an evaluation of blockage corrections for a helical cross-flow turbine

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An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine Robert J. Cavagnaro and Dr. Brian Polagye Northwest National Marine Renewable Energy Center (NNMREC) University of Washington Oxford Tidal Energy Workshop April 7, 2014

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An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine. Robert J. Cavagnaro and Dr. Brian Polagye Northwest National Marine Renewable Energy Center (NNMREC) University of Washington. Oxford Tidal Energy Workshop April 7, 2014. Motivation. - PowerPoint PPT Presentation

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Page 1: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

An Evaluation of Blockage Corrections for a Helical Cross-Flow

Turbine

Robert J. Cavagnaro and Dr. Brian PolagyeNorthwest National Marine Renewable Energy Center

(NNMREC) University of Washington

Oxford Tidal Energy WorkshopApril 7, 2014

Page 2: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Motivation NNMREC has developed a “micropower” turbine for providing

power to co-located oceanographic equipment Understand hydrodynamics of the full-scale turbine by testing

at lab scale Determine if corrections rectify variable turbine performance at

different testing facilities

Lab-scale – high variability of performance with velocity and facility

Field-scale – limited variability of performance with velocity

Blockage Ratio

Page 3: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Micropower Rotor Parameters High-Solidity, Helical Cross-flow

turbine N: Number of blades (4) H/D: Aspect Ratio (1.4) φ: Blade helix angle (60o) σ: Turbine solidity (0.3) Hydrofoil: NACA-0018 Lab (1/4) scale

H = 23.4 cm, D = 17.2 cm, c = 4.0 cm Field Scale

H = 101.3 cm, D = 72.4 cm c = 17.3 cm

DNc

Page 4: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Performance Characterization Experiments

Adjustable resistive load bank and power monitoring

Direct rotor torque measurement

Angular position measurement Inflow and wake velocity

measurement Upstream & downstream

Acoustic Doppler Velocimeters

Thrust measurement

Tow vessel

Tow line (~100 m) Skiff (w/ load bank)

Rotor

Upstream ADV

Generator & gearbox

Skiff attachment

Torque sensor & encoder

Page 5: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Field Experiment Implementation

Wake Characterization ExperimentTurbine Integration with Skiff

Page 6: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Performance Characterization Experiments

Torque control with particle brake

Reaction torque measurement

Angular position measurement

Inflow velocity measurement Upstream ADV

Thrust measurement

Scale support cage

UW Flume

Load cell

Page 7: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Experimental Facilities

8.05.0

19.015.0

Flow speed (m/s)

Blockage Ratio

35.02.0 FrFroude number

Turbulence Intensity

UW Aero Flume

1.15.0

09.0

Flow Speed (m/s)

Blockage Ratio

4.02.0 FrFroude number

UI U

Turbulence Intensity

Bamfield Flume

Reynolds Number Reynolds Number54 1010 cRe

54 1010 cRe

Cross Section (m2)80.0

Cross Section (m2)35.0

ghUFr

%10 %4

Channel

RigTurbine

AAA )(

Page 8: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Blockage Corrections

Corrections rely on various experimental parameters

TU 2U

3U

WACA

TAT

h

1U

3

F

TPP UUCC

TF

F

TTF UU

3

F

T

P

PTF CC

UU

TF PP CC TF UU TF

Page 9: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Blockage Corrections: Glauert (1933)

Becomes unstable for CT ≤ 1

TU 2U

3U

WACA

TAT

h

1U

T

TTF C

CUU14

1

Page 10: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Blockage Corrections: Pope & Harper (1966)

TU 2U

3U

WACA

TAT

h

1U44

1 C

Tt A

A

“… for some unusual shape that needs to be tested in a tunnel, the authors suggest…”

)1( tTF UU

Page 11: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Blockage Corrections: Mikkelsen &Sørensen (2002)

TU 2U

3U

WACA

TAT

h

1U

Extension of Glauert’s derivation, constrained channel LMADT

uCuUU T

TF 41

12)23()1( 2

u

T

W

AA

Page 12: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Blockage Corrections: Bahaj et al. (2007)

TU 2U

3U

WACA

TAT

h

1U

Iterative solution of system of equations, incrementing U3/U2

Assumes U1, ω, T are same in tunnel and open water

Page 13: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Blockage Corrections: Werle (2010)

TU 2U

3U

WACA

TAT

h

1U

Constrained channel LMADT

2max, )1(27/16

PC

02

0 )()1( PP CC

Also reached by Garrett & Cummins, 2007 and Houlsby et al., 2008

Page 14: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Case 1: Lab to Field ComparisonSame flow speed (1 m/s), different blockage

Lab0 09.0

LabcFieldc ReRe ,, 4

Field

No thrust measurements for lab test case at 1 m/s

Page 15: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Case 2: Performance with Varying BlockageSame flow speed (0.7 m/s) at different facilities

Pope & Harper

Bahaj et al.

Werle

Page 16: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Case 3: Performance at Varying SpeedSame blockage ratio and facility 15.0

Pope & Harper

Bahaj et al.

Werle

Indicates strong dependence on Rec at low velocity

Page 17: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Reynolds Number Effect

54 1010 UcRec

Approximate Local Velocity

Sheldahl, R. E. and Klimas, P. C., 1981, “Aerodynamic characteristics of seven airfoil sections through 180 degrees angle of attack for use in aerodynamic analysis of vertical axis wind turbines,” SAND80-2114, March 1981, Sandia National Laboratories, Albuquerque, New Mexico.

Page 18: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Angle of Attack Variation

cossintan 1

Tip Speed Ratio

Angular Position

U

R

Page 19: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Significance of Dynamic Stall

Range of α at position of maximum torque along each blade

4105xRec

Page 20: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Conclusions Determining full-scale, unconfined hydrodynamics

through use of a model may be challenging All evaluated corrections reduced scatter of lab scale

performance data Thrust measurements may not be needed to apply a

suitable blockage correction

Caution is needed when applying blockage corrections Especially for cross-flow geometry

No corrections account for full physics of problem

Family of performance curves at low speed likely due to performance at low Reynolds number and dynamic stall

Page 21: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

AcknowledgementsThis material is based upon work supported by the Department of Energy under Award

Number DE-FG36-08GO18179.

Funding for field-scale turbine fabrication and testing provided by the University of Washington Royalty Research Fund.

Fellowship support was provided by Dr. Roy Martin.

Two senior-level undergraduate Capstone Design teams fabricated the turbine blades and test rig.

Fiona Spencer at UW AA Department and Dr. Eric Clelland at Bamfield Marine Sciences Centre for support and use of their flumes.

Robert Cavagnaro is supported by the Department of Energy (DOE) Office of Energy Efficiency and Renewable Energy (EERE) Postdoctoral Research Awards under the EERE Water Power Program administered by the Oak Ridge Institute for Science and Education (ORISE) for the DOE. ORISE is managed by Oak Ridge Associated Universities (ORAU) under DOE contract number DE-AC05-06OR23100. All opinions expressed in this presentation are the author's and do not necessarily reflect the policies and views of DOE, ORAU, or ORISE.

Page 22: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Bahaj, a. S., Molland, a. F., Chaplin, J. R., & Batten, W. M. J. (2007). Power and thrust measurements of marine current turbines under various hydrodynamic flow conditions in a cavitation tunnel and a towing tank. Renewable Energy, 32(3), 407–426. doi:10.1016/j.renene.2006.01.012

Linear Momentum Theory, Actuator Disk Model

Solved iteratively by incrementing ratio of bypass flow velocity to wake velocity (U3/U2)

Free-stream performance and λ derived from velocity correction

Where U1 is the water speed through the disk

Depends on inflow velocity, blockage ratio, and thrust

4/)/(/2

1

1

TT

T

F

T

CUUUU

UU

)1)/(()1)/((11

23

223

2

1

UU

UUUU

1

2

3

2

1

2

3

2 UU

UU

UU

UUT

1)/(

1

223

2

UUCU

UT

T

Blockage Corrections: Bahaj et al. (2007)

Page 23: An Evaluation of Blockage Corrections for a Helical Cross-Flow Turbine

Induction & Wake

Flow direction