performance monitoring of iec industrial gas turbines

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Performance Monitoring of IEC Industrial Gas Turbines Victor Litinetski, Offer Weiss, Alex Gutman For presentation to 13 th Israeli Symposium on Jet Engines and Gas Turbines November 06, 2014. Haifa, Israel IEC Generation Division Headquarters Mechanical Department

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Page 1: Performance Monitoring of IEC Industrial Gas Turbines

Performance Monitoring of IEC

Industrial Gas Turbines

Victor Litinetski, Offer Weiss, Alex Gutman

For presentation to 13th Israeli Symposium

on Jet Engines and Gas Turbines

November 06, 2014. Haifa, Israel

IEC Generation Division Headquarters

Mechanical Department

Page 2: Performance Monitoring of IEC Industrial Gas Turbines

2Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Presentation Scope

1. IEC performance monitoring approach

2. Case Study 1. Compressor failure

3. Case Study 2. Control system problem

4. Case Study 3. Compressor washing optimization

5. Case Study 4. GT Inlet Air Filter upgrade

6. Summary

Part 2.

7. Case Studies in details

Page 3: Performance Monitoring of IEC Industrial Gas Turbines

3Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Performance Monitoring: Introduction

Today, industrial gas turbines already have become one of

the main engines for electricity generation.

Modern industrial gas turbines have output

250 – 350 MW (up to 470 MW in developments). Combined-

cycle applications on their base have outstanding thermal

efficiency approaching 62%.

Even small degradation of their performance (efficiency,

power output etc.) could result in noticeable loss of

profitability.

Thus, performance monitoring of operational

characteristics is especially important for effective and

reliable operation of such engines.

Page 4: Performance Monitoring of IEC Industrial Gas Turbines

4Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Performance Monitoring: Main Goals in IEC(Generation Div. Headquarters, Mechanical Dept.)

Provision of continuous data on power output and heat rate of IEC’s industrial gas turbines. Both power output and heat rate are completely corrected to

GT reference conditions.

Only use of the corrected performance allows proper interpretation and analysis of the monitoring results.

Observation of the important turbine parameters such as turbine exhaust temperature, inlet air filter dP, compressor efficiency etc.

Optimization of inlet air filters operation and maintenance.

Optimization of compressor washing procedures and schedule.

Page 5: Performance Monitoring of IEC Industrial Gas Turbines

5Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Performance Monitoring: Actual Example

Trend of corrected power output

Eshkol EM-1. Gas Turbine Operation.

Test data from 26/03/10 until 22/12/11.

Prepared by Dr. V. Litinetski, Generation Div., Mechanical Dept., Gas Turbine Section.

213

215

217

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18/03 17/04 17/05 16/06 16/07 15/08 14/09 14/10 13/11 13/12 12/01 11/02 13/03 12/04 12/05 11/06 11/07 10/08 09/09 09/10 08/11 08/12 07/01

Date, dd/mm

Co

rrecte

d O

utp

ut,

MW

- Corrected Output

- Expected Output (PTP & CSA degradation curves)

- Acceptance test level (June 2004)

Blue dashed lines denote compressor washings

Page 6: Performance Monitoring of IEC Industrial Gas Turbines

6Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Performance Monitoring: IEC approach

Performance monitoring systems are being developed in IEC Generation Division more than 10 years. Now the 5-th version of the monitoring software is used in IEC as a result of continuous long-term advancement to answer actual operation requirements.

In-house development of these monitoring systems was inspired by unsuccessful implementation of purchased monitoring software from a well-known developer. Time consuming implementation had revealed inconsistency of the purchased system with the goals of performance monitoring.

In this presentation, an IEC (Generation Division) performance monitoring experience is described for large industrial gas turbines. This experience is illustrated by several case studies.

Page 7: Performance Monitoring of IEC Industrial Gas Turbines

7Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Studies in brief

Case Studies

GT performance monitoring approach is

illustrated by several case studies.

Page 8: Performance Monitoring of IEC Industrial Gas Turbines

8Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 1. Short description

Sequence of events: - Performance monitoring data indicated a

compressor problem 43 hours before the failure.

- Waiting a response from OEM monitoring team.

- Catastrophic failure occurred in field.

The failure was a result of unfortunate combination of technical and organizational drawbacks.

IEC own performance monitoring data would allow to prevent the disaster.

Case Study 1. Compressor Failure

Page 9: Performance Monitoring of IEC Industrial Gas Turbines

9Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 2. Short description

- After a control system upgrade from Simple Cycle configuration to Combined Cycle configuration an unexpected increase of GT output was revealed.

Since modern gas turbines are designed for maximum achievable capacity, this pointed at a possible decrease of safety margins of the turbine materials.

- Detailed investigation on the base of monitoring data was undertaken by IEC's Mechanical Department.

- Analysis of the operational data revealed an error in the control system software.

- After IEC application to OEM with the explanation of the problem, the error was corrected. This had allowed to prevent future failures of the turbine internal parts.

Case Study 2. Control System Problem

Page 10: Performance Monitoring of IEC Industrial Gas Turbines

10Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case study 3. Short description

Case Study 3. Compressor wash optimization

In this particular case, NOT performing OFLWW has saved

about $80,000 and a number of man-hours.

The task was imposed by a power station, regarding a

need of early compressor off-line water washing

(OFLWW) – how much it would be profitable?.

The power station requested an analysis based on

actual performance monitoring data and experience.

The result of analysis: The disputable early OFLWW is

UNPROFITABLE.

Page 11: Performance Monitoring of IEC Industrial Gas Turbines

11Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case study 4. Short description

Case Study 4. GT Inlet air filter upgrade

The filter met expectations of the project team. It provided

much better air filtration that led to substantial improvement

of GT performance.

Use of this filter allowed to save several millions dollars on

filter house reconstruction + very high profit on improvement

of GT performance.

The tasks:

1. Substantiate an upgrade of the current inlet air filter to the

advanced technology Efficient Particulate Air (EPA) filter

of a peculiar compact design.

2. Evaluate performance of the filter during one-year operation in

field.

Page 12: Performance Monitoring of IEC Industrial Gas Turbines

12Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Summary

Only use of the corrected GT performance allows proper interpretation and analysis of the performance monitoring results.

GT performance monitoring allows effective solutions of various operational problems.

It might provide high profits on performance improvements and prevent equipment failures.

Page 13: Performance Monitoring of IEC Industrial Gas Turbines

13Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Part 2. Case Studies in details

PART 2

Page 14: Performance Monitoring of IEC Industrial Gas Turbines

14Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 1. Operational Events

Sequence of operational events

(performance monitoring data):

- Clear indications of a compressor problem were seen 43 hours before the failure.

- Strong indications of possible damage to compressor were seen 5 hours before the failure (next slide).

Case Study 1. Compressor Failure

Page 15: Performance Monitoring of IEC Industrial Gas Turbines

15Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 1. Compressor Failure: 5 hours before...

EM1 Trends. Jan. 9, 2009 10:00-10:10

400

405

410

415

420

10:00 10:01 10:02 10:03 10:04 10:05 10:06 10:07 10:08 10:09 10:10

Co

mp

r. D

isch

arg

e T

em

p.,

C

210

220

230

240

250

Ou

tpu

t, M

W

- Compressor Discharge Temperature

- Output

Possible Damage to

Compressor

Compressor

discharge

temperature

Turbine OutputAbrupt change of

other parameters

Page 16: Performance Monitoring of IEC Industrial Gas Turbines

16Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 1. Compressor Failure

Nevertheless, the catastrophic

failure occurred in field

(next slide).

Page 17: Performance Monitoring of IEC Industrial Gas Turbines

17Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 1. Compressor Failure: Rotor after failure

Page 18: Performance Monitoring of IEC Industrial Gas Turbines

18Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 1. Some conclusions

Conclusions:

Catastrophic failure of the compressor was a

result of unfortunate combination of technical

and organizational drawbacks.

Additional in-house GT condition monitoring

software has been developed

Page 19: Performance Monitoring of IEC Industrial Gas Turbines

19Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 2. Sequence of operational events

After a control system upgrade from Simple Cycle (SC) configuration to Combined Cycle (CC) configuration some operation anomalies were revealed.

Irregular increases of the power output by 10-15 MW above the expected maximum were detected in about two months after the upgrade (Figure below).

The event continued during a week and after that disappeared.

Since modern gas turbines are designed for maximum achievable capacity, this pointed at a possible decrease of safety margins of the turbine materials.

Case Study 2. Control System Problem

Page 20: Performance Monitoring of IEC Industrial Gas Turbines

20Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 2. Power output scattering

Eshkol EM-1. Gas Turbine Operation from

Test data from 03/01/06 until 28/03/06.

Prepared by Dr. V. Litinetski, Generation Div., Mechanical Dept., Gas Turbine Section.

220

221

222

223

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01/01/06 11/01/06 21/01/06 31/01/06 10/02/06 20/02/06 02/03/06 12/03/06 22/03/06 01/04/06 11/04/06

Date, dd/mm/yy

Co

rrecte

d O

utp

ut,

MW

- Corrected Output

- PTP Degradation curve

- Acceptance test level

Page 21: Performance Monitoring of IEC Industrial Gas Turbines

21Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 2. IEC investigation of the problem

Detailed investigation was undertaken by IEC's

Mechanical Department

Performance monitoring data showed that the

irregular increases of power output were

accompanied by significant scattering of the

turbine exhaust temperature (Figure below)

Page 22: Performance Monitoring of IEC Industrial Gas Turbines

22Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 2. Scattering of exhaust temperature

Eshkol EM-1. Turbine Exhaust Temperature.

Test data from 03/01/06 until 28/03/06.

Prepared by Dr. V. Litinetski, Generation Div., Mechanical Dept., Gas Turbine Section.

580

585

590

595

600

605

610

615

620

15 15.2 15.4 15.6 15.8 16 16.2 16.4 16.6 16.8 17

Compressor Pressure Ratio

Exh

au

st

Tem

pera

ture

, C

- Measured exhaust temperature

- Temperature Control Curve

Page 23: Performance Monitoring of IEC Industrial Gas Turbines

23Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 2. Performance data analysis

Thorough analysis of the data revealed an

error in the control system software, namely,

an incorrect definition of so called

Temperature Control Curve, which is an

important element of the turbine load control,

fuel efficiency and protection (Figure below).

Page 24: Performance Monitoring of IEC Industrial Gas Turbines

24Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 2. Error in control system software

Eshkol EM-1. Temperature Control Curve

Prepared by Dr. V. Litinetski, Generation Div., M echanical Dept., Gas Turbine Section.

550

560

570

580

590

600

610

620

630

640

650

660

12.0 12.5 13.0 13.5 14.0 14.5 15.0 15.5 16.0 16.5 17.0 17.5 18.0 18.5 19.0 19.5 20.0

Compressor Pressure Ratio

Exh

aus

t T

em

pera

ture

, C

- June 14, 2004 (SC)

- October, 2005 (CC)

- April 10, 2006 (CC)

Designed

CC Curv eFinal CC

Curv e

Desined

Break Point

Actual CC

Curv e

Wrong Break

Point

SC

Curve

Page 25: Performance Monitoring of IEC Industrial Gas Turbines

25Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 2. Correction of the problem

After IEC application to OEM with the

explanation of the problem, Temperature

Control Curve definition was corrected.

Figure below shows the turbine exhaust

temperature trend after correction.

Page 26: Performance Monitoring of IEC Industrial Gas Turbines

26Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 2. Exhaust temperature after correction

Eshkol EM-1. Turbine Exhaust Temperature.

Test data from 24/06/06 until 12/11/06.

Prepared by Dr. V. Litinetski, Generation Div., Mechanical Dept., Gas Turbine Section.

580

585

590

595

600

605

610

615

620

625

630

14.5 15 15.5 16 16.5 17

Compressor Pressure Ratio

Exh

au

st

Tem

pera

ture

, C

- Measured exhaust temperature

- Temperature Control Curve (After Correction)

Page 27: Performance Monitoring of IEC Industrial Gas Turbines

27Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 3. Use of performance monitoring info

The task was imposed by a power station, regarding a need of performing compressor off-line water washing (OFLWW).

The station question was: whether the station could save money if it performed OFLWW earlier than planned by ~2000 operating hours of the GT.

The power station asked for an analysis based on current performance monitoring data and accumulated monitoring experience.

Case Study 3. Compressor wash optimization

Page 28: Performance Monitoring of IEC Industrial Gas Turbines

28Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 3. Data use & approximation

Eshkol EM-1. Profitability Analysis of Off-line Water Washing in February 2011.

Test data from 3/12/10 until 14/02/11.

Prepared by Dr. V. Litinetski, Generation Div., Mechanical Dept., Gas Turbine Section.

220

222

224

226

228

230

38000 39000 40000 41000 42000

Actual Operating Hours

Co

rrecte

d O

utp

ut,

MW

- Corrected Output

- Degradation with NO OFLWW

- Degradation with OFLWW

OFLWW under question

at 40,000 op. hours

(end February 2011)

Output Trend With OFLWW

Output Trend With NO OFLWW

OFLWW at 42000

op. hours

(end May 2011)

Last OFLWW Level

3/12/2010

Page 29: Performance Monitoring of IEC Industrial Gas Turbines

29Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 3. Conclusions

The following conclusions were made:

Early OFLWW (at 40,000 op. hours) is UNPROFITABLE considering current air filter condition and GT performance degradation trends.

Not performing OFLWW might save about $128,000 in this particular case.

--------------------------------------------------------------------------------

Actually, the OFLWW was performed after 42,500 operating hours of GT. Corrected power degradation was slightly higher than predicted but the main result remained unchanged – the early OFLWW (if any) would be unprofitable.

Page 30: Performance Monitoring of IEC Industrial Gas Turbines

30Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 4. The task

The following tasks had been raised with operation and

maintenance needs:

1. Substantiate an upgrade of the current inlet air filter to the

advanced technology Efficient Particulate Air (EPA) filter.

2. After 1 year of EPA filter operation, evaluate actual

performance of the GT with EPA filter and compare with actual

performance of the GT with the regular air filter during the same

operational term.

Conclusions should be made on the base of actual performance

monitoring data

Case Study 4. GT Inlet air filter upgrade

Page 31: Performance Monitoring of IEC Industrial Gas Turbines

31Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 4. View of the installed filter

Three-layer compact design EPA cartridges

Page 32: Performance Monitoring of IEC Industrial Gas Turbines

32Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Case Study 4. Conclusions

The tasks were performed on the base of accumulated performance monitoring data during one-year operation with EPA filter.

The filter met expectations of the project team. It obviously provided much better air filtration that led to substantial improvement of GT performance.

Use of this filter allowed to save several millions dollars on filter house reconstruction.

Page 33: Performance Monitoring of IEC Industrial Gas Turbines

33Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

Summary in details

1. An actual approach to continuous performance monitoring of 250MW-class industrial gas turbines is described in this presentation.

2. The described performance monitoring practices may be useful in development, improvement and support of monitoring systems.

3. The most important outcome of performance monitoring is a detailed analysis of GT operation events, providing a basis for solution of operational problems and decision making as well.

4. Effective and reliable analyses of monitoring results could be performed only by highly educated personnel having strong knowledge in GT theory, equipment and operation. Monitoring team should include such persons.

5. In-house development of the monitoring systems in IEC was inspired by unsuccessful implementation of purchased monitoring software from a well-known developer.

6. The monitoring systems was gradually developed in Generation Division of IEC and successfully used for more than 10 years in actual gas turbines operation.

7. The presented in this presentation performance monitoring approach has a general importance; it could be helpful for other gas turbine operators and used in actual performance monitoring of various gas turbine types.

Page 34: Performance Monitoring of IEC Industrial Gas Turbines

34Prepared by V. Litinetski. IEC Generation Div., Mechanical Dept., Gas Turbine Section

THE END