chiller retrofit case study hertz 600 vine center

44
Bill Balli Donny Knight DeBra-Kuempel Chiller Group Chiller Retrofit Case Study HERTZ 600 VINE CENTER

Upload: others

Post on 02-Feb-2022

4 views

Category:

Documents


0 download

TRANSCRIPT

Bill Balli Donny Knight DeBra-Kuempel Chiller Group

Chiller Retrofit Case Study

HERTZ 600 VINE CENTER

2021 ICE Group Meeting

Presentation Summary

Project Background 1 Demolition, Retrofit, & Startup 4

Bidding Process 2 Energy Savings & ROI 5

Design Considerations 3 Outcomes & Learnings 6

2021 ICE Group Meeting

Project Background

2021 ICE Group Meeting

Hertz Investment Group @ 600 Vine Center

2021 ICE Group Meeting

Hertz Investment Group @ 600 Vine Center

Project Background

Walked into conversation at shop

– How to get chillers in penthouse of high-rise?

Hertz Investment Group in downtown Cincinnati, OH

Two 800-ton Carrier 19EB Chillers

– Located on 31st floor penthouse back of building

– Maintained since install by Carrier

2021 ICE Group Meeting

Bidding Process

2021 ICE Group Meeting

Bidding Process

DeBra Bid

Started out leveraging Turbocor TT400

– Need six total to reach tonnage req.

Contacted SMARDT

– Inquired utilizing VTT Compressor

– Similar to a parallel job, University of Cincinnati

Quoted

– Two VTT Compressors w/remote drives

– Kiltech control panel

2021 ICE Group Meeting

Bidding Process

Competition Competitive Bids

– Daikin McQuay w/four 400-ton WMCs

Complete Mechanical Changeout

– Pumps

– Chillers

– Controls

Space Limitations

Daikin contacted customer

– Warned that DeBra retrofit would not work (Due to Oil & Compressor size)

2021 ICE Group Meeting

Design

Considerations

2021 ICE Group Meeting

Design Considerations

Approach Philosophy

– Lots of moving parts

– KEEP IT SIMPLE

Retrofit Considerations

– Cost of Rigging

– Cost of New Chillers

– Customer ROI

– Space of Mechanical Room

– Excessive Noise/Vibration

– Minimum tonnage turndown

– Condition of Tube sheets

– Factory Economizer / Floats Vs. EXV

Two Turbocor VTT compressors w/remote drives mounted on chiller near control panel

– New control panel

– Retube Cooler & Condenser

– Factory Economizer / Floats Vs. EXV

– Installed distribution panel in replacing Wye Delta starter

Interfaces with BAS

Large Energy Savings

Thought Process Actual Build

2021 ICE Group Meeting

Demolition, Retrofit,

& Startup

2021 ICE Group Meeting

Two Identical Chillers in Penthouse

Chiller No. 2 (behind No.1, Remains Stock) Chiller No. 1 (Full Retrofit)

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Started with:

Original Carrier 800 ton 19 EB

– 3600 lbs of R-12

– Subsequent field addition of Hot gas bypass

~35 years old

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

All condenser and chilled water piping to be removed

– Chiller was also going to be completely retubed

Small 3-foot walkway between Housekeeping Pad & Tower

Notice that it sat on airbags to mitigate noise/vibrations

3 Feet

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Starting Point

Overhead rigging had to be fabricated.

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Tear Down

View after the motor and most of the compressor has been removed

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Tear Down

Everything removed

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Tear Down

Oil pump was removed

Traced all oil lines out of the shell

– Some of the oil/refrigerant lines go through the uni-shell

Note:

– Still on airbags

– Original Tubes

– No economizer work yet

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Tubes Removed

Added access windows

– Every condenser support sheet broke during tube removal

Dropped machine down

– Easier access to control panel

– Lowered overall height

Dropped

machine down

Added

windows

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

These are the holes we cut to gain access to the tube sheets.

As it turns out, the shell was one-inch thick.

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Welded support sheets

These are the condenser tube sheets after they were welded in

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Inside the Economizer

Keeping it simple…

Rebuilt original floats as opposed to installing electronic expansion valves

Float had worked for 35 years. Not broken – don’t fix it

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Start of Fabrication

Fabricated the suction, discharge, and economizer headers

Notice that we re-welded the condenser covers

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Test Fit of Compressors & Headers

Rigging used to set compressors

– Fabricated spreader bars for the compressors

Spreader Bar

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Both compressors Fabbed

Note the tubes are installed and the tube sheets have been coated with Belzona

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Wiring & Ancillary Piping

Electricians installing main power

– Sensor cabling

Liquid injection and economizer lines

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Compressor Table

Pipefitters fabbed a plate for the compressor to sit

– Bolted the suction and discharge flange prior to drilling the compressor feet

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Hot Gas Bypass

Incorporated hot gas bypass into overall controls strategy

Installed all new electronic flow switches

Removed the original DP switches – Installed thermal

displacement switches

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Both economizer and liquid feed for the motor cooling were built from fabricated headers

Liquid injection header

Added Caps to shell (orig. refrig./oil circuitry through shells)

Liquid

Header

Economizer

Header

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

The discharge 90’s off the compressor were back-ordered

Had to set the distance of the headers which made the center-to-center on the headers off.

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Close to Complete

Used Kiltech Panel

Original design had VFD’s next to Kiltech Panel to keep refrigerant piping and wiring nearby – Customer wanted drives

relocated to wall behind for spacing

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Relocated the VFD’s on the wall behind the chiller instead of the original location

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Finished Product

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Before

After

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

Before

After

2021 ICE Group Meeting

Demolition, Retrofit, & Startup

2021 ICE Group Meeting

Energy Savings &

ROI

2021 ICE Group Meeting

Energy Savings & ROI

Estimating cost savings:

– Original flow meters not functioning

– Chiller No. 2 “building’s best running machine”

– Measured old Machine…

Unit Operation Design (GPM) Actual (GPM)

Condenser 2400 2897

Evaporator 1200 1837

2021 ICE Group Meeting

Savings Estimate

Retrofit running at design conditions yields estimated $60k-$80k annual savings

Accounting for Condenser Relief, savings increase further

Design Carrier

(100%)

Retrofit

(100%)

Carrier

(50%)

Retrofit

(50%)

Retrofit

Condenser Relief

@ 65 degrees

Motor Amps 797 800 632 412 294 105

kW/Ton 0.7172 0.8690 0.5772 1.1745 0.4558 0.2363

Evaporator Tons 795 689 810 283 480 275

2021 ICE Group Meeting

Outcomes &

Learnings

2021 ICE Group Meeting

Lessons Learned – What went WRONG?

COVID-19 – Virtually all parts had extended lead-times shipping internationally

Drive Location Challenges – Customer wanted panels installed in different location than design

– Had to absorb cost of change within budget

– BE SPECIFIC. Outline all inclusion/exclusion assumptions

Every condenser tube support sheet broke – Had to cut windows for access

Underestimated spacing constraints in Penthouse – Needed to stage all equipment in lower floors – significant hours spent in the elevators

2021 ICE Group Meeting

Lessons Learned – What went WELL?

Every condenser tube support sheet broke

Utilized similar job at UC for reference – Startup was extremely smooth

Performance exceeds expectations

Won maintenance contract – Previously performed by Carrier past ~35 yrs

High likelihood of second machine win – Design work can be mirrored for second machine

Thank You