vapor extraction / groundwater extraction (ve/ge) system third … · 2020-06-04 · table 1 - well...
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Washington DC | Nashville TN | Richmond VA | Philadelphia PA | San Diego CA
Vapor Extraction / Groundwater Extraction (VE/GE) System
Third Monthly Update Report
Gasoline Fueling Station – Royal Farms #96 500 Mechanics Valley Road
North East, MD 21901 MDE OCP Case No. 2011-0729-CE
Facility ID No. 13326
AEC Project Number: 05-056RF096
Prepared for: Maryland Department of the Environment
Oil Control Program 1800 Washington Boulevard
Baltimore, Maryland 21230-1719
And
Royal Farms / Two Farms, Inc. Attn: Tom Ruszin
3611 Roland Avenue Baltimore, Maryland 21211
Prepared by: Advantage Environmental Consultants, LLC
8610 Washington Boulevard, Suite 217 Jessup, MD 20794
Phone – (301)-776-0500 Fax – (301)-776-1123
March 6, 2013
Royal Farms #96 Monthly Update Report OCP Case No. 2011-0729-CE AEC Project # 05-056RF096
General Site Information Regulatory Agency: Maryland Department of the Environment Agency Contact: Susan Bull Royal Farms Contact: Tom Ruszin Consultant Contact: Jeff Stein/James Wolf Case Number: OCP Case No. 2011-0729-CE Facility Status: Operating fuel station Facility ID: 13326 Current Case Status: Vapor Extraction/ Groundwater Extraction (VE/GE)
System in operation. Quarterly groundwater sampling. On-site and off-site potable well monitoring.
Area Property Use: See Site Vicinity Map, Site Map and trenching Layout Map (Figures 1, 2 and 3)
Monitoring Wells: MW-1R, MW-2, MW-4 through MW-16, MW-10D, MW-12D, MW-13D, TP-1, TP-2, TP-3, TP-4
VE/GE System Wells: MW-7, RW-1, RW-2, RW-3, RW-4, RW-6, RW-8, RW-9, RW-10, RW-11, RW-12
Potable Wells: CE-94-3354 (site well), CE-88-0994, CE-94-0008, CE-81-0226, hand dug well (no permit), CE-81-0886, CE-94-6569
VE/GE System Performance System Operation Period: 2-8-13 through 3-6-13 Calendar Days: 27 Operating Days: 21 Period Groundwater and Vapor Recovery Cumulative Water Discharge: 1,569,600 gallons Cumulative Vapor Processed: 19,252,800 cubic feet Period Water Discharge: 403,200 gallons Period Vapor Processed: 10,946,880 cubic feet Period Average Water Flow Rate: 13.3 gallons per minute (gpm) Period Average Vapor Flow Rate: 432 cubic feet per minute (cfm) Hydrocarbon Recovery Estimates (Period gallons / Cumulative gallons) System Dissolved Phase Recovery: 0.4 / 2.8 System Vapor Phase Recovery: 57.5 / 179.9 Total Recovery: 57.9 / 182.7 The VE/GE System began operation on December 11, 2012. Since start-up, groundwater drawdown has been observed across the site through gauging of on-site monitoring wells. During gauging events, vacuum gauge readings were also taken to determine vacuum influence of the VE/GE System upon surrounding monitoring wells. Figure 1 in Attachment A illustrates the site vicinity. Figure 2 in Attachment A illustrates the groundwater monitoring well, tank-pit well, recovery well, bedrock monitoring well, and onsite potable drinking water well locations. A scaled depiction of the system layout is included in Figure 3 of Attachment A. Table 1 in Attachment B includes gauging and vacuum influence data obtained through gauging events.
Royal Farms #96 Monthly Update Report OCP Case No. 2011-0729-CE AEC Project # 05-056RF096
System performance has been monitored through readings taken from diagnostic gauges on system equipment. System monitoring worksheets are included in Attachment C. It should be noted that the system was shutdown February 20 through February 25 for quarterly groundwater sampling. Approximately 403,200 gallons of liquid and approximately 10,946,880 cubic feet of air have been processed by the system during this period, removing approximately 362 pounds (or 58 gallons) of volatile organic compounds (VOCs). No liquid phase hydrocarbon (LPH) was recovered during this monitoring period. Table 2 in Attachment B summarizes the hydrocarbon recovery data, and Table 3 in summarizes the hydrocarbon recovery estimates. Figures
Figure 1 Site Vicinity Map Figure 2 Site Features Map Figure 3 Trenching Layout Map Attachments Attachment A Figures Attachment B Tables Attachment C System Monitoring Worksheets
Royal Farms #96 Monthly Update Report OCP Case No. 2011-0729-CE AEC Project # 05-056RF096
Attachment A
Figure 1 - Site Vicinity MapRoyal Farms #96
500 Mechanics Valley RoadNorth East, MDAdvantage Environmental Consultants, LLC
© 2001 DeLorme. Topo USA® 3.0
Zoom Level: 12-7 Datum: WGS84
Scale 1 : 28 125
1" = 2 343 75 ft
0 ¼ ½ ¾ 1
0 ½ 1 1½ 2
mikm
TN
MN
11.7°W
Royal Farms #96 Monthly Update Report OCP Case No. 2011-0729-CE AEC Project # 05-056RF096
Attachment B
Well ID DateDepth to
WaterDepth to
LPHTOC
ElevationWater
ElevationLPH
Elevation
Corrected Water
Elevation
LPH Thickness
CommentsVacuum Pressure
MW-1R 12/10/2012 11.08 ND 94.74 83.66 NA NA NA NA12/11/2012 12.20 ND 94.74 82.54 NA NA NA 0.2012/20/2012 13.77 ND 94.74 80.97 NA NA NA 0.1012/24/2012 13.00 ND 94.74 81.74 NA NA NA 0.051/4/2013 14.00 ND 94.74 80.74 NA NA NA 0.111/8/2013 14.20 ND 94.74 80.54 NA NA NA 0.121/15/2013 13.32 ND 94.74 81.42 NA NA NA 0.621/25/2013 11.89 ND 94.74 82.85 NA NA NA1/29/2013 11.68 ND 94.74 83.06 NA NA NA2/7/2013 12.59 ND 94.74 82.15 NA NA NA2/14/2013 12.64 ND 94.74 82.10 NA NA NA2/27/2013 12.99 ND 94.74 81.75 NA NA NA
MW-2 12/10/2012 12.46 ND 95.86 83.40 NA NA NA NA12/11/2012 13.92 ND 95.86 81.94 NA NA NA 0.0812/20/2012 15.28 ND 95.86 80.58 NA NA NA 0.0412/24/2012 14.49 ND 95.86 81.37 NA NA NA 0.041/4/2013 15.40 ND 95.86 80.46 NA NA NA 0.001/8/2013 15.70 ND 95.86 80.16 NA NA NA 0.001/15/2013 14.73 ND 95.86 81.13 NA NA NA 0.141/25/2013 13.12 ND 95.86 82.74 NA NA NA1/29/2013 12.95 ND 95.86 82.91 NA NA NA2/7/2013 14.03 ND 95.86 81.83 NA NA NA2/14/2013 14.16 ND 95.86 81.70 NA NA NA2/27/2013 14.62 ND 95.86 81.24 NA NA NA
MW-4 12/10/2012 12.95 ND 96.87 83.92 NA NA NA NA12/11/2012 14.46 ND 96.87 82.41 NA NA NA 1.0012/20/2012 17.45 ND 96.87 79.42 NA NA NA 2.9012/24/2012 14.72 ND 96.87 82.15 NA NA NA 1.501/4/2013 16.19 ND 96.87 80.68 NA NA NA 2.901/8/2013 16.32 ND 96.87 80.55 NA NA NA 2.501/15/2013 15.50 ND 96.87 81.37 NA NA NA > 5.01/25/2013 13.77 ND 96.87 83.10 NA NA NA1/29/2013 13.58 ND 96.87 83.29 NA NA NA2/7/2013 14.71 ND 96.87 82.16 NA NA NA 1.602/14/2013 14.89 ND 96.87 81.98 NA NA NA 4.502/27/2013 15.29 ND 96.87 81.58 NA NA NA 4.40
MW-5 12/10/2012 14.42 ND 98.39 83.97 NA NA NA NA12/11/2012 15.93 ND 98.39 82.46 NA NA NA 0.3912/20/2012 15.93 ND 98.39 82.46 NA NA NA 4.7012/24/2012 16.37 ND 98.39 82.02 NA NA NA 0.751/4/2013 17.59 ND 98.39 80.80 NA NA NA 2.001/8/2013 17.74 ND 98.39 80.65 NA NA NA 1.601/15/2013 17.22 ND 98.39 81.17 NA NA NA > 5.01/25/2013 15.20 ND 98.39 83.19 NA NA NA1/29/2013 15.03 ND 98.39 83.36 NA NA NA2/7/2013 16.19 ND 98.39 82.20 NA NA NA 0.752/14/2013 16.32 ND 98.39 82.07 NA NA NA 2.902/27/2013 16.82 ND 98.39 81.57 NA NA NA 2.90
MW-6 12/10/2012 15.01 ND 98.91 83.90 NA NA NA NA12/11/2012 16.24 ND 98.91 82.67 NA NA NA 5.00
Table 1 - Well Gauging SummaryGasoline Fueling Station – Royal Farms No. 96
500 Mechanic Valley Road, North East, Maryland 21901
Table 1 - Well Gauging SummaryGasoline Fueling Station – Royal Farms No. 96
500 Mechanic Valley Road, North East, Maryland 21901
12/20/2012 17.93 ND 98.91 80.98 NA NA NA 6.0012/24/2012 16.55 ND 98.91 82.36 NA NA NA 3.901/4/2013 17.96 ND 98.91 80.95 NA NA NA 7.001/8/2013 18.35 ND 98.91 80.56 NA NA NA 6.501/15/2013 17.02 ND 98.91 81.89 NA NA NA 13.001/25/2013 15.86 ND 98.91 83.05 NA NA NA1/29/2013 15.63 ND 98.91 83.28 NA NA NA2/7/2013 16.70 ND 98.91 82.21 NA NA NA 4.802/14/2013 16.29 ND 98.91 82.62 NA NA NA > 5.02/27/2013 16.68 ND 98.91 82.23 NA NA NA > 5.0
MW-7* 12/10/2012 14.27 ND 97.75 83.48 NA NA NA
MW-8 12/10/2012 14.29 ND 97.81 83.52 NA NA NA NA12/11/2012 16.81 ND 97.81 81.00 NA NA NA 2.0012/20/2012 17.53 ND 97.81 80.28 NA NA NA 2.7012/24/2012 17.00 ND 97.81 80.81 NA NA NA 4.801/4/2013 18.00 ND 97.81 79.81 NA NA NA 0.221/8/2013 18.37 ND 97.81 79.44 NA NA NA 2.701/15/2013 16.98 ND 97.81 80.83 NA NA NA 2.601/25/2013 14.96 ND 97.81 82.85 NA NA NA1/29/2013 14.80 ND 97.81 83.01 NA NA NA2/7/2013 16.30 ND 97.81 81.51 NA NA NA 2.102/14/2013 16.87 ND 97.81 80.94 NA NA NA 0.852/27/2013 17.15 ND 97.81 80.66 NA NA NA 2.40
MW-9 12/10/2012 13.29 ND 96.73 83.44 NA NA NA Mod. Odor NA12/11/2012 14.87 ND 96.73 81.86 NA NA NA Mod. Odor 0.0012/20/2012 16.28 ND 96.73 80.45 NA NA NA Mod. Odor 0.0012/24/2012 15.42 ND 96.73 81.31 NA NA NA Mod. Odor 0.001/4/2013 16.42 ND 96.73 80.31 NA NA NA Slight Odor 0.021/8/2013 16.71 ND 96.73 80.02 NA NA NA Mod. Odor 0.001/15/2013 15.64 ND 96.73 81.09 NA NA NA 0.031/25/2013 13.95 ND 96.73 82.78 NA NA NA Mod. Odor
1/29/2013 13.79 ND 96.73 82.94 NA NA NA Slight Odor
2/7/2013 14.95 ND 96.73 81.78 NA NA NA Slight Odor
2/14/2013 15.12 ND 96.73 81.61 NA NA NA Slight Odor
2/27/2013 15.62 ND 96.73 81.11 NA NA NA Mod. Odor
MW-10 12/10/2012 11.73 ND 94.95 83.22 NA NA NA NA12/11/2012 12.93 ND 94.95 82.02 NA NA NA 0.0312/20/2012 14.25 ND 94.95 80.70 NA NA NA 0.0312/24/2012 16.42 ND 94.95 78.53 NA NA NA 0.001/4/2013 14.31 ND 94.95 80.64 NA NA NA 0.041/8/2013 14.58 ND 94.95 80.37 NA NA NA 0.041/15/2013 13.65 ND 94.95 81.30 NA NA NA 0.041/25/2013 12.23 ND 94.95 82.72 NA NA NA1/29/2013 12.12 ND 94.95 82.83 NA NA NA2/7/2013 13.02 ND 94.95 81.93 NA NA NA2/14/2013 13.05 ND 94.95 81.90 NA NA NA2/27/2013 13.53 ND 94.95 81.42 NA NA NA
MW-11 12/10/2012 15.50 ND 98.69 83.19 NA NA NA NA12/11/2012 17.09 ND 98.69 81.60 NA NA NA 0.0012/20/2012 18.23 ND 98.69 80.46 NA NA NA 0.0012/24/2012 17.44 ND 98.69 81.25 NA NA NA 0.001/4/2013 18.32 ND 98.69 80.37 NA NA NA 0.001/8/2013 18.66 ND 98.69 80.03 NA NA NA 0.00
Depth to Groundwater Pump intake: 16.5 ft.
Table 1 - Well Gauging SummaryGasoline Fueling Station – Royal Farms No. 96
500 Mechanic Valley Road, North East, Maryland 21901
1/15/2013 17.61 ND 98.69 81.08 NA NA NA < 0.01/25/2013 15.98 ND 98.69 82.71 NA NA NA1/29/2013 15.85 ND 98.69 82.84 NA NA NA2/7/2013 16.99 ND 98.69 81.70 NA NA NA2/14/2013 17.09 ND 98.69 81.60 NA NA NA2/27/2013 17.71 ND 98.69 80.98 NA NA NA
MW-12 12/10/2012 14.03 ND 96.75 82.72 NA NA NA NA12/11/2012 14.96 ND 96.75 81.79 NA NA NA 0.0212/20/2012 16.16 ND 96.75 80.59 NA NA NA 0.0312/24/2012 15.35 ND 96.75 81.40 NA NA NA 0.021/4/2013 16.09 ND 96.75 80.66 NA NA NA 0.001/8/2013 16.34 ND 96.75 80.41 NA NA NA 0.001/15/2013 15.53 ND 96.75 81.22 NA NA NA 0.001/25/2013 14.29 ND 96.75 82.46 NA NA NA1/29/2013 14.22 ND 96.75 82.53 NA NA NA2/7/2013 14.92 ND 96.75 81.83 NA NA NA2/14/2013 14.86 ND 96.75 81.89 NA NA NA2/27/2013 15.32 ND 96.75 81.43 NA NA NA
MW-13 12/10/2012 8.35 ND 91.72 83.37 NA NA NA NA12/11/2012 8.81 ND 91.72 82.91 NA NA NA 0.0012/20/2012 9.96 ND 91.72 81.76 NA NA NA 0.0312/24/2012 9.51 ND 91.72 82.21 NA NA NA 0.001/4/2013 10.18 ND 91.72 81.54 NA NA NA 0.031/8/2013 10.32 ND 91.72 81.40 NA NA NA 0.021/15/2013 9.82 ND 91.72 81.90 NA NA NA 0.141/25/2013 8.98 ND 91.72 82.74 NA NA NA1/29/2013 8.86 ND 91.72 82.86 NA NA NA2/7/2013 9.25 ND 91.72 82.47 NA NA NA2/14/2013 9.17 ND 91.72 82.55 NA NA NA2/27/2013 9.32 ND 91.72 82.40 NA NA NA
MW-14 12/10/2012 10.23 ND 94.07 83.84 NA NA NA NA12/11/2012 11.03 ND 94.07 83.04 NA NA NA 0.0012/20/2012 12.49 ND 94.07 81.58 NA NA NA 0.0512/24/2012 11.82 ND 94.07 82.25 NA NA NA 0.001/4/2013 12.73 ND 94.07 81.34 NA NA NA 0.001/8/2013 12.85 ND 94.07 81.22 NA NA NA 0.001/15/2013 12.26 ND 94.07 81.81 NA NA NA < 0.01/25/2013 11.02 ND 94.07 83.05 NA NA NA1/29/2013 10.81 ND 94.07 83.26 NA NA NA2/7/2013 11.51 ND 94.07 82.56 NA NA NA2/14/2013 11.48 ND 94.07 82.59 NA NA NA2/27/2013 11.75 ND 94.07 82.32 NA NA NA
MW-15 12/10/2012 16.36 ND 99.77 83.41 NA NA NA NA12/11/2012 17.56 ND 99.77 82.21 NA NA NA 3.8012/20/2012 19.92 ND 99.77 79.85 NA NA NA 2.4012/24/2012 18.26 ND 99.77 81.51 NA NA NA 1.001/4/2013 19.75 ND 99.77 80.02 NA NA NA 5.501/8/2013 20.08 ND 99.77 79.69 NA NA NA 2.401/15/2013 18.56 ND 99.77 81.21 NA NA NA > 5.01/25/2013 17.11 ND 99.77 82.66 NA NA NA1/29/2013 16.95 ND 99.77 82.82 NA NA NA2/7/2013 18.30 ND 99.77 81.47 NA NA NA 3.102/14/2013 18.03 ND 99.77 81.74 NA NA NA > 5.02/27/2013 18.90 ND 99.77 80.87 NA NA NA > 5.0
Table 1 - Well Gauging SummaryGasoline Fueling Station – Royal Farms No. 96
500 Mechanic Valley Road, North East, Maryland 21901
MW-16 12/10/2012 7.56 ND 98.73 91.17 NA NA NA NA12/11/2012 7.30 ND 98.73 91.43 NA NA NA 0.0012/20/2012 8.17 ND 98.73 90.56 NA NA NA 0.0012/24/2012 7.96 ND 98.73 90.77 NA NA NA 0.001/4/2013 8.02 ND 98.73 90.71 NA NA NA 0.051/8/2013 8.03 ND 98.73 90.70 NA NA NA 0.051/15/2013 7.65 ND 98.73 91.08 NA NA NA < 0.01/25/2013 7.81 ND 98.73 90.92 NA NA NA1/29/2013 7.77 ND 98.73 90.96 NA NA NA2/7/2013 7.90 ND 98.73 90.83 NA NA NA2/14/2013 NG ND 98.73 NA NA NA NA2/27/2013 NG ND 98.73 NA NA NA NA
MW-10-D 12/10/2012 13.53 ND 94.05 80.52 NA NA NA12/20/2012 17.51 ND 94.05 76.54 NA NA NA12/24/2012 16.55 ND 94.05 77.50 NA NA NA1/4/2013 16.99 ND 94.05 77.06 NA NA NA1/8/2013 17.31 ND 94.05 76.74 NA NA NA1/15/2013 14.85 ND 94.05 79.20 NA NA NA1/25/2013 14.14 ND 94.05 79.91 NA NA NA1/29/2013 13.71 ND 94.05 80.34 NA NA NA2/7/2013 14.11 ND 94.05 79.94 NA NA NA2/14/2013 14.03 ND 94.05 80.02 NA NA NA2/27/2013 14.03 ND 94.05 80.02 NA NA NA
MW-12-D 12/10/2012 27.34 ND 96.25 68.91 NA NA NA12/20/2012 42.81 ND 96.25 53.44 NA NA NA12/24/2012 41.17 ND 96.25 55.08 NA NA NA1/4/2013 40.97 ND 96.25 55.28 NA NA NA1/8/2013 41.25 ND 96.25 55.00 NA NA NA1/15/2013 29.10 ND 96.25 67.15 NA NA NA1/25/2013 NA ND 96.25 NA NA NA NA1/29/2013 NA ND 96.25 NA NA NA NA2/7/2013 29.05 ND 96.25 67.20 NA NA NA2/14/2013 29.76 ND 96.25 66.49 NA NA NA2/27/2013 30.57 ND 96.25 65.68 NA NA NA
MW-13-D 12/10/2012 17.26 ND 91.85 74.59 NA NA NA12/20/2012 24.43 ND 91.85 67.42 NA NA NA12/24/2012 23.94 ND 91.85 67.91 NA NA NA1/4/2013 24.16 ND 91.85 67.69 NA NA NA1/8/2013 22.84 ND 91.85 69.01 NA NA NA1/15/2013 19.18 ND 91.85 72.67 NA NA NA1/25/2013 19.40 ND 91.85 72.45 NA NA NA1/29/2013 20.68 ND 91.85 71.17 NA NA NA2/7/2013 19.66 ND 91.85 72.19 NA NA NA2/14/2013 22.22 ND 91.85 69.63 NA NA NA2/27/2013 21.51 ND 91.85 70.34 NA NA NA
TP-1 12/10/2012 11.04 ND NM NA NA NA NA NA12/20/2012 14.32 ND NM NA NA NA NA 0.0612/24/2012 13.60 ND NM NA NA NA NA 0.061/4/2013 14.75 ND NM NA NA NA NA 0.041/8/2013 14.98 ND NM NA NA NA NA 0.051/15/2013 14.10 ND NM NA NA NA NA 0.081/25/2013 12.49 ND NM NA NA NA NA1/29/2013 12.04 ND NM NA NA NA NA2/7/2013 12.73 ND NM NA NA NA NA
Well head submerged in puddle
Well head submerged in puddle
Table 1 - Well Gauging SummaryGasoline Fueling Station – Royal Farms No. 96
500 Mechanic Valley Road, North East, Maryland 21901
2/14/2013 12.54 ND NM NA NA NA NA2/27/2013 12.62 ND NM NA NA NA NA
TP-2 12/10/2012 11.37 ND NM NA NA NA NA NA12/20/2012 15.24 ND NM NA NA NA NA 0.0612/24/2012 14.51 ND NM NA NA NA NA 0.051/4/2013 15.68 ND NM NA NA NA NA 0.071/8/2013 15.89 ND NM NA NA NA NA 0.061/15/2013 15.03 ND NM NA NA NA NA 0.101/25/2013 13.41 ND NM NA NA NA NA1/29/2013 12.97 ND NM NA NA NA NA2/7/2013 13.63 ND NM NA NA NA NA 0.062/14/2013 13.46 ND NM NA NA NA NA 0.042/27/2013 13.53 ND NM NA NA NA NA 0.08
TP-3 12/10/2012 12.72 ND NM NA NA NA NA NA12/20/2012 15.96 ND NM NA NA NA NA 0.0512/24/2012 15.23 ND NM NA NA NA NA 0.041/4/2013 16.40 ND NM NA NA NA NA 0.081/8/2013 16.60 ND NM NA NA NA NA 0.081/15/2013 15.73 ND NM NA NA NA NA 0.101/25/2013 14.13 ND NM NA NA NA NA1/29/2013 13.67 ND NM NA NA NA NA2/7/2013 14.37 ND NM NA NA NA NA 0.052/14/2013 14.17 ND NM NA NA NA NA 0.052/27/2013 14.27 ND NM NA NA NA NA 0.17
TP-4 12/10/2012 12.82 ND NM NA NA NA NA NA12/20/2012 15.12 ND NM NA NA NA NA 0.0612/24/2012 14.38 ND NM NA NA NA NA 0.051/4/2013 15.55 ND NM NA NA NA NA 0.051/8/2013 15.76 ND NM NA NA NA NA 0.061/15/2013 14.91 ND NM NA NA NA NA 0.091/25/2013 13.29 ND NM NA NA NA NA1/29/2013 12.85 ND NM NA NA NA NA2/7/2013 13.53 ND NM NA NA NA NA2/14/2013 13.35 ND NM NA NA NA NA2/27/2013 13.42 ND NM NA NA NA NA
RW-1* 12/10/2012 12.50 ND 95.92 83.42 NA NA NA
RW-2* 12/10/2013 13.80 13.80 96.21 82.41 82.41 82.41 0.00Sheen
RW-3* 12/10/2013 14.55 ND 97.59 83.04 NA NA NA
RW-4* 12/10/2013 14.15 14.15 97.38 83.23 83.23 83.23 0.00Sheen
RW-5 12/10/2012 12.41 ND 96.21 83.80 NA NA NA NA12/20/2012 15.80 ND 96.21 80.41 NA NA NA 7.0012/24/2012 15.02 ND 96.21 81.19 NA NA NA 3.901/4/2013 16.39 ND 96.21 79.82 NA NA NA 8.001/8/2013 16.66 ND 96.21 79.55 NA NA NA 8.001/15/2013 15.86 ND 96.21 80.35 NA NA NA1/25/2013 13.25 ND 96.21 82.96 NA NA NA1/29/2013 13.04 ND 96.21 83.17 NA NA NA2/7/2013 14.52 ND 96.21 81.69 NA NA NA2/14/2013 15.11 ND 96.21 81.10 NA NA NA > 5.02/27/2013 15.49 ND 96.21 80.72 NA NA NA > 5.0
Depth to Groundwater Pump intake: 14.5 ft.
Depth to Groundwater Pump intake: 15.0 ft.
Depth to Groundwater Pump intake: 16.5 ft.
Depth to Groundwater Pump intake: 15.0 ft.
Table 1 - Well Gauging SummaryGasoline Fueling Station – Royal Farms No. 96
500 Mechanic Valley Road, North East, Maryland 21901
RW-6* 12/10/2013 13.33 ND 96.78 83.45 NA NA NA
RW-7 12/10/2013 13.23 ND 96.60 83.37 NA NA NA NA12/20/2012 16.09 ND 96.60 80.51 NA NA NA 13.0012/24/2012 16.28 ND 96.60 80.32 NA NA NA 15.001/4/2013 17.22 ND 96.60 79.38 NA NA NA 21.001/8/2013 17.60 ND 96.60 79.00 NA NA NA 21.001/15/2013 16.96 ND 96.60 79.64 NA NA NA1/25/2013 13.99 ND 96.60 82.61 NA NA NA1/29/2013 13.79 ND 96.60 82.81 NA NA NA2/7/2013 15.62 ND 96.60 80.98 NA NA NA2/14/2013 15.73 ND 96.60 80.87 NA NA NA > 5.02/27/2013 15.60 ND 96.60 81.00 NA NA NA > 5.0
RW-8* 12/10/2013 13.60 ND 97.98 84.38 NA NA NA
RW-9* 12/10/2012 7.30 ND 97.25 89.95 NA NA NA
RW-10* 12/10/2013 13.87 13.87 96.98 83.11 83.11 83.11 0.00Sheen
RW-11* 12/10/2013 13.21 13.21 96.29 83.08 83.08 83.08 0.00Sheen
RW-12* 12/10/2013 13.70 ND 98.20 84.50 NA NA NA
RW-13 12/10/2012 14.37 14.37 97.52 83.15 83.15 83.15 0.00 Sheen NA12/20/2012 17.64 ND 97.52 79.88 NA NA NA 6.0012/24/2012 17.26 ND 97.52 80.26 NA NA NA 2.201/4/2013 18.05 ND 97.52 79.47 NA NA NA 7.001/8/2013 18.46 ND 97.52 79.06 NA NA NA 7.001/15/2013 17.74 ND 97.52 79.78 NA NA NA1/25/2013 14.88 ND 97.52 82.64 NA NA NA1/29/2013 14.70 ND 97.52 82.82 NA NA NA2/7/2013 16.54 ND 97.52 80.98 NA NA NA 2.202/14/2013 16.82 ND 97.52 80.70 NA NA NA > 5.02/27/2013 17.78 ND 97.52 79.74 NA NA NA > 5.0
* - Well used for recovery by the VE/GE SystemVE/GE System began operation 12/11/2012LPH = Liquid Phase HydrocarbonTOC = Top of Casing ElevationND = None DetectedNA = Not ApplicableNG = Not GaugedNM = Not MeasuredVacuum pressure readings measured in inches of waterCorrected water elevation based on LPH density of 0.7 grams per milliliter
Depth to Groundwater Pump intake: 15.0 ft.
Depth to Groundwater Pump intake: 14.5 ft.
Depth to Groundwater Pump intake: 15.5 ft.
Depth to Groundwater Pump intake: 13.75 ft.
Depth to Groundwater Pump intake: 9.5 ft.
Depth to Groundwater Pump intake: 16.0 ft.
System Influent Dissolved Benzene
Concentration (ug/L)
System Influent Dissolved BTEX Concentration
(ug/L)
System Influent Dissolved
MTBE Concentration
(ug/L)
System Influent
Dissolved TPH-GRO
Concentration (ug/L)
PID (ppm) Airflow (cfm)
12/11/12 - 1/8/13 28 503 2007 0 2870 25 866,880.0 866,880.0 1.95 21.50 351 1221/9/13 - 2/7/13 16 47.1 233 0 383 16 299,520.0 1,166,400.0 1.18 13.00 262 1472/8/13 - 3/6/13 22 41.5 722.3 0 967 15 403,200.0 1,569,600.0 1.16 12.73 107 362
BTEX = Benzene, toulene, ethylbenzene and xylenes
Calculation used for dissolved phase recovery in pounds: Flow rate gpm * contaminate concentration ug/L * 3.785 L/gal * 1440 min/day *(2.205 lbs/10^9 ug)
Calculation used for dissolved phase recovery in gallons: Flow rate gpm * contaminate concentration ug/L * 3.785 L/gal * 1440 min/day *(2.205 lbs/10^9 ug) / 6.25 lbs/gal
Groundwater discharge is estimated due to malfunction in discharge totalizer
Liquid (gallons)
Dissolved (gallons)
Liquid (lbs) Dissolved (lbs)Dissolved (lbs/day)
Vapor (lbs)Vapor
(lbs/day)12/11/12 - 1/8/13 0 2.32 83.21 83.21 0.00 14.52 0.52 505.51 18.05 520.03 520.03
1/9/13-2/7/13 0 0.09 41.66 124.87 0.00 0.58 0.04 259.80 16.24 260.39 780.422/8/13 - 3/6/13 0 0.39 57.87 182.74 0.00 2.43 0.11 359.27 16.33 361.70 1142.12
Calculation used for dissolved phase recovery in pounds per day: Flow rate gpm * Total BTEX concentration ug/L * 3.785 L/gal * 1440 min/day *(2.205 lbs/10^9 ug)Calculation used for vapor phase recovery in pounds per day: Airflow ft³/min * 0.0283 m³/ft³ * VOCs ppm * 105 g/mole BTEX * .00268 gas constant * 0.001 kg/g * 52.91 lbs per day / kg per hr
1 gallon = 6.25 pounds
41.5757.48
Average Extraction Rate
for System (gpm)
Period Total Gallons
Cumulative Gallons to
Date
Cumulative GW Discharge (gallons)
Dissolved Phase
80.88
Cumulative Pounds to
Date
Gallons of Hydrocarbons (BTEX) Recovered During Period Pounds of Hydrocarbons (BTEX) Recovered During Period
Monitoring PeriodAverage
Extraction Rate per Well (gpm)
Vapor Phase
Monitoring
Period
Operating Days
Maximum System
Discharge Flow Rate
(gpm)
Period GW Discharge (gallons)
Vapor (gallons)
500 Mechanics Valley Road, North East, MD 21901
Period Total Pounds
Table 2 - VE/GE System Quarterly Hydrocarbon Recovery Data
Fueling Station – Royal Farms #96
Table 3 - VE/GE System Quarterly Hydrocarbon Recovery Estimates
Fueling Station – Royal Farms #96
500 Mechanics Valley Road, North East, MD 21901
Royal Farms #96 Monthly Update Report OCP Case No. 2011-0729-CE AEC Project # 05-056RF096
Attachment C
VE/GE System Monitoring Worksheet Date: 2/14/2013Gasoline Fueling Station – Royal Farms #96 Time: 16:00500 Mechanics Valley Road Recorded By: JDWNorth East, MD
System Running (Y/N) YesAlarm Condition (Y/N) NoCircuits Tripped (Y/N) NoStripper Backpressure (psig) 15.5Run Time (hours) 1,174.2Electric (kw/h) 54,554
SVE Exhaust Temperature (°F) 145AWS-1 Vacuum Pressure (inHg) 9.0Dilution Valve (% open) 25Compressor Tank Pressure (psi) 120Pressure to Wells (psi) 22GW Return Pressure (psi) 0Ambient Room Temperature (°F) 49Sump Transfer Pump Pressure (psi) 50Bag Filter Vessel Pressure (psi) 46Carbon 1 Pressure (psi) 42Carbon 2 Pressure (psi) 22Flow Rate (gal/min) 15A backflush was performed on both Carbon tanksGroundwater filter bags were replaced
VE/GE System - Building Interior
Main Control Panel
VE/GE System Monitoring Worksheet Date: 2/27/2013Gasoline Fueling Station – Royal Farms #96 Time: 9:30500 Mechanics Valley Road Recorded By: JDWNorth East, MD
System Running (Y/N) YesAlarm Condition (Y/N) NoCircuits Tripped (Y/N) NoStripper Backpressure (psig) 15.5Run Time (hours) 1,353.8Electric (kw/h) 59,761
SVE Exhaust Temperature (°F) 138AWS-1 Vacuum Pressure (inHg) 9.0Dilution Valve (% open) 0Compressor Tank Pressure (psi) 125Pressure to Wells (psi) 21GW Return Pressure (psi) 0Ambient Room Temperature (°F) 49Sump Transfer Pump Pressure (psi) 51Bag Filter Vessel Pressure (psi) 47Carbon 1 Pressure (psi) 42Carbon 2 Pressure (psi) 13Flow Rate (gal/min) 12.5A backflush was performed on both Carbon tanksGroundwater filter bags were replaced
VE/GE System - Building Interior
Main Control Panel