my home industries private limited. mellacheruvu cement...
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Renewable Energy & Waste Heat Recovery Excellence
2nd Edition of Cement Conclave Award Presentation 2018
My Home Industries Private Limited.
Mellacheruvu Cement Works
❖ My Home Industries Pvt Ltd (MHIPL) is established in the year 1998 with an installed capacity of 0.2 mtpa and rose to10.0 mtpa.
❖ MHIPL entered into a Joint Venture with CRH Plc, Ireland in 2008 an internationally reputed group having thebusiness in cement and building materials in 35 countries.
❖ Other core businesses of the group are Construction & Real Estate, Power, Transport, Power Consultancy andEducation.
❖ MHIPL-MCW is an ISO 9001:2015, ISO 14001:2015, OHSAS 18001:2007,ISO 50001:2011 certified company.
❖ MHIPL-MCW received CII Green Co GOLD Rating in June’2017
❖ MHIPL is the members of CSI (Cement Sustainability Initiative ) and also have the road map for sustainability.
Company Profile
MY HOME INDUSTRIES PVT LIMITED
Group Profile
Sl. No Description Units 2015-16 2017-18
1 Renewable Energy (RPO) - -
2 REC Purchased – Solar REC - -
3 REC Purchased – Non Solar REC - -
4 RPO met through own generation - -
5 RPO met through PPA - -
6 Waste Heat utilized Million kCal7771 64878
7 Power generated from waste heat Million kWh9.03 75.44
RE PERFORMANCE
Solar Plant
Sl.No Capacity Annual kWh Generation (2017-18) % Consumption
1 1.2 MW 18.43 Lakhs 0.86%
2 12.7Kw 4148 (5Months) ---
RENEWABLE ENERGY SOURCES
12 Kwp Solar Plant at Mines (Nov-17)1.2 MW Solar Plant
RENEWABLE ENERGY SOURCES2x 500 LPD ROOF TOP SOLAR HEATER AT GUEST HOUSE
Commissioned in Nov-2016 -(Units saved @3000Units/Annum)
RENEWABLE ENERGY SOURCES SOLAR FENCE AT MINES MAGZINE
Solar Fencing
Waste Management System
❖ Well developed technology steps like Waste Heat Recovery power plant (12.5MW) incorporated in process.
❖ Usage of alternative fuels (pharmaceutical waste) 1.90 % (TSR) in kiln’s to reduce usage of natural resources.
❖ Fly ash addition in cement is 30.8%
❖ Slag addition in raw meal is 0.57%
❖ Fly ash addition in raw meal is 0.59%
❖ Shale consumption in raw meal is 0.36%
❖ Internally generated wastes like cotton waste , waste bags, grease are also being fired in kiln.
❖ STP water (200 KLD) is being used for plantation .
WHR Power Plant
❖MHIPL-MCW installed and commissioned 12.5MW Waste Heat Recovery System in Jan’2017 witha capital expenditure of about Rs 120 crores and started utilizing waste heat from preheater andcooler of all the lines for power generation.
❖ Waste Heat Recovery System was installed by M/s LNVT/SINOMA Energy Conservation Ltd andachieving PLF of 85% an average.
Suspension Preheater Boiler Air-Quenching Boiler (AQC) Turbine -Generator
WHRPP - 12.5MW
CO2 Emission reduced by 75440 MT/Annum in 2017-18
DESCRIPTION UNIT 2017-18
POWER GENERATION Lakhs KWH 754.40
PLF % 68.90
PLANT AUX. CONSUMPTION KWH 5710503
PLANT AUX. CONSUMPTION % 7.57
POWER SUPPLIED TO MCW Lakhs KWH 697.29
11
WHRPP - 12.5MW
Monthly Avg Generation vs Aux Power
0.00
1.00
2.00
3.00
4.00
5.00
6.00
7.00
8.00
9.00
10.00
APRIL MAY JUN JUL AUG SEP OCT NOV DEC JAN FEB MAR 2017-180.00
2.50
5.00
7.50
10.00
12.50
POWER GENERATION (MWH) AUX CONSUMPTION (PLANT) (%)
12
MW
%
Monthly PLF vs PAF5
0.7
4
76
.18
70
.59
65
.99 7
3.9
2
78
.37
78
.19
55
.73
59
.31
73
.93
65
.18
77
.60
68
.90
0
10
20
30
40
50
60
70
80
90
100
0
20
40
60
80
100
APR MAY JUN JUL AUG SEP OCT NOV DEC JAN FEB MAR 2017-18
%
PLF (%) PAF (%)
12.50 MW 13
PROPOSED RENEWABLE ENERGY/WASTE UTILIZATION PROJECTS
(Electrical and Thermal Energy)
S.No Description
Approx. Cost@Rs.
Lakhs Status Remarks
1 Installation of Solar plant at Mines Magzine 5.00Floating enquiry Proposed to arrange Mines Magazine
2 2x10kgs Bio Gas plant with cow dust 1.5 working Gas is using in Canteen
3 Installation of Day Light tubes 2.5
Floating enquiry
Proposed for Work shop and substation
4 MSW utilization in plant 25.00 Under studyPlanning to utilize Colony and Guest house
waste to generate Gas and use in Kiln(Pyro)
5 10 MW Solar plant at SJCL 8000Work underprogress
6 4 MW Solar Plant at VGU 3000 Under study
GHG Emission Reduction
Year Scope-1 emissions Scope-2 emissions Scope-3 emissions TotalKg Co2/MT of Clinker
2015-16 1080.70 0.78 5.65 1087
2016-17 1013.87 3.64 6.37 1024
2017-18 929.40 0.77 7.21 937
Scope Emission Sources Considered
Scope 1 EmissionsCement process-Calcination, Fuel Burning in Kiln & HAG, CPP -Coal Consumption etc.
Scope 2 Emissions Electricity Consumption from Grid
Scope 3 EmissionsRaw material Transport, Cement dispatch through rail & Road, Employee commute etc.
GHG INVENTORISATIONCO2 (Kg Co2/Ton of clinker)
GHG reduction due to Encon Projects,Installation of 12.5 MW WHR,and Thermal saving in Unit-3 Cooler upgradation.
2015-16 2016-17 2017-18
1087
1024
937
Established & Certified EnMS as per ISO 50001: 2011
Total investment made in last three years -148.43 Crores
Green Co Rating 2016 – Gold Rating
“ GOLD RATING” IN CII GREENCO SUMMIT 2017 : PUNE
19th National Award for Excellent Energy Efficient Unit from CII in Hyderabad in Sep 2018
18th National Award for Excellent Energy Efficient Unit from CII in Hyderabad in Sep 2017
17th National Award for Energy Efficiency from CII in Hyderabad in August 2016
PATH FORWARD
❑ Green Co Rating - Platinum
❑ Bio Gas from Domestic Waste
❑ Bio Fertilizer / Organic Manure from Colony & Canteen Waste
❑ PAT-2 Cycle target Achievement
❑ Reach Global Bench Marking
❑ Upgradation of EnMS as per the guide lines of ISO 50004:2018