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    Vibrations

    Spring 2016 | Volume 33, Number

    Dedicated to the dissemination of practical information on evaluating machinery behavior and condition.

    www.vi-institute.org

    Turbocharger Rolling-ElementBearing Observed During Failure

    By Maryon J. Williams, Jr., Ph.D., P.E.

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    INTRO TO MACHINERY VIBRATION (IMV) 

    April 18-21, 2016

    Knoxville, TennesseeAugust 15-18, 2016

    Oak Brook, Illinois

    June 14-17 2016

     Asheville, North Carolina

    October 4-7, 2016

    Salem, Massachusetts

    BASIC MACHINERY VIBRATION (BMV) 

    July 25-29, 2016

    Knoxville, TennesseeSeptember 19-23, 2016

    San Diego, California

    Nov. 28 — Dec. 2, 2016

    New Orleans, Louisiana

    2016 TRAINING SCHEDULE 

    Practical Application. 

    Expert Knowledge. 

    Real-World Solutions. 

    Vibration Institute training courses strike the perfect balance among theory, principles,

    techniques, case histories, and practical knowledge to help you be a better analyst.

     Attend a Vibration Institute training course and take your career and organization to the

    next level. 

    2016 Training Course Schedule and Locations * 

    MACHINERY VIBRATION ANALYSIS (MVA) 

    September 19-23, 2016

    San Diego, California

    Nov. 28 — Dec. 2, 2016

    New Orleans, Louisiana

    ADVANCED VIBRATION CONTROL (AVC) 

    April 18-21, 2016

    Houston, Texas 

    ADVANCED VIBRATION ANALYSIS (AVA)

    Nov. 29 — Dec. 2, 2016

    New Orleans, Louisiana 

    BALANCING OF ROTATING MACHINERY (BRM)  ROTOR DYNAMICS AND MODELING (RDM) 

    July 25-29, 2016 

    Knoxville, Tennessee

    October 3-7, 2016 

    Salem, Massachusetts

    May 9-13, 2016

    Knoxville, Tennessee 

    * Assigned course dates and locations are subject to change.  

    Visit www.vi-institute.org for the most up-to-date information on the 2016 training schedule. 

    Remaining Dates

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    June 15-17, 2016

    Renaissance Asheville Hotel

    Asheville, NC

    Save 15% in addition to the Early Bird DiscountUse Exclusive Discount Code: nc2016

    vi-institute.org/conference | 630.654.2254 | [email protected]

    Pre-workshops | IMV Training Course | Keynote Speaker |

    25 Exhibitors | Networking Reception | Giveaways & much more!

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    2  VIBRATIONS SPRING 20

    Contents

    columns | departments

    4  Feature Article  Turbocharger Rolling-Element

    Bearing Observed During FailureBy Maryon J. (Skip) Williams, Jr., Ph.D., P.E.

    8  Case History  Analyzing the Start-Up Vibration

    of HOT PUMPSBy Joppu Thomas 

    16  Case History  Rub Identification in Hydrogen

    Centrifugal CompressorBy Juan C. Ustiola 

    SPRING 2016Volume 33, Number 1ISSN 1066-8268

    3  Letter from the President By David Correlli, VI Board President 

    22  2016 Newly Certifed Individuals

    24  A Fond Farewell By Robin Ginner 

    Vibrations  is published quarterly inspring, summer, fall, and winter bythe Vibration Institute. Statements offact and opinion are the responsibilityof the authors alone and do not implyan opinion on the part of the officersor members of the Vibration Institute.Acceptance of advertising does not implyan endorsement by the Vibration Institute.

    © 2016 by the Vibration Institute. All rightsreserved. Materials may not be reproducedor translated without the express writtenpermission of the Vibration Institute.

    Technical EditorBarry T. [email protected]

    Editor & AdvertisingNicole [email protected]

    List of AdvertisersConnection Technology Center Inc.PCB Inc./IMI SensorsRBTS, Inc.Reliability Web

    Postmaster

    Send address changes to the VibrationInstitute, 2625 Butterfield Road, Suite128N, Oak Brook, IL 60523.

    SubscriptionsVibrations  is sent quarterly toInstitute members. The subscriptionrate is $75/year for individuals notaffiliated with the Institute.

    Reprints and Back IssuesTo order article reprints or request reprintpermission, please send your requestin writing to [email protected] call the Institute at (630) 654-2254.

    Vibration Institute

    Please send any correspondenceregarding change of address oradvertising to the Vibration Institute.

    Vibration Institute2625 Butterfield RoadSuite 128NOak Brook, IL 60523(630) 654-2254

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    4  VIBRATIONS SPRING 20

    feature article

    Skip Williams is Senior Engineer with Condition Analyzing Cor

    ration (www.cacvibe.com). He has conducted vibration surv

    and has analyzed the data from ships for over 25 years. He c

    tributes to ISO/TC 108/SC 2/ WG2 “Vibration of Ships” and to ISO/

    8/SC 8/WG12 “Ship Vibration.” He was project leader for ANSI/A

    S2.28-2009 “Guide for the Measurement and Evaluation of BroadbVibration of Surface Ship Auxiliary Machinery.”

     ABSTRACT

    This article shows the failure of a rolling-element bearing in real ti

    on the turbocharger of a ship’s Diesel engine. The failure was ant

    pated because the bearing had failed previously when the turbochar

    reached a certain speed. Instrumentation was prepared to take conti

    ous samples of the data before, during, and after the failure. While

    time from initial detection of a bearing fault until failure of the bear

    can typically take months, the failure reported here occurred in m

    seconds. The vibration data at failure indicated a bearing cage prob

    which was later confirmed with debris in the bearing cage.

    BACKGROUND

    A unique situation was provided when it was known that a bear

    on the main Diesel engine turbocharger of an oil tanker had failed

    previous occasions. The propulsion system consisted of a medium sp

    8-cylinder engine with a reduction gear to the propeller of ratio 5:05

    (Figure 1). The propeller was controllable pitch, meaning the thrust

    ward or aft was controlled by the pitch of the propeller, not by the sp

    and direction of the propeller. Also attached to the gear was a PTO g

    erator with a step-up ratio of 2.022:1. The normal engine speed wa

    constant 595 rpm. The expected forcing frequencies from this mach

    are shown in Table 1.

    The turbocharger bearings were proprietary anti-friction roller tylubricated with oil pumps operating on the same shaft as the turbine

    compressor and mounted on the outside of the compressor and turb

    wheels. The compressor bearing was the thrust bearing and consiste

    11 balls in two rows. The turbine bearing had 11 rollers in one row. T

    bearings were mounted on damped spring assemblies on the radial

    axial sides meant to absorb a degree of imbalance in the rotor. Aft

    By Maryon J. (Skip) Williams, Jr., Ph.D., P.E.Certied Vibration Specialist IV 

    Condition Analyzing Corporation

    Eatontown, NJ

    Turbocharger

    Rolling-Element BearingObserved During Failure

    Figure 1: Layout of engine, step-up gear to generator/motor 

    Figure 2: - Waterfall plot during failure 

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    feature article

     SPRING 2016 VIBRATIONS 

    failure of the turbine side lube oil pump, a replacement rotor was bal-

    anced and installed. On two subsequent occasions the turbocharger

    bearings had also failed when the rotation rate reached 13,400 rpm.

    TURBOCHARGER BEARING FAILURE

    The vessel was run at lower load than normal with a propeller

    pitch of 55% until the end of the voyage. The greatest vibration

    was found in the axial direction with radial vibration low. Measure-

    ments were set up on the turbocharger with an axially-mounted gen-eral-purpose accelerometer. Initial readings were taken at Fmax of

    5,000 Hz with minimal high-frequency activity. Sampling was then

    taken with Fmax of 500 Hz and 800 lines with aterfall slices every

    9.6 seconds. With these settings up to 16 minutes could be saved in

    a single waterfall. Toward the end of the voyage the propeller pitch

    was gradually increased to 73% over a time period of half an hour.

    During the increased loading, the turbocharger rpm increased from

    10,000 rpm to 13,400 rpm when the turbocharger failed (Figure 2).

    Table 1: Speeds & Forcing Frequencies

    Component Rotation rate (rpm) Harmonics Comment

    Engine 595 2X, 4X, 6X-engine 8 cylinders

    Turbocharger 8,000-18,000 11X 11 full compressor vanes

    Step Up Gears 595/1203 91X-engine Teeth 91/184 (2.022:1)Reduction Gears 595/118 19X, 76X -engine Teeth 19/96 (5.042:1)

    Propeller 118 4X 4 blades

    fig.

    3

    fig.

    4

    fig.

    5

    fig.

    6

    fig.

    7

    fig.

    8

    fig.

    9

    Figure 3: T-9 minutes 

    Figure 4: T-9.6 seconds 

    Figure 5: Failure 

    Figure 6: T+9.6 seconds 

    Figure 7: T+19.2 seconds 

    Figure 8: T+2 minutes (Maximum vibration at rotation rate) 

    Figure 9: T+3 minutes 

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    6  VIBRATIONS SPRING 20

    feature article

    The failure was preceded with no indication of abnormal p

    rameters on the turbocharger, turbocharger lube oil pump, engi

    or gear. What was observed during the load increase was a d

    crease in the vibration at rotation rate from 0.09 to 0.03 inch p

    second peak, then a slight increase to 0.05 ips peak. From owaterfall slice to the next, an increase in 1X-rotation rate to 0.

    ips suddenly appeared, but more importantly a new frequency

    0.47X-rotation rate also appeared (Figure 6). In other words, t

    time from detection of an abnormal spectrum until the failure w

    observed was less than 10 seconds or approximately 2000 rot

    tions. The vibration at 0.47X-rotation rate continued for only o

    more waterfall slice (Figure 7) and was not seen again. Vibrati

    also appeared at the upper rotation-rate sideband at 1.47X-ro

    tion rate. Over the next 2 minutes, vibration at 1X-rotation r

    increased to 0.73 ips peak (Figure 8). A time sample just after t

    failure showed spikes at intervals of 9.4 milliseconds correspon

    ing to the vibration at 0.47X-rotation rate (Figure 10).

    After the failure the vibration at rotation rate decreased as t

    pitch of the propeller was reduced to limit the vibration while t

    vessel proceeded into port. The turbocharger never locked

    and continued to function until the vessel got to the dock.

    When the vessel reached port, the turbocharger was disassem

    bled. . The bearing spring assemblies in the bearing were fou

    broken as shown in Figure 11, Figure 12 and Figure 13 with

    spring clip lodged in a roller of the turbine bearing.

     ANALYSIS

    The vibration at 0.47X-rotation rate in the regular spectra is t

    frequency expected for a Fundamental Train Frequency beari

    defect (FTF). The clip lodged in the bearing roller is further e

    dence of the failure of the bearing cage.

    Vibration on a turbocharger normally consists of three comp

    Figure 10: Time sample of axial acceleration from one waterfall

    slice to the next before and after the failure. Pulses correspond to

    0.47X-rotation rate or FTF.

    Figure 11: Turbine bearing (left) and compressor bearing (right) 

    Figure 12: Turbine bearing with loose spring clip  Figure 13: View of installed turbine bearing with spring clips in

    rollers. Oil pump also shown.

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    feature article

     SPRING 2016 VIBRATIONS 

    nents: (1) vibration from the engine

    at low-frequencies, (2) vibration at

    turbocharger rotation rate, and (3)

    vibration at compressor vane-pass

    frequencies. Vibration from theengine is constant with load and is

    sometimes associated with cracking

    of the turbocharger foundation. Vi-

    bration at turbocharger rotation rate

    is associated with imbalance in the

    rotor or wear in the bearings. The

    manufacture’s recommended alarm

    level for ltered rotation rate vibra-

    tion was 0.17 ips peak. The alarm

    levels for turbocharger rotation rate

    used during the this study were 0.27

    ips peak for the 1st alarm (alert)

    and 0.40 ips peak for the 2nd alarm

    (fault). Sometimes vibration at 2X,

    3X, or 4X-rotation rate indicates

    additional wear, but was not seen in

    this case. Vibration from the engine

    was normal, and no lube oil failure

    occurred this time. Vibration at

    compressor vane-pass frequencies

    of 11X and 22X-rotation rate also

    were not seen in this case.

    Possible mechanisms for a bear-

    ing failure in a turbocharger:

    1. Thrust bearing overload2. Excessive vibration

    transmitted from the engine

    3. Lube oil failure4. Imbalance in the rotor5. Wrong thrust bearing,

    incorrect installation,

    excessive axial clearance

    The loading on the thrust bear-

    ing decreased in the axial direction

    with increasing speed (Figure 14

    and Figure 15). The decrease in

    the axial vibration with increasing

    load was due to compression of theaxial load spring with increasing

    axial thrust. The turbocharger is an

    axial turbine and a radial compres-

    sor meaning the exhaust gas pass-

    es through the turbine in the axial

    direction and the intake air passes

    through the compressor in the ra-

    dial direction (Figure 16). A major

    component of the axial thrust is the

    pull of the compressor wheel away

    from the turbine.

    The manufacturer reported that

    an incorrect balance procedure had

    been used to balance the rotor. Thebalance condition is specic for

    each turbocharger by the manufac-

    turer, but ISO quality grade 2.5 is

    a close approximation. When the

    correct procedure was used and the

    rotor re-installed, no further prob-

    lems occurred.

    Still, the absence of signicant

    vibration at 1X-rotation rate before

    the failure indicated that balance

    was not the primary cause. It is

    possible that one of the other fac-

    tors (wrong bearing, installation

    or clearance) might have been in-

    advertently corrected during the

    re-commissioning repair.

    CONCLUSIONS

    As vibration analysts we have

    several tools available to us to di-

    agnose bearing failures, including

    high-frequency algorithms. Often

    these techniques show a degree of

    bearing failure, and the question is,

    “When is the bearing going to fail”?

    The same question arises when one

    decides how often to conduct vibra-

    tion tests: should the frequency be

    monthly, weekly, or continuously

    with automatic shutdown of the

    machine?

    Bearing failure rates can happen

    in months, weeks, days, hours, min-

    utes or even seconds depending on

    the cause, machine loading, and ma-

    chine speed. The example here was

    one where the high machine speed

    (over 10,000 rpm) clearly played arole. This is one example when a

    failure could not be predicted using

    traditional vibration analysis tech-

    niques even 10 seconds beforehand.

    While the conditions of this failure

    are unique due to the circumstances

    of the installation, there is no one

    way to predict the moment of bear-

    ing failure with certainty.

    Figure 14: Time course of failure: 30-minute period (10 sec intervals)

    Figure 15: Zoom on failure event (3-minute period).

    Note only two readings at 0.47X-rotation rate 

    Figure 16: Turbocharge with axial flow turbine and

    radial flow compressor 

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    8  VIBRATIONS SPRING 20

    case history

    Analyzing the Start-UpVibration of HOT PUMPS

    INTRODUCTION

    The subject of this case history was a hot service pump of center-hung

    configuration with a multiple volute casing. The pump was directly

    driven by a 740 KW induction motor with a rated capacity of 2,800

    m3/hr with fluid specific gravity of 0.6. The pumping temperature was 280

    C (540 F).

    1ST START-UP ATTEMPT

    The commissioning team attempted a start-up of the pump many times

    However, the pump tripped on high vibration each time. High vibration waexperienced at both the pump drive-end and non-drive-end bearings. The

    values exceeded 150 microns (6 mills) at both ends. The recorded run time

    was barely a few seconds. The pump had a fluid film bearing (plain sleeve

    installed at the drive-end (DE) and a fluid film bearing/antifriction bearing

    combination installed on the thrust end (ODE). Since the run time of the

    pump was only a few seconds, it was decided to analyze the coast-down

    transient data to help determine the cause of high vibration. Due to the

    rapid acceleration of the pump during startup, start up transient amplitude

    and phase data were not considered meaningful. Therefore coast-down data

    By Joppu Thomas ABSTRACT

    One line monitoring and diagnostic systems

    are widely employed by petrochemical plants

    and refineries worldwide for monitoring critical

    machinery. These systems provide comprehen-

    sive diagnostic capabilities which can be used to

    reduce machine downtime and provide consid-

    erable savings in maintenance costs. This case

    history shows how the diagnostic capabilities

    of an online monitoring system were utilized by

    a leading refinery in the Middle East to solve a

    vibration problem experienced with a 740 KW

    Hot Pump. Hot pumps are centrifugal pumps em-

    ployed in services with temperatures above 150

    C (300 F); warm-up of these pumps are required

    prior to start-up. These pumps must be handled

    carefully during start-up to ensure normal levels

    of vibration and to prevent unwanted trips.

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     SPRING 2016 VIBRATIONS 

    case history

    was recorded and analyzed. Figure 2 below

    shows the vibration trend plots for the pump

    DE and NDE bearings.

    PUMP COAST-DOWN &

    SLOW ROLL DATA 

    Following the first start up attempt, coast-

    down and slow roll data from the pump was

    examined. A slow roll vibration level of 125

    microns (5 mils) and 163 microns (6.4 mills)

    was observed at the drive end (DE) and non-

    drive-end (NDE) of the pump respectively

    at a speed ≤ 10% of operating speed (~ 300

    rpm). In addition, this radial vibration at the

    drive and non-drive-end was observed to be

    in-phase. Both orthogonal set of probes (X

    & Y) installed on the pump bearings indi-

    cated high amplitudes. Slow roll data on

    rotating equipment is typically collected at

    speeds < 10% of the operating speed of the

    machine. At these slow speeds, the dynam-

    ic forces due to problems such as unbalance

    are very low and can be reasonably dis-

    counted; the “vibration” seen at these very

    slow speeds can be due to mechanical or

    electrical run-out, a physical bow or bend in

    the rotor, or other problems that are not al-

    ways easy to determine without this unique

    data. Prior tests at these hot pumps had rou-

    tinely measured slow-roll “vibration” at or

    near 10 microns (1/2 mill).

    BEARING INSPECTION

    Owing to the high vibration noticed, the

    contractor decided to open the pump bear-

    ings for a quick inspection. The drive-end

    and non-drive-end bearing clearances

    were checked and found to be within rec-

    ommended tolerances. The wear marks on

    the bearings also appeared nor-

    mal. It was advised to the contractor to do a

    manual slow roll check on the pump rotor

    after assembly of the bearings and check for

    run-out. Typically the slow roll vectors are

    around 5 microns (0.2 mills). This is mostlydue to mechanical/electrical run-out of the

    probe target surface and some small residual

    bow of the rotor. However the values mea-

    sured during manual rotation were much

    larger around 26 microns (1 mill).

    EXPLORING THE REASON

    FOR VIBRATION

    Many hot pumps employed in refineries all

    around the world experience high levels of

    vibration during start-up. However, many of

    these cases go unnoticed due to absence of

    shaft proximity probe monitoring systems.

    A set point multiplier is a useful feature pro-

    vided for machinery with proximity probe

    based monitoring systems which exhibit

    Certifcation SurveillanceIn order to protect the Institute members who have justly earned certication a

    a Vibration Analyst, the Vibration Institute wants to pursue individuals who falsi

    Institute certication in any manner.

    If you are aware of any instance in which you believe an individual is falsifying hi

    her certication status, please call or contact the Vibration Institute immediately.

    If you are aware of any individual who you believe is violating basic ethics, pleas

    contact the Institute as soon as possible. Failure to do so degrades the reputatio

    of your certication and the Vibration Institute.

    (630) 654-2254

    [email protected]

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    10  VIBRATIONS SPRING 20

    case history

    high levels of vibration during transi

    condition. TRIP/SET POINT MULTIP

    ERS enable the ALARM & TRIP values

    be temporarily elevated until steady s

    conditions are achieved in these machin

    Since most machines are designed to sand operate below set levels of vibrati

    caution must be exercised before appli

    tion of a multiplier. Arriving at a pro

    value and duration for a set-point multi

    er involves making a database of vibrat

    levels and their duration during multi

    start-stops of machine. Pumps emplo

    in hot service commonly experience st

    up vibration due to uneven expansion of

    casing during warm-up. In extreme ca

    poor warm-up can lead to shaft bows. V

    ious warm-up piping arrangements are

    forward by pump manufacturers.

    API 686 gives guidelines for warm

    piping arrangements. Typical warm-up

    rangements for a top-suction, top discha

    pump (center-hung conguration) norma

    consists of two routes of entry for the wa

    up uid - through the discharge check va

    bypass and through the warm-up line at

    bottom of the pump casing. The entry ro

    through the discharge check valve byp

    introduces uid into the discharge volute

    the pump. The introduction of uid thro

    the bottom of the pump casing ensure

    uniform bottom-up heating of the cas

    and rotor.

    Due to the high start-up vibration ex

    rienced at the pump in question, an inv

    tigation of the warm-up piping system

    rangement was carried out by the ren

    engineering team. It was noted that at a

    pumps, the discharge check valve by-p

    route was absent thus heating was carr

    out solely through the bottom casing dra

    These “bottom warm-up only” pumps c

    sistently experienced lower levels of vibtion during start-up.

    The investigation also discovered a p

    ticular hot pump which experienced h

    vibration during start-up until a discha

    drain line was introduced. Introduction

    the discharge drain line was intended a

    temporary measure until repairs to the ch

    valve by-pass arrangement could be ma

    The drain line from the discharge was

    Figure 2: Trend of pump vibration during start-up and coastdown? 

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     SPRING 2016 VIBRATIONS  1

    case history

    lized to introduce warm-up uid into the casing bot-

    tom. Following the introduction of the discharge

    drain line, this pump experienced lower levels of vi-

    bration during start-up.

    The investigation concluded that the hot pump

    warm-up piping arrangements played a signicantrole in the start-up vibration levels experienced at

    the pumps. Subsequently, it was agreed to perform

    only bottom-up warm-ups of the pumps. Also it was

    agreed that a controlled warm-up was required with

    a maximum casing top to bottom temperature differ-

    ential not to exceed 50 C (122 F). On the basis of all

    the above incidents, the engineering team concluded

    that heating from the pump top to bottom is an infe-

    rior practice as it results in an excessive temperature

    differential within the pump casing (top to bottom).

    This temperature differential creates a very large

    “humping” or “bowing” tendency since the pump ex-

    pands more at the top than the bottom. As a result,

    the bearing brackets & housings might shift down at

    both ends of the pump (center-hung arrangement)

    and the rotor will bow along with them. However, it

    is worth mentioning that a few hot pumps of similar

    arrangement from a different manufacturer did not

    show a signicant effect on start-up vibration, irre-

    spective of their warm-up routing – the exact cause

    for this was not known.

    TRIP/SET POINT MULTIPLER

    With the reason for excessive start-up vibration iden-

    tified, it was necessary to estimate and apply a suit-

    able TRIP or SETPOINT MULTIPLER to the ma-

    chines. The criterion for arriving at the trip multiplier

    duration and set points are based on machine histo-

    ry. A carefully compiled data base of the vibration

    data for a machine during multiple start-ups is very

    valuable information. The SET POINT multiplier

    duration should be sufficient to overcome start-up

    temperature transients and stabilization. A bowed

    rotor or unevenly heated casing on these machines

    can endure anywhere between 45 to 180 seconds be-

    fore the vibration levels stabilize below alarm levels.

    Depending on the machine, sometimes it is advisable

    to apply a multiplier to a specific vibration channel,based on prior history where the other channels ex-

    hibit lower levels of vibration.

    CONCLUSION

    The pump was finally put in service with the modi-

    fied warm-up arrangement and exhibited acceptable

    vibration levels. The operation team modified the

    warm-up procedures and piping per the findings of

    the investigation to ensure a bottom-up heating of

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  • 8/15/2019 VI1603 Spring R2 Final

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    14  VIBRATIONS SPRING 20

    the pump. The TRIP MULTIPLER settingwas also judiciously applied. A multipli-

    er of 2 times trip value (2X) for a duration

    of 120 Seconds was applied which ensured

    temperature stabilization of the pump. Sub-

    sequent bearing inspection was also done to

    physically verify that the applied multiplier

    did not exceed the bearing clearance values.

    Insufficient warm-up or fast warm-ups can

    lead to high vibration in the pump during

    start-up due to a thermally induced bow ofthe rotor. A thermally induced bow can also

    occur due to a temperature differential in the

    mechanical seal area. Some other factors

    which can induce a thermal bow are:

    1. Length of time pump remainedstationary (not rotating)

    in a hot condition.

    2. Casing differential temperatures.

    REFERENCES

    1. Fundamentals of Rotating

     Machinery Diagnostics by Dona

     E. Bently and Charles T Hatch.

    2.  Rotordynamics by Agnieszka Muszynska.

    3.  Design and Opeartion of pumps f

     Hot standby services by Charles.C

    .Heald and David.G.Penry.

    4.  Review of Vibration problem in power station Boiler feed Pumps

     David France, Weir pumps,Glasg

    case history

    Figure 4: Warm-up piping arrangement 

    Certication as a Vibration Analyst is valid for ve years from the

    date of current certication level. After ve years, and in com-

    pliance with ISO 18436: Part I, certied Vibration Analysts are

    required to recertify. Recertication at the current level of certica-

    tion can be achieved in one of two ways:

    Renewal. You may provide evidence of continuing education ex-

    perience, training and/or technical activity. Points for renewal canbe earned for vibration-related activities including work experi-

    ence, professional development, attending industry, association or

    chapter meetings, and vibration-related presentations and pub-

    lished articles.

    Re-examination. You may take the certication exam at the level

    you are currently certied. This requires scheduling an examination

    and securing a proctor per established Vibration Institute protocol.

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    level certied.

    Points toward recertication can be earned in various ways. The

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    Visit www.vi-institute.org and click on Certification  to learn more

    about earning points for re-certication!

    Recertifcation Requirements

    Figure 3: Pump BODE for coast-down (Pump DE)

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    16  VIBRATIONS SPRING 20

    case history

    Rub Identification in HydrogenCentrifugal Compressor

    MACHINE DESCRIPTION

    The machine to be analyzed is a 5-stage

    Hydrogen Centrifugal Compressor

    manufactured in 1995 by Nouvo Pig-

    none. It is driven by a steam turbine whose

    normal operating speed is between 8,000

    and 9,500 rpm. The machine is monitored

    using X-Y proximity probe pairs on each

    fluid film bearing as shown in the instru-

    mentation diagram (Figure 1) along with

    two axial probes and a Keyphasor.

    SYMPTOMS

    A sudden increase in the vibration lev

    was observed in the DCS and PI softw

    (Figure 2). After observing the abnorm

    increase in the vibration levels, an imme

    ate request was made to the vibration s

    cialist to analyze and identify the cause

    the sudden change.

     VIBRATION ANALYSIS

    Rubs are generally defined as contact

    Juan C. Ustiola,

    Vibration Specialist Category III.

     ABSTRACT

    The following case history ex-

    plains how a rubbing condition

    was identified in a centrifugal

    compressor by the utilization

    of phase, bode and orbit plots.

    This information was required

    during the troubleshooting pro-

    cess to analyze sudden changes

    observed in the vibration levels

    during compressor operation.

    An abnormal increase was no-

    ticed in the control room by the

    night shift crew. The rotating

    equipment group was quickly

    dispatched to investigate the

    problem.

    KEYWORDS:

    Rub, rubbing, bow, orbit, phase,

    bode, shaft centerline, vibration

    analysis.

    (Right) Figure 2: PI software showing the sudden

    increase in vibration levels at the DE X & Y probes.

    Figure 1: System 1 Machinery Diagram 

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     SPRING 2016 VIBRATIONS  1

    case history

    tween stationary and rotating

    components of a machine. A

    rub in a rotating machine usu-

    ally doesn’t happen by itself; it

    is usually a secondary effect of

    several malfunctions occurring

    at the same time. There are two

    types of rubs, as shown in figure

    3. The first is an impact rebound

    type rub; in this case an impact

    occurs, and then the rotor bounc-

    es back, and the process is repeat-

    ed and repeated, etc. The second

    is a friction rub that causes fairly

    constant contact between a rotat-

    ing and stationary part.

    Our case had all the symptoms

    of a friction type, where the rub

    looks like unbalance. The vibra-

    tion characteristics were high

    1X vibration, with no major

    amplitude in harmonics and no

    sub-harmonic frequencies.

    There are certain myths about

    rubs and the way it is presented.

    In our situation (friction type) one

    of the most common effects ob-

    served in the vibration response

    are changes to the 1X vector due

    to thermal bowing of the rotor. A

    rub under different circumstances

    is manifested in different ways.

    For example, if operating speedis sufciently above the rst crit-

    ical speed (resonance frequency),

    then a sub-synchronous frequen-

    cy may be present such as 1/2 X,

    1/3 X, or 1/4 X.

    In practice it has been observed

    that vibration due to a rub occur-

    ring at 1/2 X might take place

    when the running speed is above

    two times the rst critical speed

    and 1/3 X when the running speed

    is above three times the rst crit-

    ical speed. In our case this con-

    dition did not apply since our op-

    erating speed was not far enough

    above the rst critical speed. Full

    spectrum waterfall indicates the

    change in the 1X vibration ampli-

    tude (Figure 4).

    It is possible to sort rubbing out

    from a balance issue by looking at

    the 1x amplitude and phase over

    time. If a shaft is unbalanced, the

    phase angle should not change

    over time at a constant speed.

    However if the rotor is bowed

    due to a rub, the amplitude and

    phase angle may shift over time

    as shown in gure 5.

    In turbomachinery is always

    important to trend the 1x val-

    ue (Amplitude and Phase) since

    the symptoms of many prob-

    lems occur at that fre-

    quency. When rubbing

    occurs, sudden changes

    in the phase are expected

    at a constant speed; this

    was observed in this case

    study, where two sudden

    steps in phase & ampli-tude were observed within

    a period of 13 days. These

    changes primarily occur

    due to the contact of sta-

    tionary & rotating parts;

    heating from friction is

    generated at certain areas

    of the rotor (where the rubs

    Figure 3: Types of rubs [1] 

    Figure 4: Waterfall spectrum showing

    increase at 1X Vibration Amplitude.

    Figure 5: 1x Amplitude & Phase shift over the time at constant speed.

     Figure 6: Rotor in Healthy Condition (June 2013).

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    case history

    are) which in turn results in a bowed shaft.

    Bode plots revealed the change in the critical speed where the

    rotor stiffened due to the rub. In some cases it can be higher than

    the normal critical speed, since we are modifying the natural fre-

    quency.

    Several diagnostic plots are useful when diagnosin

    rub. Chief among these is the shaft orbit plot (Figure

    In some occasions shaft orbit presentations can give qu

    dramatic indications of a rub as evidenced by at sp

    on portions of the orbit where contact is occurring

    restriction of orbital motion. [2]

    FINDINGS

    The drawing shown in figure 9 highlights the areas wh

    the rubbing occurred in the hydrogen compressor. T

    sectional drawing will allow us to visualize the c

    cerned areas in a better way.

    The following pictures provide evidence of the pr

    lems analyzed through the vibration plots, where our t

    ory of rubbing was proven. The drive end probes (Dwere the key for the investigation, since the problem w

    reected best in that area. During disassembly much da

    age was observed in stationary and rotary parts, howe

    most of the severe problems were noticed near the s

    tion (non-drive end), where rubbing at the inter-stage l

    yrinth seals (rst stages) and fractures at the diaphra

    were found. By analyzing the evidence, we suspect t

    the shaft was internally misaligned & bowed during

    eration causing a pivoting effect in the DE side where

    18  VIBRATIONS SPRING 20

    Figure 8: Orbit plots before and after the rub.

    Figure 7: Rotor with Rubbing problem (May 2015).

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    20  VIBRATIONS SPRING 20

    case history

    increase of vibration levels was observed.

    Piece of suction strainer found attached at impeller

    eye. Solid deposits found inside and outside the

    cylindrical inner bundle (cartridge casing) where rotor

    and stationary internals are assembled.

     ROOT CAUSE DETERMINATION

    So we knew that a significant rub had occurred but

    why? What caused or initiated this problem? From

    figure 10 below notice that the shaft centerline position

    had moved over time. This was observed as evidence

    of internal misalignment between the rotor and station-

    ary diaphragms, which caused an upward trajectory

    from July 2013 to February 2015.

    Damage was observed in both stationary and rotating parts during

    the site inspection. Damage was observed at the inter-stage laby-

    rinth seals, diaphragms and balance drum; contact between these

    components created a rub, resulting in high vibration levels. The

    contact between these stationary and rotating parts also generated

    heat from friction causing thermal growth changes. These chan

    in thermal growth altered the internal alignment, reducing cleara

    enough to generate the contact.

    From our inspections of the dismantled machine, a possible r

    cause of this problem could have been the continuous formation

    deposits in the compressor seals or ingress of foreign debris l

    pieces of the strainer found attached to the rst stage impeller. O

    Piece of suction strainer found attached at impeller eye.

    Severe rub at discharge of lab. seal at 1st stage impeller 

    Solid deposits found inside and outside the cylindrical inner bundle

    (cartridge casing) where rotor and stationary internals are assembled.

    Cracks were found on diaphragm (top and bottom half).

    Figure 9: Compressor sectional drawing showing key areas of trouble.

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    case history

    accumulation of these deposits exceeded the available

    clearance, a friction rub could be developed at one point of

    the shaft surface, causing an increase of the shaft surface

    temperature and subsequent shaft bowing.

    REFERENCES:

    1.  Bently Nevada Corporation “Machinery DiagnosticCourse”. Figure 3.

    2.  Arthit Phuttipongsit (Principal Engineer) “The Morton Effect and Light Rubs in Rotating

     Machinery”. ORBIT Vol.27 No.1 2007.

    BIBLIOGRAPHY:

     Ronald L. Eshleman “Machinery Vibration Analysis” Vol-

    ume II: Analysis and Correction. Vibration Institute 2002.

    SPRING 2016 VIBRATIONS  2

     All inter-stage labyrinths have heavy contact mark 

    Rub observed at balance drum area 

    Solid deposits on labyrinths seals.

    Piece of suction strainer lost in 2013 found

    trapped between case and bundle.

    Figure 10: Shaft centerline position from July 2013 to February 2015.

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    22  VIBRATIONS SPRING 20

    newly certied

    CATEGORY I

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    Paul Morgan; Donald Robb; Ali Abdullah

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     SPRING 2016 VIBRATIONS  2

    newly certied

    Yahya Alamri; Khaled Saad Al-Ghamdi; Mark Anthony Silvallana

    Banal; Willman R. Pinto Flores; Francisco Gerardo Sosa De Los Santos;Francisco Javier Sanchez Olivares; Jesus Tellez Reyes; Raul Leana

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    John Paul Anderson; Edwin Evaristo Tapia Chuquimamani; Yahia A

    Abdelhamid Ismail; Hongxing Wang; Gian Carlos Reyes; Elia Doretto;Eduardo Aguilar Armendariz; David Martinez Cantera; Jorge Angel

    Saenz Serdio; Juan Carlos Serrano Orozco; Carlos Galan; Cesar Orlando

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    Albassam; Chellaiah Ganesh; Philippe Athanasiadis; Matias Canedo;

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    Mayor; Frederic Micco; Hans Claudius Reiss; Stefano Trono; Kyle

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    Joseph; Zhen Zhang; Han-Yuan Chu; Ke Tan; Jian Gao; Chengzhong

    Gu; Jiang Wang; Thomas Jerimy McDowell; Shivakumar Swaminathan;

    Michael Supplee; Michael Merten; Sudhar Rajagopalan; Ahmed Rifaat

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    VI headquarter update

    24  VIBRATIONS SPRING 20

    A fond farewell

    Two and a half years ago I sat down to an interview with members of the

    Vibration Institute’s Executive Committee to discuss my qualifications

    as a Director and the challenges that lie ahead as the leader of an organi-

    zation that serves the vibration community worldwide. In the time since, I’ve

    been honored to work closely with the Board of Directors to make some good

    and lasting changes that will continue to benefit our members and certifiedanalysts who call the Vibration Institute their professional association.

    It is with mixed emotions that I’ve submitted my resignation from the Vibra-

    tion Institute. Although just over two short years, I have thoroughly enjoyed

    the time I have spent at the Vibration Institute. I am appreciative of the trust

    the Board has given me, and have had a wonderful experience in my time with

    the Institute. My only regret is that I will not have the opportunity to be part

    of the continued progress being enjoyed by this time-honored organization.

    I have been tapped to lead a school and nature center in my home town of

    Eagle River, Wisconsin – an organization that is near and dear to my heart and

    played a signicant part in forging my love of the outdoors in my youth. My

    last ofcial day with the Vibration Institute was Friday, February 19, 2016.

    In the interim, until a replacement Director can be found, I trust in the skills

    and commitment of the Institute’s headquarters staff to be able to assist you in

    anything you may need. I have enjoyed my time with the Institute, and getting

    to know so many of you. I hope to see you on LinkedIn, and wish you all the

    best in your careers.

    Kindest regards,

    Robin Ginner

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