, when the safety
valves opened they concluded that the opening
pressure was about 1.60 bar, which was the
pressure reading on the pressure gauge. In
fact, the valves had operated at a pressure of
7.2 bar (which was the opening pressure
recorded in the presence of the class surveyor
on the previous day).
It was evident that the engine-room personnel
perceived that the opening pressure of the
safety valves was set far too low and therefore
their intention was to rectify the situation by
tightening the safety valves even further.
Evidence suggested that this procedure was
repetitive, given that each time the safety
valves opened, the pressure on the gauge read
1.60 bar.
The boiler burner continued to supply
uninterrupted heat until the boiler working
pressure of 8.0 bar was exceeded. As a result
of the excessive tightening, the safety valves
MV Hellenic Sea 201204/018 8
failed to open and eventually the pressure
inside the boiler exceeded the design pressure,
resulting in the implosion of the furnace and
the release of the boiler contents and steam
into the engine-room.
The tightening procedure did not reflect
industry established procedures. It is the norm
that safety valves of oil-fired and exhaust gas
boilers are adjusted in the presence of a
classification society surveyor. Moreover, the
set pressure should not exceed the working
pressure of the boiler3.
It is also the norm that in the case where there
are two safety valves fitted, one of the safety
valves is to be gagged (by means of a gag),
whilst the other safety valve is tested. On
completion, the procedure is then reversed so
that in turn, all valves would have been tested.
There is no evidence to show that this was the
procedure followed on board.
Safety Management System and Risk
Assessment
Boiler maintenance and inspection was
addressed in Volume VII, Chapter 1 of the
company‟s safety management system
(SMS)4. The SMS manual made reference to
periodic inspections of the boiler‟s fire and
water sides to ensure that they were
maintained clean and free from corrosion, and
ensuring that the intactness of the brickwork
and the tightness of the boiler casings was
maintained.
Reference was made to specific parts of the
boiler, including the brickwork, boiler furnace
and gas spaces, external fittings and the super
heaters. Whilst there was no cross-reference
to any specific guidelines or procedures on
3 It is not being stated in any way that the engine-
room personnel were negligent. The status of the
system was such that that it did not allow the engine-
room personnel to deduce its actual status. This will
be further discussed in the following sections of the
safety investigation report.
4 Procedure 08.7: E/R Equipment Maintenance
Guidelines.
how these periodical inspections had to be
carried out, the procedure made no reference
to the testing procedure of the boiler‟s safety
valves.
Despite the SMS in place (one of its scopes is
to avoid accidents similar to this one), the risks
materialised into an accident. It is the view of
the MSIU that the problem was not at policy
level but at the middle level of the system.
The middle level of the SMS is the level where
general safety policy objectives are translated
into maintenance concepts, planning and
procedures to achieve improved safety. The
translation process is the responsibility of the
senior management. The lack of operational
procedures (including a detailed risk
assessment) for the testing and adjustment of
the safety valves was indicative of a problem
in the translation process.
The accident dynamics suggested that the
policy level was not represented by the
operational realisation of the system. Safety
management relates to the actual practices
(associated with remaining safe) and this is
where a formal procedure was missing and not
highlighting potential job safety related issues.
In this particular case, i.e. work on the boiler
safety valves, a specific company procedure
was lacking, and when the operations did not
follow the rules of logic and unforeseen risk
materialised, the crew members became
unsafely exposed to the residual hazards of the
system.
Risk Assessment and Situation Awareness
A Risk Assessment Analysis Form was filled
in before the repair job was initiated. The
Analysis Form only made reference to the
sight glass. The existing control measures
seemed very shallow, i.e. not addressing the
details of the task. For instance, one of the
identified control measures was “before
performing the job, discuss the potential
hazard.” However, there was no reference as
MV Hellenic Sea 201204/018 9
to the actual potential hazards identified during
the pre-job discussion.
The Form also required the inclusion of a
detailed hypothetical scenario as part of the
hazard/incident identification (related to the
task to be performed). Even in this area, it did
not transpire that the hazards were correctly
identified – the only entry (hazard scenario)
being “personnel injury and fire.”
The aim of a risk assessment exercise is to
qualify whether or not the status of any system
is acceptable and to help determine what
changes are necessary to make it acceptable.
Such an exercise would have not only
provided an estimate of the size of risk, but it
should have also enabled a comparison of the
risk level with some given criteria and serve as
a platform for a professional judgement to be
made in determining what system
improvements are needed to increase safety.
Maintenance activities cause deviations during
normal operations. Thus, whilst maintenance
increases component reliability and safety,
accidents often occur during maintenance.
From the perspective of situation awareness,
risk assessment is crucial. Risk assessment is
a process (which depends on, inter alia,
perception), that will generate a person‟s
knowledge of the system or situation
awareness even during maintenance activities.
The link between risk assessment and situation
awareness is that the former is vital to pave the
way for a compatible representation of people
and systems i.e. a stage when the awareness of
system status in the minds of the crew
members becomes a true reflection of the
actual and real status of the system.
Incompatible representations (either on the
crew member‟s side or the boiler‟s status)
would definitely mean potential problems. On
board Hellenic Sea, the information exchanges
were hampered by the closed valve (which
compromised the operation of the safety
defences, the boiler itself, and the crew
members‟ potential to understand the system
status) and a shallow risk assessment –
severely compromising the information flow
between system components that included the
crew members.
What actually happened prior and during the
unfolding of the events was that the crew
members were neither able to comprehend the
system status nor project an accurate future
status. This phenomenon was so crucial that
the crew members did not perceive any
problem (or suspected anything) when several
minutes had elapsed and the steam pressure on
the gauge had remained almost constant at
about 1.6 bar.
Memory and Situation Awareness
A (memory) failure to carry out a necessary
check can be caused by some local distraction.
Distractions may lead to „premature exits‟ i.e.
a job is terminated before all the actions are
complete – especially if it is the end of a
routine task.
It is expected that tasks on board may be
subject to frequent interruptions, and the work
on the boiler was not an exception.
Irrespective of their nature, all interruptions
may raise stress levels and increase the
likelihood of memory lapse – omission being
the most likely one.
The ability to maintain information in the
working memory is particularly important,
especially when engaged in safety critical
tasks5. For instance, working memory is
utilised when going through a series of steps
within a process.
If someone is distracted or interrupted while
focussing attention to hold this information,
they would probably forget steps s/he may
have completed. Literature suggests that any
information contained in the distraction phase,
erases the material that the working memory
store would have been holding.
5 Double checking the status of all the valves before
start-up is a safety issue where memory would have
been critical.
MV Hellenic Sea 201204/018 10
Attention is a cognitive system that has a
limited capacity and depends on, inter alia,
memory. Thus, attention and working
memory are closely tied together. It is for this
particular reason that workload is considered
to be very important to attention and working
memory.
Whilst sequencing tasks (even by the use of
checklists or a list of items whose status had
been altered before the initiation of the
maintenance task), is an effective way to
address workload, interruptions may be
problematic – especially when these lead to
the loss of memory contents. This may create
a situation where system status is
(inadvertently) not reinstated.
It is not excluded that the time window during
which the maintenance was carried out and the
unavailability of a checklist / memo had
contributed to the missing of the last stages of
the task i.e. the reinstatement of the system
defences prior to the start-up of the boiler.
CONCLUSIONS
1. The pressure inside the steam drum
exceeded the design pressure, resulting
in the implosion of the furnace and the
release of boiler contents and steam into
the engine-room.
2. The injuries sustained by the crew
members were a result of the collapse of
the oil-fired boiler steam drum following
a pressure build-up, which exceeded the
design pressure.
3. During the examination of the damaged
boiler, it was noticed that a steam valve,
designated OV15, and mounted on top of
the boiler, was found closed. This status
had effectively de-activated all the
boiler‟s safety defences.
4. The engineers altered the oil-fired boiler
safety valves settings by adopting a
procedure which did not reflect the
industry‟s norm.
5. The safety valves were tightened
excessively and consequently failed to
open to relieve the pressure.
6. The SMS manual lacked an operational
procedure (including a detailed risk
assessment) for the testing and
adjustment of the boiler safety valves.
7. As a result of the shallow risk
assessment made on board, the crew
members were neither able to
comprehend the system status nor
accurately project its future status.
8. It is not excluded that the crew members
had a memory lapse as a result of which,
the system status was not reinstated, and
the steam valve remained closed.
SAFETY ACTIONS TAKEN DURING
THE COURSE OF THE SAFETY
INVESTIGATION6
The company has taken the following safety
actions:
1. A Safety Office Meeting was held with
the participation of the Managing
Director, Fleet Divisions Manager, DPA
and all Department Managers in order to
discuss and assess the accident, identify
the root causes and contributing factors,
and decide upon the corrective and
preventive actions.
2. The Company advised the boiler
manufacturer of the company‟s findings
in order to share the lesson learned.
3. A Safety Alert has been forwarded to all
managed vessels describing the accident
and requesting all chief engineers to
thoroughly inspect and ensure the proper
operation of the auxiliary and the
exhaust gas boilers, and report back to
the Company. It was also requested that
the Safety Alert is discussed during the
on board safety meetings and relevant
6 Safety actions and recommendations should not
create a presumption of blame and/or liability.
MV Hellenic Sea 201204/018 11
crew members revert with suggestions
regarding additional preventive controls.
4. A full review of the Company‟s PMS
and checklists related to boiler and
associates, had been conducted. A note
was inserted in the PMS highlighting
that before starting the boiler, the
shipboard personnel should ensure that
the operation is conducted according to
manufacturer‟s instructions.
5. A risk assessment has been conducted
with the hypothetical scenario of the
boiler‟s failure in auto and manual
modes.
6. The company‟s auditors and
superintendents were instructed to place
special/particular attention during their
regular visits on board to all tests /
checks conducted prior to auxiliary
boilers‟ operation.
7. The company contacted the boiler‟s
maker in order to establish additional
ways / means for the early identification
of any malfunction of the auxiliary
boiler.
8. Although hours of work and sleep were
not identified as a contributing factor to
this accident, software licenses were
purchased for all ships to monitor the
crew members‟ hours of work and rest
more effectively.
RECOMMENDATIONS
Hellenic Ship Management Corp. is
recommended to:
07/2013_R1 Adopt a training programme for
relevant crew members in order to provide
the necessary tools and skills to
objectively identify hazards and
understand risk and its assessment.
MV Hellenic Sea 201204/018 12
SHIP PARTICULARS
Vessel Name: Hellenic Sea
Flag: Malta
Classification Society: Bureau Veritas
IMO Number: 8905828
Type: Bulk Carrier
Registered Owner: Patmos Shipping Co. Ltd.
Managers: Hellenic Shipmanagement Corp.
Construction: Steel
Length Overall: 225.0 m
Registered Length: 215.65 m
Gross Tonnage: 36448
Minimum Safe Manning: 16
Authorised Cargo: Solid Cargo in Bulk
VOYAGE PARTICULARS
Port of Departure: Yuzhny, Ukraine
Port of Arrival: Incheon, Republic of Korea
Type of Voyage: International
Cargo Information: Corn in bulk
Manning: 23
MARINE OCCURRENCE INFORMATION
Date and Time: 26 April 2012 at 20:25 (LT)
Classification of Occurrence: Serious Marine Casualty
Location of occurrence: Port of Incheon
Place on board Engine-room
Injuries / fatalities: Five crew members injured
Damage/environmental impact: Extensive damage to the boiler and minor damage to the engine-room
Ship Operation: Normal Service – Alongside/Moored
Voyage Segment: Alongside
External & Internal Environment: Calm wind and calm glassy sea. Artificial lighting in the engine-room.
Persons on board: 27