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    Case Study: Weld shop productivity improvement through elimination

    of Process, Parts quality & Equipment down time.

    Ahmedabad Plant

    IMTMA-Siemens Productivity Championship Awards Competition 2014

    Alok Bhavik Sanjay Devesh Bishnu Anand Nihar Sohan

    1

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    2

    About Us

    The worlds most affordable car

    Passenger Vehicle Business Unit

    Commercial Vehicle Business Unit

    Jaguar Land Rover

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    Vision:A brand most admired by our customers, employees, business partners

    and shareholders for the experience and value they enjoy from being with us

    3

    About Us

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    FY09 FY10 FY11 FY12 FY13

    10.2812.22 13.13

    15.6917.68 18.88

    23.97

    29.4531.25 32.41

    FY03 FY04 FY05 FY06 FY07 FY08 FY09 FY10 FY11 FY12

    InLacs

    Capacity Utilization

    Indian Passenger Car Market

    Share of Market (SOM)Passenger Cars

    Source: SIAM, ICRAs estimates.

    Passenger Vehicle Density (per 1000 persons)Passenger Vehicle Sales (India)

    13

    45

    85

    158

    188

    246

    445

    1200

    463

    500

    India

    China

    Turkey

    Brazil

    Russia

    South Korea

    Japan

    U.S.A

    U.K.

    Germany

    Potential Growth in

    Passenger Car

    Segment in India

    Sustainable

    car market

    Capacity

    utilization has

    been at the

    core of each

    OEMs strategy

    for the Indian

    market

    A1 & A2

    Segment:

    Hatchback,

    78%

    A3 Segment:

    Mid Size

    Sedan, 18%

    A4 Segment:

    Executive

    Sedan, 3%

    A5 Segment:

    Premium

    Sedan, 1%

    4

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    5

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    Optimizing

    productivity of

    existing facility

    through LaborProductivity

    Cobb-Douglas Equation: Product ion output

    is determined by the amount of labor

    involv ed and the amoun t of capita l invested

    Leveraging Labor Productivity

    Capacity Enhancement

    Facility addition or

    enhancement

    through CapitalInvestment

    Leverage Labor

    Productivity to

    optimize Capacity

    Utilization

    Tata Motors Limited, Sanand Capacity Map

    Total Area of plant = 725 Acres

    250,000 cars per year

    6

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    Weld Shop Flowchart

    7ASP

    6ASP5

    Roof

    Logistic Shed

    POWER SUB

    STATIONOFFICE(MAZZNINE) LOGISTIC AREA

    Robot

    Training

    ASP 4 ASP 3

    Body Side Inner Body Side Outer

    Underbody Frame

    Underbody Respot

    Front Door LH Rear Door LH Tailgate

    HoodFront Door RH Rear Door RH

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    Factors of under utilized capacity

    Factor 1: Cycle Time > Takt Time

    Pitch

    Factor 2: Occurrence of Losses

    Pitch

    Resulting

    Loss of JobsPer Hour

    (JPH)

    8

    PitchPitchPitch Pitc

    Cycle End Cycle Start Cycle End Cycle Start

    SafetyQuality

    CheckCTQ

    Element

    Location

    Work while

    WalkingWalk only

    Return toStart

    Time ForElement

    on conveyor

    HomePosition

    PitchMarking

    Start Point End Point

    Q #

    znano

    z nano

    z z z znano nano nano nano

    Exceeds

    the Pitch

    BreakDown

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    Weld Shop Operation and Methodology Followed

    Theme Selection based on bottlenecks

    Grasping Current Situation and Target Setting

    Make an activity plan

    Analysing the factors

    Developing and implementing Kaizen

    Confirming effectiveness

    Sustenance and Establishing controls

    1

    2

    3

    4

    5

    6

    7

    Methodology Followed

    7 Steps Problem Solving Approach

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    Grasping Current Situation and Set Target

    20.9

    35.3 37.4

    62 62 62

    May'12 Jun'12 Jul'12

    Existing JPH Trend Actual Target

    Better

    Tools & Techniques to be used to understand current situation?

    Time Study

    Standard

    Work

    Combination

    Sheet

    Spaghetti

    ChartLoad Chart Losses Pareto

    Better

    10

    3753

    Before (Jul'12) After (Jan'13)

    Target : JPH 85%Capacity

    For Factor 1 For Factor 2

    100%

    Capacity

    60 %Capacity

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    1 2 3 4 5 6 7 8

    46 49 48 48 45 49 49 47

    48 48 48 48 48 48 48 48

    51 49 51 52 53 50 54 51

    99 97 99 100 101 98 102 99

    46 49 45 45 47 47 46 45

    145 146 144 145 148 145 148 144

    STEP OPERATION ELEMENTObserved readings (In Seconds) Task

    Time

    (Seconds

    1 Main Framing Line - 10 48

    2 Main Framing Line - 20 51

    3 Main Framing Line - 30 46

    Ma nua l Au to Wa lk Wait

    1 2

    2 2

    3 14

    4 48

    Step

    No

    Work Content DescriptionObserved Time Work Content Graph : (Scale : 1 Div = 1 sec)

    5 10 15 20 25 30

    Take out the key before reach the body

    at 130 and wait for reach the body at

    130

    35 40 45 50 65 70 75

    Check station=140 in home position in

    home position in HMI Panel

    Insert key in panel select body take in

    55 60

    Waiting for droplift returning at home

    position

    164Stations

    303Operators

    134

    Robots

    106Parts

    11

    Time

    Study

    SWCS

    Spaghetti

    Time Study, SWCS and Spaghetti Chart

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    586169

    63

    83

    62

    7

    4

    5961

    54

    5456

    54 5

    656 5

    857

    54

    61

    BC20

    BC40

    BC60

    BC140

    BC160

    BC230

    BC260

    BSI-LH

    BSO-LH

    MR-10

    MR-30

    MR-50

    MR-70

    MR-90

    MR-110

    MF-10

    MF-30

    MF-50

    MF-70

    MF-90

    MF-110

    MF-130

    MF-150

    MF-170

    MF-190

    UBF-10

    UBF-30

    UBF-50

    UBF-70

    UBF-90

    UBF-110_

    1

    UBC-20

    UBC-40

    UBC-60

    UBC-80

    UBC-100

    UBC-120

    UBC-140

    UBC-160

    UBC-180

    FE-010

    C

    ycleTime(seconds)

    Station Number

    Station Wise Load Chart:

    Takt Time-53 Sec to meet additional

    requirements like Spare parts production

    9 Stations > 58 Sec

    What : Major Bottleneck Stations

    Where : BIW Shop

    When : In All shifts

    Who : Team Members of those stations

    Why : Cycle time > Takt time of next customer

    shop demand

    How much: 9 Stations

    Problem Definition: Imbalanced Load Chart

    9

    0

    Before (Jul'12) Target (Oct'12)12

    Takt Time-58 Sec to meet other shops demand

    Target: Major Bottleneck Stations

    1 243

    5 76

    8 9

    Load Chart, Problem Definition and Target Setting

    Takt time58 Sec

    Takt time

    53 Sec

    Requirement

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    Activity Responsibility Status Aug12 Sep12 Oct12 Nov12 Dec12

    1Grasping Current Situation (All Lines) :

    Preparation Process at a Glance

    Sanjay, AlokPlan

    Actual

    2 Time study & preparation of load chart Devesh, NiharPlan

    Actual

    3 Identify bottleneck areas / processes SohanPlan

    Actual

    4Understanding last three month breakdown &

    other losses issueBhavik

    Plan

    Actual

    5a) Analysis of major factors

    b) Identification of MURI & MUDA from SWCSTeam

    Plan

    Actual

    6 Root cause analysis (C&E Diagram & Why WhyAnalysis)

    Team PlanActual

    7 Kaizen proposals identification TeamPlan

    Actual

    8 Kaizen implementation TeamPlan

    Actual

    9 Result Validation & Tracking Sanjay, AlokPlan

    Actual

    10 After time study & load chart preparation Devesh, BishnuPlan

    Actual

    11 Updation of Process at a Glance if any Devesh, BhavikPlan

    Actual

    12Standardization of results & Sustenance of

    Kaizen implementedAnand, Sohan

    Plan

    Actual

    13 Horizontal Deployment Sanjay, AlokPlan

    Actual

    14 Final presentation to Sr. Management Sanjay, AlokPlan

    Actual

    Activity Plan

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    Analyzing the Factors

    6169 63

    83

    6274

    59 61 61

    BC 30 BC 40 BC 50 BC 60 BC 150 BC 190-220 BSO-LH BSO-RH UBC - 170CycleTime(seconds)

    Station Number

    Load Chart of Bottleneck Stations:Takt Time: 58 Sec

    Robotics

    Operation: 03

    Manual

    Operation: 06

    CorrectionOver Production

    Inventory

    Movement

    Processing WaitingTransportation

    Defects

    Overburden

    Find out Muri & Muda

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    Muri (Overburden) & Muda (Wastage) identification

    and analysis

    Over Burden

    High cycle time for thumb sealant

    application

    No. of spot more in IR-25 (12 no.)

    No. of spot more.(14 no.) in IR-11

    Over

    Production

    Inventory

    Motion

    Takes 2 step extra to complete the

    work.

    Waiting

    Body take in take out

    T/C fault

    Body setting fault

    Transportation

    Defect/

    Rework

    Door gap not OK

    Sash Profile not OK

    Sash joint Crack

    Over

    Processing

    Hammering in backlight cross

    member in each cycle

    Hammering in front floor in each

    cycle to remove the gape

    Excess work load on

    operators

    Operators Work load

    was not balanced

    Analyzed work contents

    in details and rebalanced

    the line

    Operator bending in

    each cycle for

    sealant application

    Platform height wasmore

    Platform height

    reduced

    All Work contents

    were not well

    analyzed

    High Cycle time for Thumb sealant application

    Variation in No. of

    sealant application

    points

    Operator fatigue

    Kaizen Kaizen

    15

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    Operation Problem Measure Taken Results

    Thumb sealant

    application on Body

    Joints

    8 points per person

    were applied & after

    half days of working,

    cycle time was

    increasing due to

    Ergonomic Issues.

    Operation distributed

    zone-wise and platform

    modified as per height of

    application to avoid

    bending.

    - Operators bending

    eliminated

    - 10 points per operator

    achieved.

    Before Kaizen After Kaizen

    Name of employee: Mukesh, Sanjay Date: 07/09/12 Shop: BIW Line/Station: BC-30, 40

    Kaizen 1Elimination of Operator Fatigue

    16Tools Used for root cause analysis: Seven Ways and Why-Why

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    Operation Problem Measure Taken Results

    Door Assembly by

    Spot Welding

    Door Gap

    Inconsistency

    Intermediate quality check

    at D-Sash Assembly Level

    by incorporating D-Sash

    Checking Fixture

    Confirmation of Gap &

    consistency at D-Level and

    the same is reflected at

    Door Level.

    Before Kaizen After Kaizen

    Name of employee: Sanjay, Bishnu, Anand Date: 10.09.12 Shop: BIW Line/Station: BC-50, 60, 150

    Kaizen 2Elimination of Door Gap Inconsistency

    17Tools Used for root cause analysis: Cause & Effect diagram and Why-Why

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    Operation Problem Measure Taken Results

    Body Side Outer

    Assembly

    Robot is waiting until

    turn table is rotated

    and locked.

    Bottleneck robot is now

    pre-started while turn

    table is rotating

    Cycle Time improved by 2

    sec per cycle

    Before Kaizen After Kaizen

    Name of employee: Nihar, Devesh Date: 10/10/12 Shop: BIW Line/Station: BSO LH/RH

    Kaizen 3Elimination of BSO robot waiting time

    18Tools Used for root cause analysis: Seven Ways and Why-Why

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    Operation Problem Measure Taken Results

    Material Handling &

    Spot Welding

    Dent & Ding due to

    Gun Handling & Parts

    Loading

    Manual spots are

    eliminated on 18 points by

    implementing 3 Poka Yoke

    and 1 individual Kaizen

    1. Cycle Time improved

    from 74 sec to 53 sec at

    Station Nos. BC 190220

    2. Body Touch point

    reduced w.r.t Metal Finish

    Before Kaizen After Kaizen

    Name of employee: Sohan, Bishnu, Anand Date: 14/10/12 Shop: BIW Line/Station: BC 190-220

    Kaizen 4Poka Yoke implementation in BC Line

    19

    Inner Panel and Bottom

    hinge not matching

    Dent & Ding due to Gun

    hitting with panel

    Dent between Sash &

    Inner PanelResting Myler Surface

    contact area found less

    At

    Caparo

    At

    Vendor

    Vendor

    Poka Yoke provided for

    new Spot Location

    Spot Locator provided for

    Gun

    Copper Plate provided to

    ensure no damage at Sash Area

    New Myler provided with

    more surface contact

    MR

    At

    Caparo

    At

    Vendor

    Vendor

    MR

    Tools Used for root cause analysis: Cause & Effect diagram, Seven Ways & and Why-Why 19

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    Operation Problem Measure Taken Results

    Spot welding Spot weld burrs and

    off location spot

    welding.

    Gun guide provided at 6

    different location / Weld

    parameter and gun

    alignment fine tune at 8

    different spot gun.

    1. Cycle Time improved

    from 61 sec to 53 sec at

    UBC 170

    2. Quality Rate improved

    Before Kaizen After Kaizen

    Name of employee: Bishnu, Nihar Date: 18/10/12 Shop: BIW Line/Station: In-house UB Line

    Kaizen 5Cycle time Reduction at UBC 170

    20

    Spot Burrs

    Spot Burrs

    Spot Burrs

    Off location Spot

    No Spot Burrs

    No Spot burrs

    No Spot burrs

    Gun guide for fix location Spot

    1 2

    3 4

    1 2

    3 4

    20Tools Used for root cause analysis: Why-Why

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    Results Achieved: Factor 1

    9

    0 0

    Before (Jul'12) After (Oct'12) Target (Oct'12)

    Major Bottleneck Stations

    Target Partially achieved

    6169 63

    83

    6274

    59 61 6155 54 57 58 53 53 54 58 58

    BC 30 BC 40 BC 50 BC 60 BC 150 BC 190-220 BSO-LH BSO-RH UBC - 170CycleTime(sec

    onds)

    Station Number

    Load Chart: After

    21

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    Factor 2: Losses Pareto and Target Setting

    What : Major losses during production

    Where : BIW Shop

    When : In All shifts

    Who : Respective Functions

    Why : Major contribution in OEE

    How much: 42%

    Problem Definition: Losses during manufacturing

    42%

    21%

    Before (Oct'12) Target (Jan'13)

    Target: Losses %age

    9.56.2 5.1 4.2 3.5 3.4 3.1 2.7 2.5 1.5 0.4

    2337

    49 5968

    7683 89

    95 99 100

    0

    20

    40

    60

    80

    100

    0

    10

    20

    30

    40

    StandardLoss

    Body TakeIn Take Out

    BodySetting

    fault

    T/C Fault PartQualityIssue

    LimitSwitchfault

    D Net Fault EquipmentB/D

    Stationwork delay

    InternalBuffer

    Full/Empty

    Partshortage

    Cumulative%

    %LoadingTime

    Losses

    Losses Pareto: May to Oct12

    22

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    Operation Problem Measure Taken Results

    Body setting fault at

    UBC#30

    Part positioning

    sensor not sensing

    due to part variation

    Limit switch provided

    instead of part positioning

    sensor

    Eliminated loss due to

    body setting fault at

    UBC#30

    Before Kaizen After Kaizen

    Name of employee: Nihar, Devesh Date: 30/10/12 Shop: BIW Line/Station: UBF

    24

    Kaizen 6Modification of Part Positioning sensor

    Tools Used for root cause analysis: Cause & Effect Diagram, Seven Ways and Why-Why

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    Operation Problem Measure Taken Results

    Robotic Tip Dressing Different robots were

    going for tip dressing

    at different time

    according to their

    individual tip dressing

    counter.

    All the tip dressing

    counters made common

    for a single line so that

    every robot will go

    simultaneously for tip

    dressing.

    Cycle time reduction

    Before Kaizen After Kaizen

    Name of employee: Sanjay, Nihar Date: 12/12/12 Shop: BIW Line/Station: All Main Line

    Kaizen 8Simultaneous Tip Dressing

    26Tools Used for root cause analysis: Why-Why

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    Operation Problem Measure Taken Results

    Main Respot (MR)

    Body take in take out

    Body take-in take-

    out takes more than

    3 min per hour

    during production.

    Programme modified for

    Body take in take out.

    Single key selection for

    take-in and take-out

    Approximate 1.5 min for

    take in & no time for take

    out

    Before Kaizen After Kaizen

    Name of employee: Prem, Alok Date: 03/12/12 Shop: BIW Line/Station: MR-140

    Kaizen 9Body Take In Take Out

    27Tools Used for root cause analysis: Cause & Effect Diagram and Why-Why

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    Result

    3.1 2.9 2.5 1.9 1.4 1.2 1.1 0.8 0.3 0.220

    39 5168 77 85 90 92

    99 100

    0

    20

    40

    60

    80

    100

    0

    10

    20

    3040

    InternalBuffer

    Full/Empty

    EquipmentB/D

    Partshortage

    Part QualityIssue

    Station workdelay

    D Net Fault MES B/D StandardLoss

    T/C Fault Body Setingfault

    Cumulative%

    %LoadingTimeLosses Pareto After(Jan'13)

    42%

    20% 21%

    Before (Jun'12) After (Jan'13) Target (Jan'13)

    Losses %age

    9.5 6.2 5.1 4.2 3.5 3.4 3.1 2.7 2.5 1.5 0.423 37

    4959 68

    76 8389 95

    99 100

    0

    20

    40

    60

    80

    100

    0

    10

    20

    30

    40

    StandardLoss

    Body TakeIn Take Out

    BodySetting

    fault

    T/C Fault PartQualityIssue

    LimitSwitchfault

    D Net Fault EquipmentB/D

    Stationwork delay

    InternalBuffer

    Full/Empty

    Partshortage

    Cumulative%

    %Loading

    Time

    Losses

    Losses Pareto Before: May to Oct12

    28

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    37

    4551 52 53

    55

    Before

    (Jul'12)

    Sep'12 Oct'12 Nov'12 Dec'12 Jan'13

    Overall Results

    JPH Trend

    56 56 57

    Feb'13 Mar'13 Apr'13

    Kaizen1 & 2

    Kaizen

    3,4,5,6

    Kaizen

    7

    Kaizen

    8 & 9

    Target

    53

    Sustenance Trend

    VCC (KWH/Car) First Shot OK (%)Cost Benefits:Rs. 32 LPA

    OEE (%)

    29

    90~92% Capacity Utilization

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