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    58 ORBIT Vol .28 No.1 2008

    CASE HISTORY

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    Vol .28 No.1 2008 ORBIT59

    CASE HISTORY

    n ethylene plant experienced a vibration isse after start-p of a mlti-nit chare as train

    followin a relatively short mitiation otae in Ast 2006. The chare as compressor

    has five staes of compression via three different compressor bodies. All three are driven by

    a 35,000 hp steam trbine with a desin speed of 5,300 rpm (Fire 1). The compressors were

    oriinally installed in the late 1960s and still had the oriinal floatin oil rin desin and

    lbricated ear coplins. The rotors had been praded with rb-tolerant internal seals and spherically

    seated tilt-pad bearins.

    The short dration of the otae limited the wor scope to overhals of the A and C compressor bodies

    only. The C compressor had exhibited performance problems thoht to be cased by folin, while the

    A compressor was overhaled as a reslt of recent vibration isses. The B compressor was not opened p

    becase it had no mechanical or performance problems. The inboard bearin on the dischare end of the

    B compressor (bearin 5) was chaned becase it was felt that the clearance had increased.

    The train is monitored via a Bently Nevada* 3500 series machinery protection system and all critical trains

    in the ethylene nit were connected to Bently Nevada Data Manaer* 2000 (DM2000) software to provide

    continos condition monitorin and machinery dianostic capabilities. For increased

    data collection resoltion, an ADRE* portable data acisition system was sed to captre

    shtdown and startp transient data and ament the data available

    from the online software.

    Dianosin

    Wallace E. (Ed) Wilcox, P.E. Staff Machinery Enineer Chevron Enery Technoloy Company [email protected]

    a coplin problem on a chare as trainHow vibration data and a loical process of elimination saved millions in downtime

    The eThylene unIT deTaIled In ThIs case

    hIsTORy has suBsequenTly Been upgRaded

    TO sysTem 1* sOfTwaRe whIch addResses

    many Of The daTa ResOluTIOn lImITaTIOns

    ThaT weRe InheRenT In dm2000 sOfTwaRe.

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    60 ORBIT Vol .28 No.1 2008

    CASE HISTORY

    5Y 5X2Y 2X1Y 1X 6Y 6X

    7Y 7X4Y 4X3Y 3X 8Y 8X

    CompressorBody C1 2

    3 4

    4

    5 6

    7 8Compressor

    Body B

    CompressorBody A

    35,000 hpSteam Turbine

    View as seen from turbine lookingtowards driven machines

    421 1T 53

    Figure 1. Machine train diagram o charge gas compressor train showing A-B-C compressor bodies,fve compression stages, and proximity probe arrangements or all eight radial bearings.

    Problem

    Approximately 10 mintes after the chare as

    compressor train was restarted followin the otae,

    radial vibration on the B compressor increased rapidly.

    Althoh the speed remained basically nchaned, the

    radial vibration went from 0.5 to over 3 mils, as can be

    noted in Fire 2. This increase in vibration occrred

    immediately after the compressor train sred. Note

    the lare increase in vibration amplitde even thoh

    the speed remained relatively constant on the riht sideof Fire 2. The vibration amplitde contined to rise

    after startp as the load on the compressor train was

    increased in response to increasin nit rates.

    Overall amplitdes had reached approximately 4.5

    mils by early September with a short excrsion in

    late September above 5.5 mils.

    Figure 2. Bode plot o bearing #6 y-probe during

    start-up on 8/27/06. Note substantial change

    in vibration amplitude while speed remains

    essentially constant at approximately 4,300 rpm(region enclosed by the red oval). The blue cursor

    position shows the frst balance resonance or

    this machine occurs at about 2400 rpm.

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    Vol .28 No.1 2008 ORBIT61

    CASE HISTORY

    Vibration Analysis

    Analysis of the problem was essentially a process of

    elimination whereby the available data was examinedto systematically determine what was not casin the

    vibration. Five separate malfnctions where considered.

    1. Unbalance

    An initial assmption by plant operations personnel

    was that the hih radial vibration on the B compressor

    was cased by nbalance. This assmption was not

    withot basis since olefins chare as is considered

    to be a folin service. In particlar, this compression

    train had experienced heavy folin several years in

    the past. Two other factors spported this assmption.

    First, as previosly mentioned, the C compressor was

    overhaled drin the otae and some folin was

    fond. Second, the B compressor was the only case

    not opened drin the otae, so its cleanliness was

    nnown. While most of the vibration was indeed

    occrrin at the rnnin speed (1X) of the compressor,

    nbalance was not the major contribtin case of

    the problem. This was ascertained by notin that the

    lare increase in amplitde on the riht side of Fire 2

    had occrred at relatively constant speed. While it was

    possible that some folin material cold have been

    thrown off one of the impellers resltin in a sdden

    chane in balance, this wold have been accompanied

    by a sdden phase shift. However, Fire 2 shows that

    no sch phase shift occrredthe phase remained

    constant at approximately 215, eliminatin nbalance

    as the case of the lare observed increase in vibration

    amplitde. To lend additional credence to this concl-

    sion, an acceptance reion plot (i.e., trend of amplitde

    and phase sin polar coordinates) of the bearin #6

    y-probe was examined for a data rane encompassin

    the two wees after startp. It showed that the synchro-

    nos phase anle was almost constant (Fire 3).

    Figure 3. Bearing #6 y-probe acceptance region plot or 2-week period between 8/25/06 and 9/7/06 showing

    an essentially constant phase angle o 215.

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    62 ORBIT Vol .28 No.1 2008

    CASE HISTORY

    2. Locked oil seals

    The possibility also existed that the floatin rin oil

    seals cold have loced in an eccentric position, actin

    as additional rotor spports instead of jst the jornal

    bearins. However, this type of problem wold have

    ndobtedly exhibited some sb-synchronos vibration

    peas in the spectrm, becase of the oil whirl that

    wold be present in the seals at this speed. Examination

    of the spectral data showed that the vibration was

    almost entirely at 1X and had no sb-synchronos

    components. Conseently, loced seals were extremely

    nliely. Additionally, loced seals typically affect the

    rotors natral freencies becase they effectively

    redce the rotors span between spports and ths

    increase its stiffness. Had a chane in the compressors

    1st balance resonance been noted (particlarly an

    increase), this wold have pointed toward the oil seals.

    However, comparison of the Bode plot collected prior

    to the shtdown (Fire 4) with that taen drin the

    post-otae startp (Fire 2) showed that the rotors

    first balance resonance had not chaned. Combined,

    the lac of sb-synchronos freency components

    and no observed chane in the first balance resonance

    eliminated loced oil seals from frther considerationas a liely root case.

    3. Cracked shat

    A craced shaft will normally be indicated by a decrease

    in shaft stiffness that reslts in a noticeable (and

    sometimes sbstantial) redction in the rotors critical

    speed. As noted previosly by comparin Fires 2 and

    4, the rotors critical speed measred prior to the otae

    was essentially nchaned from that measred after

    the otae, main a craced shaft very nliely.

    4. Internal rub

    In contrast to a craced shaft, a hard rb on internal

    seals will normally increase the critical speed becase

    of the redced span between rotor spports, since the

    seals are now actin as asi-bearins. For the same

    reasons listed above, the lac of chane in the first

    balance resonance between the pre-otae coastdown

    and post-otae startp data did not spport a rb

    hypothesis. Additionally, a rb wold normally be

    observable as flat spots or other anomalies in the

    shaft orbits. However, the shaft orbits (Fire 5)

    exhibited no sch evidence. Combined, this made

    a rb extremely nliely.

    Figure 4. Bode plot o bearing #6 y-probe on shutdown, 8/3/06, prior to the outage. The blue cursor positionshows the frst balance resonance or this machine occurs at about 2400 rpm, essentially unchanged rom

    the post-outage resonance o Figure 2.

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    Vol .28 No.1 2008 ORBIT63

    CASE HISTORY

    Figure 5. Bearing #6 orbit ater start-up

    showing no evidence o seal rub.

    5. Locked Coupling

    Althoh the chare compressor train had a history

    of loced coplin problems, these had not manifest

    for several years. After a maintenance trnarond

    several years prior, the radial vibration on the A and B

    compressors increased to approximately 3.5 mils, and

    at the time, it was assmed the problem was cased by

    coplin loc-p. However, the vibration had trended

    down to normal levels over time. Additionally, the

    coplins removed drin the Ast 2006 otae did

    show indication of wear between the end of the hbs

    and spacer, and for this reason were replaced with

    identical new components. The fact that the coplins

    were brand new seemed to rle ot the lielihood

    of coplin loc-p. Liewise, the alinment of the

    compressor had been checed and fond to be in ood

    condition. Measrements had been taen in the past

    that showed the thermal rowth assmptions in the

    cold alinment tarets were ood.

    For all of these reasons, the coplin was not

    immediately sspect.

    IN THIS SPECIFIC INCIDENT,

    THE ABILITY TO ACCuRATELY

    DIAgNOSE THE ROOT CAuSE

    ALLOWED MACHINERY

    PERSONNEL TO RECOMMEND

    A REDuCED WORk SCOPE.

    THIS SAVED APPROXIMATELY

    1011 DAYS OF LOST

    PRODuCTION WHEN

    COMPARED WITH A COMPLETE

    OVERHAuL THAT WOuLD

    HAVE BEEN REquIRED IN THE

    ABSENCE OF SuCH DATA.

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    64 ORBIT Vol .28 No.1 2008

    CASE HISTORY

    The first stron indication that the coplin miht be the

    problem afterall came approximately one wee after

    the startp. Becase of a overnor control oil problem,

    the trbine speed dropped rapidly (from approximately

    5000 to 3500 rpm in a few seconds). When this occrred,

    the overall radial vibration at bearin #6 dropped from

    approximately 4.5 mils to 0.7 mils. However, the speed

    retrned almost as icly as it had dropped, and the

    hih vibration retrned (Fire 6). Initially, this event was

    not that enlihtenin becase the 1X trend (see Fire 7)

    seemed to indicate that the synchronos amplitde and

    phase anle had not chaned maredly, in star con-

    trast to the chanes observed in the overall nfiltered

    vibration of Fire 6. However, after contactin gEs

    Bently Nevada Machinery Dianostic Services (MDS) per-

    sonnel, it was learned that the overall vale displayed in

    the DM2000 software is received directly from the 3500

    series machinery protection system and merely passed

    throh, while the 1X vale is calclated in the software

    from the raw vibration waveform. Since the chane in

    speed and vibration happened so rapidly, the DM2000

    softwares tracin filter was not fast enoh to captre

    this rapid excrsion. Ths, it seemed liely that the 1X

    amplitde and phase had in fact chaned alon with

    the overall nfiltered amplitde drin this excrsion.

    Figure 6. Rapid drop in bearing #6 y-probe unfltered overall vibration amplitude during speed upset.

    Note that ollowing the event, the amplitude returns to nearly the same level as prior to the speed upset.

    Figure 7. Same data as in Figure 6, but fltered to compressor running speed (1X).

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    Vol .28 No.1 2008 ORBIT65

    CASE HISTORY

    In an attempt to re-create the drop in vibration

    mentioned above, approximately one month after the

    otae, the compressor speed and load were decreased

    drin a redction in nit rates. Drin this test, an

    ADRE portable data acisition system was connected

    to the 3500 machinery protection rac as it provided

    hiher data resoltion than the DM2000 software.

    Becase the speed decrease was radal, there was

    no rapid decrease in vibration as seen earlier. However,

    drin the redction in nit rates, the compressor was

    accidentally sred and becase the ADRE system

    was connected, hih resoltion data was acired.

    Examination of this data showed that the synchronos

    amplitde had dropped rapidly drin the two sre

    events. Liewise, the synchronos phase anle had

    chaned as well (Fire 8). These facts pointed stronly

    to the lielihood that the coplin between the B and

    C compressors was loced in a riid condition, bt

    had momentarily broen free drin the sre event

    becase of the rapid flow reversal and sbseent

    relaxation of torsional loadin on the coplin.

    Figure 8. Bearing #6 y-probe 1X fltered amplitude and phase data collected during surge events on 9/28/06.

    Note high-resolution time span on horizontal axis (1 second per division) indicating that the back-to-back

    surge events occurred within approximately 10 seconds o one another.

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    66 ORBIT Vol .28 No.1 2008

    CASE HISTORY

    Examination of the shaft centerline plots of the #6

    bearin revealed that the jornal had dropped approxi-

    mately 2.0 mils drin the coast-down before the

    otae, bt had raised 4.0 mils drin the sbseent

    start-p (see Fires 9 and 10 respectively). This meant

    that the sction end jornal was ridin in the center of

    the bearin, instead of the lower half, since the desin

    bearin clearance was approximately 8 mils. The indica-

    tion was that somethin was liftin the B compressor

    sction end jornal off of its bearin. This was frther

    confirmed by examination of the bearin metal tem-

    peratres for bearin #6 (see Fire 11). As can be seen,

    the bearin #6 temperatre is approximately 15 coolerafter the mitiation otae, even thoh the vibration

    was obviosly hiher. In contrast, the bearin #7 tem-

    peratre was approximately the same before and after

    the otae, indicatin that no other external factors,

    sch as oil temperatre or ambient temperatres, were

    affectin the reslts.

    Figure 9. Shat centerline plot or bearing #6during pre-outage shutdown on 8/3/2006.

    Figure 10. Shat centerline plot or bearing #6during post-outage startup on 8/27/2006.

    THIS TEST WAS A FuRTHER

    CONFIRMATION THAT THE B

    COMPRESSOR ROTOR WAS

    BEINg LIFTED OFF BEARINg

    #6 BY A RIgID COuPLINg

    BETWEEN THE B AND C

    COMPRESSORS.

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    Vol .28 No.1 2008 ORBIT67

    CASE HISTORY

    Figure 11. Trend rom the plants process historian showing bearing #6 (red) and bearing #7 (blue)

    temperatures beore and ater outage. Note that the temperature o bearing #6 drops approximately 15

    degrees ater the outage, while the temperature o bearing #7 stays approximately the same. This helped

    corroborate that bearing #6 was more lightly loaded and riding more towards the center o its clearance

    (i.e., lower eccentricity ratio) ater the outage.

    Validation

    In an attempt to redce the radial vibration amplitde atbearin #6, and confirm that that the low jornal eccen-

    tricity was associated with the problem, an online test

    was condcted to chane the relative vertical alinment

    between the B and C compressors. The basic concept

    was to pll the B sction end jornal down frther in

    its bearin, thereby increasin its eccentricity and bear-

    in stiffness and redcin the radial vibration. This was

    accomplished by sin an air mover with water spray

    on the dischare foot of the C compressor, and a steam

    hose on the sction pedestal of the B compressor. The

    objective was to chane the alinment, lowerin the C

    case dischare end and raisin the B case sction end

    (Fire 12). Becase heatin and coolin effects were

    localized to the compressor spports, it did not chane

    the bearin hosin temperatre, which potentially

    cold have sewed the shaft centerline plots de to the

    probes rowin away from the shaft.

    The chanes had exactly the effect predicted. The shaft

    centerline plots of bearins #6 and #7 are shown in

    B Case C Case

    Cooling applied to C

    case dischargewobble foot

    Heat applied to

    B case suctionpedestal

    Figure 12. Graphical depiction o online alignment

    adjustments used to confrm the locked couplingpostulate.

    Fire 13. Liewise, the redction in radial vibration is

    shown in Fire 14. This test was a frther confirmation

    that the B compressor rotor was bein lifted off bearin

    #6 by a riid coplin between the B and C compressors.

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    68 ORBIT Vol .28 No.1 2008

    CASE HISTORY

    Figure 13. Steady-state shat centerline trends o bearings 6 (let) and 7 (right) showing eects o online

    alignment adjustments. The rotor moves downward in its bearing clearances or bearing #6 and upward or

    bearing #7.

    Figure 14. Drop in bearing #6 y-probe vibration during online alignment adjustment occurred exactly

    as predicted.

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    Vol .28 No.1 2008 ORBIT69

    CASE HISTORY

    The hih-resoltion data (Fire 8) taen drin the

    compressor sre showin the rapid synchronos

    phase chane, and the drop in vibration (Fire 14)

    observed drin the online alinment chane all

    indicated that coplin loc-p was the problem.

    Approximately two months after the otae, the overall

    vibration at bearin #6 was still trendin above 4 mils

    with occasional excrsions above 5 mils.

    Corrective Actions

    Another otae was planned in the winter months

    to address the vibration isse. De to the isolation

    reirements of the compressor, the coplins cold

    be chaned withot completely clearin the compres-

    sors. This wold allow the compressor to be ready for

    maintenance approximately one day after the nit was

    sht down. In contrast, if the case had to be opened,

    this wold reire a minimm of 4 days jst to clear

    the compressor cases before maintenance wor cold

    bein. The end reslt was that a coplin chane

    cold be accomplished with 3 to 4 days of interrpted

    prodction, while a complete overhal wold reire at

    least 2 wees, incrrin 10 or more days of additional

    downtime. While this made the coplin wor loo very

    attractive, the prospect of chanin only the coplin,

    restartin the compressors, and then discoverin that

    the hih vibration was still present was hihly ndesir-

    able. For this reason, some advocated the safe rote

    of a complete overhal. However, based on the clear

    indication of the coplin loc-p from the test data,

    the site machinery personnel were able to alleviate

    manaements concerns and redce the wor scope

    to that of jst replacin the coplins.

    Reslts

    The chare as compressor train was broht down

    and the last two ear coplins in the train were

    replaced with dry, flex-element style coplins. As

    expected, the vibration on bearin #6 retrned to

    normal levels of approximately 0.5 mils. Fire 15 shows

    the ear coplin removed from between the B and C

    compressor bodies. It clearly exhibits an abnormal wear

    pattern considerin it had only been in operation for

    approximately two months.

    Conclsions

    Chevron is increasinly sin condition monitorin data

    as an effective method of enhancin decision-main

    confidence and accracy, and the willinness of plant

    manaement to rely on this data when main operat-

    in and maintenance decisions is increasin as well. This

    case history was merely one example of more than half

    a dozen that the athor has compiled drin the last

    several years.

    In this specific incident, the ability to accrately dia-

    nose the root case allowed machinery personnel to

    recommend a redced wor scope. This saved approxi-

    mately 10-11 days of lost prodction when compared

    with a complete overhal that wold have been reiredin the absence of sch data. Each day of downtime typi-

    cally costs in excess of 200k uSD for this plant, meanin

    that several million dollars in savins were realized de

    to accrate and timely machinery data.

    * denotes the trademars or reistered trademars of Bently Nevada,

    LLC, a general Electric company.

    Figure 15. November 2006 photo showing

    replaced gear coupling between B and Ccompressor bodies. Abnormal wear is clearly

    evident ater only 2 months o operation.