ip’s lesson learned of geothermal power plant o&m · ip’s lesson learned of geothermal...
TRANSCRIPT
The Outline
Indonesia Power in Brief
Units Performance & Management
Unit 1 KMJ Rehabilitation Project
Layout of Unit 2-3 KMJ Life Extension Program
Ulumbu-Mataloko Geothermal Power Plant
Who Are IP?
PT Artha Daya Coalindo (ADC)
PT Cogindo Daya Bersama (CDB)
PT. Indo Pusaka Berau (IPB)
99,9%
100%
PT Perusahaan Listrik Negara (Persero)
(PLN)
SUBSIDIARIES
Unit JasaPemeliharaan
UPJPKamojang
UP MricaUP
SagulingUPJP Bali
UPJPPriok
UP Perak Grati
UP
Semarang
UP
Suralaya
UNITS
CDB Business
-Co-Generation
-Energy Outsourcing
-Energy Efficiency
-Assessment Package
ADC Business
- Coal Supplier &
- Distributor/Transportation
IPB Business
- Operating 14 MWe
CFPP
UJP
-SLY 8, BSR, Labuan,
-Pl Ratu, Adipala,
-Pangkl Susu, Baru,
- Jerajang, Ulumbu
VISION Sustainable and Trusted Energy Company
MISION Engage in Environmentally Friendly Power Generation Business and O&M Services
Geothermal PP
PLTP KAMOJANGDesa LaksanaKecamatan IbunKabupaten BandungJawa-BaratKetinggian : 1,500 dpl
GUNUNG SALAK GPPDesa PurwabaktiKecamatan PamijahanKabupaten BogorJawa-BaratKetinggian : 900 dpl
PLTP DARAJATDesa Padaawas, Kecamatan Pasir WangiKabupaten GarutJawa-BaratKetinggian : 1,700 dpl
PLTP ULUMBU (O & M)UlumbuNusa Tenggara Timur
GUNUNG SALAK GPP180 MW
KAMOJANG GPP140 MW
DARAJAT GPP55 MW
PLTP MATALOKO (O & M)MatalokoNusa Tenggara Timur
Installed Capacity
Installed Capacity Nett COD
(MW) (MW)
1 Kamojang 2 55 52.3 29-Jul-87
2 Kamojang 3 55 52.3 13-Sep-87
KAMOJANG GPP 110 104.6
3 Gunung Salak 1 60 56.5 12-Mar-94
4 Gunung Salak 2 60 56.5 12-Jun-94
5 Gunung Salak 3 60 57 16-Jul-97
GUNUNG SALAK GPP 180 170
6 Darajat 1 55 52 6-Oct-94
UPJP KAMOJANG 345 326.6
No. Units
Installed Capacity Nett
(MW) (MW)
1. Ulumbu ADB #1 2.5 2.5 14-Jul-14
2. Ulumbu ADB #2 2.5 2.5 14-Jul-14
3. Ulumbu APBN #1 2.5 2.3 9-Jun-12
4. Ulumbu APBN #2 2.5 2.3 4-Jan-12
PLTP ULUMBU 10 9.6
UnitsNo. COD
Performance Outline
UNIT YEAREAF(%)
EFOR(%)
SdOF(kali)
PROD(MWH)
SOLD(MWH)
HOUSELOAD
(MWH)
PLTP KAMOJANG2 & 3
2011 97.99 0.71 1.5 951,291 908,410 42,881
2012 94.33 0.18 2.0 894,261 854,826 39,435
2013 99.09 0.08 1.0 823,280 786,811 36,469
2014 99.16 0.14 1.0 798,697 763,840 34,857
2015 94.23 1.10 2.0 909,508 872,546 36,962
2016 99.42 0.17 1.00 627,332 599,778 27,554
EAF in average > 94% as per NERC Standard Target TOP KMJ (as per agreement with Pertamina) – 72.23% TOP KMJ in 2011 until 2016 (August) average reach – 75.94 % Considering only two operating units in 2015, TOP KMJ can still be achieved by
74.16%, including Simple Inspection (SI) & Shutdown Total (SDT)
Description: Data 2016 till August
Description: Data 2016 till August
-
200,000
400,000
600,000
800,000
1,000,000
1,200,000
1,400,000
2011 2012 2013 2014 2015 2016
TOP PLTP KAMOJANG 2 & 3
TARGET
REALISASI
TOP44,75%
Asset Management
Pertahanan
Failure Defense Task
Reliability Management
Pertahanan
Detect Failure
Condition Base Management Pertahanan
Risk Failure
Risk Management
Pertahanan
Mitigation of Failure
Outage Management
Pertahanan
Mitigation of Failure
WPC
Pertahanan
End of Life
Aging Asset Management
Pertahanan
Analysis and Opportunity
Continuous Improvement
Turbine Highlight
Roll-in/Roll-out strategy for every 24,000 operation hours Scaling problems :
Occurs on 1st & 2nd stage in form of Silica Occasionally, Ferrous deposit was found on GSL – solved with non-
oxygenated steam washing Common problems :
Failed shroud & seal strips Deformation on blade’s dove tail Plugging on condensate drain system
Double axial flow turbine
5 stage : 2 stage Impulse 3 stage Reaction
Nominal Capacity : 55,000 KW
rpm : 3000 rpm
Inlet Steam Press. : 6.5 bar abs
Outlet Steam Press. : 0.1 bar
Critical speed : 1 st 1700 rpm2 nd 3600 rpm
Generator Highlight
Inspection of generator rotor & stator in every 72,000 operation hours –scope of Major Inspection (MI).
Problems : Retaining ring – due to 1980’s design was MnCr 18-5 – replaced in 2006 Rewinding of stator – due to base load position on the grid Rotor winding reinsulation – due to environment & lifetime
Power : 68.750 KVA
Voltage : 11,800 KV
Current : 3364 A
Power Factor : 0,8 PF
Frequency : 50 Hz
Speed : 3000 rpm
Number of Phase : 3 Phase
Insulation Class : B
Stator Temperature : 790 C
Rotor Temperature : 900 C
Water Cooler Temp. : 320 C
U1 KMJ Rehab Project
STEAM TURBINE, ST-100DM-100DEMISTER
M CT-100
M
Generator Coolers
P-201
Lube Oil Coolers
P-202
CV-105A
CV-105B
CV-106A CV-106B
MAIN COOLING WATER PUMPS(NEW 2 x 50%)
P-101
P-102
PRIMARY INTERCOOLING WATER PUMPS(NEW 2 x 100%)
GEN-100
MCND-100CONDENSER
FR STEAM RECEIVING HEADER
VP-100
TO FLASH TANK
GENERATOR
VACUUM BREAKER
VACUUM BREAKER
SIPHON BREAKER
CV-107
CV-109
MSVRMSVL
GVRGVL
SE10160%
CV-111
MV-___
CV-___
1V-1
CV-____
STEAM TRAP
S
M
M
M
CV-101
SE10240%
SE10330%
1ST
STAGEICND100
(100%)
2ND
STAGEACND101
(100%)
1 X 100% LRVP w/ SEAL WATER
SEPARATOR
SP-100
GAS EXTRACTION
SYSTEM
COLD WELL OVERFLOW& DRAIN
BLOWDOWN VALVE
SE104
100%
A
B
A
BSS
Flow Meter
U1 KMJ Schedule
Contract Awarded : 21 Des 2015 – Project Duration 21 months EPC Period : 25 Jan 2016 to Mar 2017 Commissioning : Starting May 2017 COD : Oct 2017
U2-3 KMJ Life Extension
Life time power plant has been operating almost 30 years with high availability> 92%
Kamojang Power Plant currently supports West Java Electrical System,especially in Southern West Java Sub System
Kamojang PP regarded as one Green Power Plant that participate fordecreasing emission which has already awarded by GoI for the 8th times since2008
Remaining Life Assessment (RLA) has been carried out in Kamojang PP relatedto main equipment which can be used as prediction and clarification ofremaining life of equipment
Rehabilitation Program is necessary carried out for improving reliability,efficiency and modernization in control system in order to able to easy tooperate and profitable in long operation period
First it was going to be funded by JBIC, but now KfW taking over the financialmatter
Scope of U2-3 KMJ LEPU
nit
Ass
ets
Turbine System
Turbine Rotor & DiaphragmLife extension – improvement of efficiency
for output
Lube & Control Oil System Reliability improvement
Journal & Thrust Bearing Life extension
Generator System
Generator Rotor Renewal & rewinding for strategic operation
Exciter – AVR – GCBLife extension – modernization – reliability
improvement
Main Transformer 11.8/150 kV – Aux Transformer 11.8/6.3 kV
Reliability improvement – efficiency improvement
Auxiliary System
Cooling Water SystemImprovement CWP, CT, Pri & Sec Pump, Main
Cond, Intercooler
Gas Removing System Improvement Ejector, Aux Cond Flash tank
Main Steam SystemImprovement Rock Muffler, Separator,
Demister, IAC, MUIV
Control System
Plant DEHC Modernization – reliability improvement
Plant DCS – TSI – UPS Modernization
Ulumbu & Mataloko
Lokasi PLTP mataloko di desa Todabelu,
Kecamatan Golewa,Kabupaten Ngada,
Propinsi Nusa Tenggara Timur, berada
sekitar 16 km ke arah timur dari Kota Bajawa
Lokasi PLTP Ulumbu di
desa Wewo, Kecamatan
Satarmese,Kabupaten
Manggarai, Propinsi Nusa
Tenggara Timur