doi sach cho phe pham duc ap luc

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  • 8/2/2019 Doi Sach Cho Phe Pham Duc AP Luc

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    Summary

    The aluminum die casting enables to build precise products with high productivity in short cycle

    even if the product shape is complicated and thin. However, a process of filling up the hot molten

    metal speedily grows high load to the die, causing problems such as core pin breakage and mold

    breakage, resulting into disturbance to the MP operation. In order to eliminate the pin breakage, the

    engineers thoroughly investigated and analyzed the actual products on site and understood the

    mechanism of the pin breakage due to seizure. Then the pin design standard was optimized using

    Quality Engineering and adopted to the mass production. This improved the MP operation. Moreover,

    by conducting design operation with the optimized standard, the MP preparation process without re-

    designing was achieved.

    Optimization of Die-Design Standard for Core Pin

    1

    2

    Takashi O zeki Yusaku M urao

    28

    1

    Fig.1

    12 Pow ertrain Production E ngineering D ept.

    Fig.1 Die-Casting

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    2

    A

    Fe-A l-SiB

    Fig.2C

    D

    E

    Fig.3

    3

    Fig.4

    Table 1

    4

    4.1

    8

    L18T able 2

    4.2

    Fig.2 Fe-Al-Si Compound Layer

    Fig.3 Pin Breakage by Burning of Aluminum

    Fig.4 Relation of Surface Area-Load

    Table 1 Noise Factor

    Table 2 Control Factor and Level

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    Fig.5

    5

    5.1

    Fig.6

    A

    B

    L18

    5.2

    SN

    T able 3

    SN Table 4

    Fig.78

    5.3 Fig.78SN

    Fig.5 Experimentation

    Fig.6 Relation of Surface Area-Load

    Table 3 Analyses Data

    Table 4 S/N Ratio, Sensitivity Calculation Result

    Fig.7 Response Graph S/N Ratio

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    Table 5SN

    6

    6.1

    Fig.9

    E

    6.2

    Fig.78SN C

    CE

    D

    6.3

    650kgf3,000kgf

    600kgf1,000kgf

    Fig.10

    L18

    Fig.1112

    Fig.8 Response Graph Sensitivity

    Table 5 Confirmation Test Result

    Fig.9 Test Result

    Fig.10 Relation of Surface Area-Load

    Fig.11 Response Graph S/N Ratio

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    Fig.1112SN

    Table 6

    SN

    SN 6db

    1/4

    CE

    2db

    30

    7

    78

    50

    V ol.15p.91-961999

    Fig.12 Response Graph Sensitivity

    Table 6 Confirmation Test Result