11statoilhydro_nordsve
DESCRIPTION
11statoilhydro_nordsveTRANSCRIPT
Classification: Internal
Flexible risers at Kristin
Flexible Pipelines and Risers PSA Norway 12.12. 2007
Nils Terje Nordsve, StatoilHydro
2
Kårstø
DraugenNjord
Ormen Lange
NyhamnaKristiansund
Trondheim
Stjørdal
Brønnøysund
Sandnessjøen
Harstad
Åsgard
Tjeldbergodden
Mikkel
SLP/UK
Heidrun
Kristin
* *
Alve
NorneUrd
Skarv
Idun
HammerfestDrift Nord
3
• Water depth: 320 m
• Reservoir pressure: 911 barg
• Reservoir temperature: 170 °C
• Production capacity
– Gas: 18.3 MSm3/sd
– Condensate: 20000 Sm3/sd
• Number of risers: 9
• Number of umbilicals: 5
Key data for Kristin
Photo: Trond Sigvaldsen
4
Kristin field layout
Grid North
P
R
P-211 Oil
export
N-101
P-101
S-101S-102
Kristin Semi
S-103/S-201
N
P-102/P-201
N-102/N-201
R-102
R-101
R-103/R-201
Fibre optical cable
S
To Åsgard FOC-1/B-401
Åsg
ard
Tran
spor
t P-
121
P-212 NP-212 S
P-212 Gas export loop
FORE
FORE
Åsgard C
S1
S2
S3 S4
FORE
AFT
STB
PORT
16”
Templateand wellslot ID’s:
Pigdirection
Not accessible
Permanent P&A
”S-4 target”
Tofte
Possiblesidetrack to existing N-3H well
10" ID prod (13% Cr.) w/ DEH12" oil export (CS)18" gas export (CS) Umbilical w/ 2" ID centre line3.5“ ID service line (CS)Fibre optical cable (FOC)Direct el. heating (DEH) risersFuture tie-in hubSSIVROV operated ball valveCheck valveDiverless hot tap teeTemporary pig launcher
Completed well
Completion ongoing
Drilled and cappedwell
Drilling commenced
Planned well
Spare well slot
Not available well slot
5
Kristin risers – historical account until early November 2006
• The export risers were parked on seabed in October 2004
• The flexible risers were tied back to the platform in April to June 2005
• Annulus vacuum testing performed in May/June 2005 confirmed thatall risers were intact after installation
• First production took place 3rd November 2005 (through S-101)
• Problem with one riser detected early November 2006 (S-101)
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End fitting
Normal gas permeation
Water spray
Leakage detected early November 2006
by annulus vent monitoring system
Rapid pressure build up
Valve opens automatically to release gas when pressure gauge measures 0.5 barg
Gas
dif
fusi
on
or
leakag
e t
hro
ug
h p
oly
mer
lin
er
Air
pressure
1.7 barg
7
Kristin riser S-101 – early work done to identify damage
• Supposed reason was leakage of hydrocarbons from riser bore through the pressure sheath into annulus
• Riser S-101 was depressurized down to ambient pressure
– Frequent pressure relief of annulus continued after ambient pressure was achieved
• The pressure in the riser was increased to 80 bar; the riser remaining out of service
• The pressure in the Riser Guide Tube was reduced to ambient pressure
– Frequent pressure relief of annulus ended
=> The phenomenon was due to leakage in the outer sheath
7.5
m
20.5
m20
.5 m
RG
T w
ater
leve
l
17 m
1.0
m
Cast insert
Water spraying
(prod. risers only)
RGTs pressurised to ~
1.7 barg (P &GE risers)
8
S-101 – Test to determine location of damageTesting was carried out 20th to 21st November 2006
7.5
m
20.5
m20
.5 m
RG
T w
ater
leve
l
17 m
1.0
m
Cast insert
Damage
location
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Kristin risers – damages detected• Scheduled vacuum tests in November 2006 showed that all export risers were
intact
• Vacuum tests in December 2006
– Damage to four risersconfirmed:S-101, R-101, R-102 andP-211A
– Damage to riser S-102detected May 2007
10
Consequences of damage• Tensile armours are exposed
– Possible wear against RGT inner surface
– Corrosion fatigue in aerated sea water
• Riser calculated fatigue lives in aerated sea water
– Production risers: Five to eight years
– Condensate export riser: 2.5 years
– Gas export risers: Six months
11
Potential causes – as evaluated at an early stage
• Possible material problem?
–TP-Flex™ is a new material
–Brittle behaviour?
–Bad wear resistance?
• Mechanical damage – due to inadequate Riser Guide Tubes?
–Surface roughness?
–Misalignment?
12
Material testing performed
• Fatigue of tensile armours
• Tensile testing of outer sheath
• Wear testing of outer sheath
Fracture
13
Preliminary wear test results of outer sheath materials
Con
tact
pre
ssur
e
Wear depth
Riser RGT•Testing carried out for 0.13 to 2.0 MPa contact pressure
•Wear rate varies linearly with contact pressure
•TP-Flex wears faster than Rilsan (dry and wet)
•Both materials wear faster wet than dry
•Largest difference between Wet TP-Flex and dry Rilsan
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Roughness typically measured with profile print-outs at three points for all bellmouths
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Kristin vs. Åsgard B guide tube solution
Kristin, vertical + 5° bend Åsgard, straight 5° inclined
Hang-off at
Riser balcony
Contact force difference:
∆ load=sin 5°x50 tonnes=4.5 tonnes
KRIÅSG B
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Wear protection collars at Værnes
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Installation of wear protection collars
1. Mount clamp anti-sliding clamp (A) on riser
2. Install collars consecutively; neck down
3. Mount extra locking clamp (B) on neck of lowermost collar
4. Hang clump weight on lowermost collar
5. Release and remove anti-sliding clamp (A)
6. Release collars from clump weight
7. Collars will then slide into the RGT driven by buoyancy
1
2
3
28/42
29/43
30/44
A
B
ROV handles
Locking mechanism
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Wear protection collars on R-101 entering RGT
19
Experiences from installation of wear protection
• Practice makes perfect:
–From more than one hour per collar to typically four collars per hour
• Due to friction against the RGT the collars may stop on their way upwards:
–Will eventually move during rougher seas
–Tilting the platform and/or adding buoyancy would help
• One some collars the locking mechanism opened
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Examples of wear protection collars that have opened
P-211A
P-212S
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16 collars missing on riser P-212N
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Lost collar - Picture taken after recovery
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Wear protection collar – locking mechanism
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Dry riser repair• Project with Aker Reinertsen
–Kick-off 28th March 2007
–First riser repaired 20th August 2007
• Complex project with short execution time
• Close co-operation between the
parties involved was required
Cheap
Safe
Fast
25
Damage to riser P-211A before cut-out for welding
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Damage to the R risers before cut-out for weldingR-101 R-102
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Damage to the S risers before cut-out for welding
S-101 S-102
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Connection of patch to outer sheath
By Sikaflex By welding
R-102
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Application of heat shrink R-102
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Temporary offloading of condensate during repair of P-211A
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Summary of damages and repairs
• Damages were detected as follows:
– S-101: 5th November 2006
– R-101: 19th November 2006
– R-102: 25th November 2006
– P-211A: 16th December 2006 (vacuum test – OK in November)
– S-102: 11th May 2007
• Repair carried out:
– R-102 repaired 20th August 2007; second time 5th October 2007
– S-101 repaired 28th August 2007
– P-211A repaired 10th September 2007
– R-101 repaired 18th September 2007
– S-102 repaired 25th September 2007
32
New risers
• Contract with Technip:
–Delivery 01.09.2008
–6 new risers (1 x condensate export, 1 x gas export, 4 x production)
• Outer sheath material:
–Rilsan for all risers
–Rilsan protective sheath in RGT area
–Cooling of production risers required for flow temperatures exceeding 92°C
• Wear protection collars most likely to be used for new risers
33
Lessons learned so far• Damage is due to wear rather than fracture
• Rilsan has better wear resistance than TP-Flex
• Wear resistance is better dry than wet
• Riser Guide Tubes are important
– Geometry
– Inner surface condition
• Riser configuration is important
• Locking mechanism of Wear Protection Collars is crucial
34
Concluding remarks• Wear protection collars installed on all risers
• Problems with the locking mechanisms encountered
– Design changed
• Fast track repair project
– All suppliers have met schedule
– No HES incidents
• Work ongoing to clarify cause of damages
– Wear of outer sheath against inner surface of RGTs
– RGT geometry?
– Riser configurations?