tata steel bsl limited, khopoli. mr. brajesh nahar (vp ...€¦ · © confederation of indian...
TRANSCRIPT
© Confederation of Indian Industry
TATA Steel BSL Limited, Khopoli.
Mr. Brajesh Nahar (VP-Operation) Mr. Hemendra Tiwari (DGM) Mr. Vijay Patil (Jr. Manager)
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1.1 Company Profile
TATA Steel BSL Limited, Khopoli
Plants & Products
History
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1.2 Company Process
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2.1 Energy Consumption Overview
4
9.29.8 9.3 9.5 9.9
FY16 FY17 FY18 FY19 FY20
Production in Lakhs tonne
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2.2 Energy Consumption Overview
5
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2.3 Energy Consumption Overview
6
Electrical Energy mtoe, 13082, 44%
Thermal Energy in
mtoe, 16870, 56%
Electrical & Thermal Energy Share
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3.1 Sp. Energy Consumption (FY16-20)
173 175184
164155
FY16 FY17 FY18 FY19 FY20
Electrical SEC in KWh/tonne of Production
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3.2 Sp. Energy Consumption (FY16-20)
0.180 0.175 0.1720.162
0.172
FY16 FY17 FY18 FY19 FY20
Thermal SEC in million Kcal/tonne of Production
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3.3 Sp. Energy Consumption (FY16-20)
0.0329 0.0326 0.0330
0.0303 0.0306
FY16 FY17 FY18 FY19 FY20
Total SEC in mtoe/tonne of ProductionSEC Increased due to COVID Lockdown in
March
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3.4 Sp. Energy Consumption (FY16-20)
Unforeseen market
condition
SEC Increased due to COVID Lockdown in
March
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4.1 National Benchmarking
184
215
164 162161 159
Electrical SEC in KWh/tonne Thermal SEC in Mcal/tonne
JSW, Tarapur TSBSL, Khopoli Target Plan
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11.1 SEC Target Long Term
0.03670.0345
0.0303 0.0300 0.0298 0.0296 0.0294
Baseline FY19 Target FY19Achieved
FY20 FY21 FY22 FY23
Five Year Target Plan in mtoe/tonne
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4.2 Major Encon project planned in FY 2020-21
SlNo
Project Details Investments Lakh Rs
Savings Lakh Rs
Payback
1 To replace 7 No. of existing CCL blower with TurboMax Blower.
70 44 19
2 To install thermostatic control with VFD, based on return temperature of water from process tocooling tower.
30 15 23
3 To install Excess Air Control system based on O2 monitoring at Stack level for 8 TPH Boiler.
15 33 5
4 To modify Heat recovery System of H & T Furnace. 10 15 8
5 Replacement of Shed lights with LED Light in plant 98 88 13
6 Furnace tuning close to psychometric ratio and system modification (GP-1&2)
16 7 28
7 Modification of salt bath tank of color tempering line (H&T NCRM)
5 25 2
8 Install VFD Drive for 4 no's of brush roll motor (wider) in placed of DOL Starter
6 4 18
9 Estimate use of air dryer motor and use of flue gases hot air from incinerator for drying material (sheet in wider)
_ _ 4 _ _
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5.1 Energy Saving projects implemented
Year No of Proposals Investments in Lakhs Savings in Lakhs
2017-18 15 223 291
2018-19 14 131 153
2019-2020 9 50 148
223
131
50
250
291
153 148
235
FY18 FY19 FY20 FY21 Plan
Investments in Lakhs Savings in Lakhs
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5.2 Energy Saving projects implemented FY18
SlNo
Project DetailsInvestments
Lakh RsSavings Lakh Rs
Payback in Months
1 VFD Installation and Speed Optimization. 2.88 28.60 2
2Increased Furnace efficiency by optimizing psychometric ratio and gap of entry seal reduced (GP02 Prod).
13.00 74.48 NIL
3Construction / Heater mode Modification at Color Tempering Line (H&T dept.).
3.41 0.30 NA
4Improvement of specific power consumption of air compressor (centac) no.1 & no.3 by replacing old air end (Utility)
104.00 120.01 10
51200 no's of 400 Watt Shed lights replaced with 150 Watt LED lights
98.10 64.80 18
6Submersible pump installed in place of commercial cent. pump in Tube mill
0.00 6.65 NIL
Total 222.58 290.80
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5.3 Energy Saving projects implemented FY19
SlNo
Project DetailsInvestments
Lakh RsSavings Lakh Rs
Payback (months)
1Temperature of PMP reduced from 640 C to 630 C during
idle condition in GP-2 (Production).0 15.62 NIL
2Enhance the effectiveness of HAG to reduce the use of HF
furnace at chromic cycle in GP-2 (Production).0 19.00 NIL
3Install 260TR 4th no. chiller with new energy efficient
chiller (Utility).87.97 48.96 22
4 VFD Installation and process parameter optimisation. 3.30 15.99 2
5Replacement of conventional light with LED light & control
through relay logic.38.28 37.64 12
6 Pumping System Modification and Design. 1.40 15.99 1
Total 130.95 153.2
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5.4 Energy Saving projects implemented FY20
SlNo
Project Details Investments Lakh Rs
Savings Lakh Rs
Payback (months)
1Efficiency improvement of PSA-3 (Nitrogen Plant) through modification in the existing system (Utility).
40 104.87 5
2Installed 2 no. of Air Amplifier at forming section & reduced 25% air consumption out of initial usage (API Electrical).
0.16 0.73 3
3Power consumption reduced by covering GL pot during line stand by (Wider Electrical).
0.00 24.74 NIL
4Installed 3 no. shut off valve and programmed it with line run command to air consumption (API Electrical).
0.07 0.92 1
5Replacement of conventional light with LED light & control through relay logic.
8.74 11.51 9
6Submersible pump installed in place of commercial cent. pump in Tube mill (Tube Mill-4th shed).
0.70 4.02 2
7CCL Steering Unit HPP auto stop after 5 min. of line stop (Wider Electrical).
0 1.50 NIL
Total 49.67 148.29
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6.1 Innovative Projects implemented
Project Title :- Modification of Existing PSA-3 Plant (Nitrogen plant ) to improve the efficiency of Plant.
Problem Statement :- The PSA-3 Plant was not running on full capacity and so the efficiency was down whereas the other inputs (compressed air, power,NH3 etc.) was same as per design.
Action Taken :- 1. We had modified the design of PSA-3's both towers and taken the improvised process of nitrogen generation cycles of towers. Also replace the accutor valve ( Plug type to Angle type) to prevent leakage and passing. 2. We changed the quantity as well as quality of CMS ( carbon molecular sieves) and alumina.
Before Modification
After Modification
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6.2 Innovative Projects implemented
Project Title :- Enhance the effectiveness of HAG to reduce the use of HF furnace at chromic cycle in GP-2 (Production).
Problem Statement :- 1. HAG system not reaching the temperature of the sheet as per the process requirement and due to this additional heat is required by means of Induction heating.
Action Taken :- Overhauling and maintenance done of HAG system and increased its parameter setting. Its temperature accomplished the desired process requirement and eliminated the additional heating of Induction heater.
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9.1 GHG Inventorisation
0.161
0.164
0.161
0.158
FY18 FY19 FY20 Target FY21
CO2 Emission in tonne per tonne of Production
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9.2 GHG Inventorisation
Sr. No.
Carbon Emission Reduction Action Plan Co2 Emission (Ton/Year)
1 Waste heat recovery boiler/Hot water generator at exhaust of CCL thermal oxidizer.
- -
2 Solar PV plant of 10MWatt at Roof-top. 11480
3 Identify air usage at different operating area & Reduce air consumption through air amplifier units.
1919
4 To replace 7 No. of existing CCL blower with Turbo-Max Blower. 446
5 To install thermostatic control with VFD, based on return temperature of water from process to cooling tower.
156
6 To install Excess Air Control system based on O2 monitoring at Stack level for 8 TPH Boiler.
254
7 Colour Tempering Line Salt Bath Heaters. Controlled by ThyristorControl System with PID Controller & Line Stop System. (NCRM)
266
8 Strip Grinding Lines- Coolant Systems Motor Controlled By VFD With Line stopes & Flow Transmitter. (NCRM).
131
Total 14652
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10.1 Teamwork, Employee Involvement & Monitoring
Training and Energy Awareness SessionsEnergy walk
Prize Distribution
Inauguration
Painting and drawing competition Quiz competition
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10.2 Teamwork, Employee Involvement & Monitoring
Tree Plantation in Plant & TSBSL Township
Environment Stewardship Training and Awareness Prize Distribution
Environment Day walk
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11.1 Implementation of ISO 50001
EnMS ISO50001
ISO 50001
Implemented in
year 2015
04 Certified
Lead Auditors
06 BEE Certified Energy
Auditors/Managers
24 Internal Auditors
Total 879 Employees covered in
Energy Awareness
Training.
Conducting Quarterly
Review meeting on
energy Conservation
Practices .
Energy Week
Celebration
Presentation for energy
conservation & current
scenario given from MEDA
person
Awareness session for employees on Energy
Conservation opportunity & for ladies on energy conservation in
household appliances
Painting Competition,
Essay Competition & Departmental
Energy Conservation Presentation
Training and awareness on
Energy Conservation Techniques by PAT
Consultant Mr. Puneet Hegde.
Pick and win Contest on energy
conservation, global warming,
environment, renewable energy.
Audit Culture
Base Line
Energy Audit-
Yr.2010
Optional Energy Audit-
Yr.2013
Steam Walk
Through Audit-
Yr.2014
Pump Audit-
Yr.2016
Steam Detailed Audit-Yr.2017
Insulation
Audit-Yr.2017
MEA Audit
Nov.18
Thermal Audit
Jan.2019
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11.2 Monitoring of Energy Performance
0.03020.0259
0.0282 0.0298
0.0336
0.0283 0.0280
0.0378
0.0601
0.02460.0269
0.0309
0.0000
0.0100
0.0200
0.0300
0.0400
0.0500
0.0600
0.0700
Energy Performance (SEC) Monitoring
SEC in mtoe/tonne Target
SEC Increased due to COVID Lockdown in
March
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11.2 Investment of energy saving projects
287
74
223
131
286
242
452
291
153
FY15 FY16 FY17 FY18 FY19
Investment Vs Energy Saving in Lakh Rs.
Investment towards ECM (Rs. in Lakhs)
Total Energy cost Saved (Rs. In Lakhs)
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12.1 Other Innovative technologies Under implementation
27
1
KW
2 - 3
KW
3 - 4
KW+ =
Heat
is taken in fro
m t
he a
mbie
nt
The system pumps heat from a
low temperature reservoir to a
high temperature
Heat Pump Air Amplifier
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12.2 Other Innovative technologies Under implementation
28
Regenerative Thermal Oxidizer
ROT is an extremely efficient
thermal oxidizer that uses number
of ceramic beds, either loose
saddles or honeycomb blocks, to
absorb heat from its exhaust gases.
It than uses this captured heat to
pre-heat the process incoming
process air stream and destroy air
pollutants contained in this air
stream, at temperature ranging
upto 1000°C.
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12.3 Other Innovative technologies Planned
29
Biomass based Green Fuel Briquette Boiler in place of Conventional Fuel fired Boiler.
• Optimum Cost-Effective Steam Price
• Guaranteed Boiler Uptime & Efficiency
• throughout the Product Lifecycle• No investment for boiler plant and• machinery by customer• Significant SPM reduction in
emissions
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12.4 Other Innovative technologies Under implementation
30
HHO mixed Combustion System
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12.4 Other Innovative technologies Under implementation
31
EMS System
Energy Management System (EMS) allows utilities to better visualize, operate, optimize, and maintain transmission and sub transmission networks.
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Reducing Air Pressure by use of Air Amplifier.
Installation Solar PV system of 10 MWp on Roof Top.
HHO Mixed combustion system gives fuel saving are in the range of 20% to 50%.
Replacement of existing thermal oxidizer by energy efficient RTO (Regenerating Thermal Oxidizer).
Use of Heat Pump in Hot water generation process.
Biomass based Green Fuel Briquette Boiler in place of Conventional Fuel fired Boiler.
13.1 Long Term Vision on EE
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Any other relevant information
33
Achievements
"Energy Efficient Unit" award in 20th National Award for Excellence in Energy Management 2019 arranged by CII (Confederation of Indian Industry).
2nd position in National Energy Conservation Award in steel sector (Year 2015-16).
1st Position in 9th state level energy conservation award in steel sector from MEDA (Maharashtra Energy Development Agency) (FY 2012-13).
3rd Position in 8th state level energy conservation award in steel sector from MEDA (Maharashtra Energy Development Agency) (FY 2011-12).
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Mr. Brajesh Nahar ([email protected], )
Mr. Hemendra Tiwari ([email protected],)
Mr. Vijay Patil([email protected], 9503113041)
Thank you