recovery of sale-able slag from jigging tailings in femn production
TRANSCRIPT
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RECOVERY OF SALEABLE SLAG FROM JIGGING TAILINGS
ENVIR
ON
MEN
T
CONSERVE
NATURAL
RESOURCES
CONSE
RVE
MIN
ERAL
S
WEA
LTH
GENER
ATION
WEALTH OUT OF WASTE…
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Leader : B.D.NANDA (HEAD, FAP JODA)
Unit : FAP JODA
Division : FAMD, TATA STEEL Ltd.
Members :
D.D.Parida
B.Srinivas
Kaushik Shubhank
B.N.Rout
INNOVATORS
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PROCESS FLOW OF FERRO ALLOYS PLANT, JODA
ARC FURNACE TAPPING METAL & SLAG CAKES
H C FERRO MANGANESE
HIGH MnO SLAG
STEEL MELTING SHOP
SILICO MANGANESE INDUSTRY
CUSTOMER
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PROCESS FLOW OF METAL & SLAG RECOVERY
WASTE
MIXED METAL WITH SLAG INCLUSIONS MIXED METAL CRUSHING [0-20mm]METAL & SLAG BREAKING
JIGGED METAL
JIGGING MACHINE
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BACKGROUND [THE TRIGGERS…]
FAP, Joda produces 50400 MT of High Carbon FeMn /annum and generates about 36000 MT of High MnO slag as a byproduct.
High MnO slag is one of the input raw materials for SiMn industry [FY 11 requirement ~ 55000 MT ].
As per the TS expansion plans for FY15, 78000 MT of High MnO FeMn slag will be required.
Current demand-supply gap [19000 MT] will shoot up.
200 Kg of waste is generated per ton of FeMn produced at FAP,Joda [ ~ 800MT/month].
Storage of waste creates space constraint and dumping is not an environment friendly methodology.
Idea generation Trial implementationTriggers Results Benefits
Waste dump
GENERATION OF IDEAS
IDEA # 1: Entire waste can be sent for re-jigging with an attempt for slag separation.
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IDEAS
IDEA # 2: Entire waste can be sent for dressing of slag pans used for tapping.
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IDEAS
IDEA # 3: Entire waste can be sent for filling of low lying areas (inside plant)
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NEED FOR AN INNOVATIVE APPROACH:
It was observed that the waste material had 60% of slag pieces in it.
Customer requirement of High MnO slag was for MnO ~30%, Silica ~22%.
Composition of tailings: MnO ~ 22%, Silica ~ 38%.
A challenge came up to convert the waste into usable material.
The major challenge was to enhance the quality from 22 – 30 % MnO.
An innovative thought of recovering slag from the waste and reducing the waste dumping simultaneously.
Idea generation Trial implementationTriggers Results Benefits
IDEAS
IDEA # 4: Entire waste can be sent for manual screening to recover saleable slag.
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PROCESS IMPROVEMENT
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FUSED SAND
FINAL PRODUCT
Idea generation Trial implementationTriggers Results Benefits
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ACHIEVEMENTS: THE ASPECT OF DEMAND–SUPPLY GAP
+10 mm screen recovered slag having MnO ~ 34 % and Silica ~ 25%.
The recovery of slag is 500 MT/month.
Supply-demand gap of slag was reduced by 6000 MT/annum.
Recovered slag was used @ 400Kg/MT of SiMn as input material.
QUALITY TRAILS & RESULTS
6/8/10 mm MANUAL SCREEN [Jig feed: -20mm]
10 mm MANUAL SCREEN [Jig Feed: -15mm]
Chemical Analysis
MnO – 22% MnO – 34%
SiO2 – 38% SiO2 – 25%
Idea generation Trial implementationTriggers Results Benefits
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Dumping of waste was reduced by 100%.
Environment friendly approach adopted.
Elimination of diesel consumption by vehicles used for dumping from 160 L/month to 0L.
ACHIEVEMENTS: ENVIRONMENTAL ASPECT
Total captive reserve of Mn Ore in Joda contains only 20% of High grade Ore, rest being medium and low grade ore.
Recovered slag substitutes High Grade Mn ore by 400Kg/MT of SiMn produced, thus saving the precious natural reserves.
High Mn:Fe ratio helps in consuming more of low/medium grade Mn ore for SiMn.
Idea generation Trial implementationTriggers Results Benefits
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The undersize waste from screening is being used for dressing of slag pans.
Recovered slag substitutes fresh river sand consumption by 30%.
ACHIEVEMENTS: ENVIRONMENTAL ASPECT
Using High MnO slag instead of high grade ore reduces the need for carbothermic reduction of the substituted amount.
Coke consumption required for reduction reduces by 320 MT/annum.Power consumption accordingly drops by 50 KWH/MT of SiMn when slag is used.
Idea generation Trial implementationTriggers Results Benefits
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DIRECT TANGIBLE BENEFIT:
Total recovery of slag from waste till Feb’11 = 6200 MT.
Realization of slag = Rs. 6000/MT
Processing cost for screening = Rs. 90/MT
Net benefit = Rs 322 Lakhs/annum.
ACHIEVEMENTS: FINANCIAL ASPECT
Idea generation Trial implementationTriggers Results Benefits
RIVERSAND :
Reduction in fresh river sand consumption = 1235 Cu.m/annum.
Cost of sand = Rs 435/Cu.m
Net benefit = Rs 5.3 Lakhs/annum.
DISPOSAL:
Reduction in waste = 9600 MT/annum.Cost of handling = Rs 90/MTNet saving = Rs. 8.64 Lakhs/annum.
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ACHIEVEMENTS: FINANCIAL ASPECT
Idea generation Trial implementationTriggers Results Benefits
BENEFITS to SiMn INDUSTRY:
[A] High Grade Mn Ore:
Substitution of high grade ore = 400 Kg/ MT of SiMnTotal substitution = 4000 MT/annum Differential cost = Rs 9000 / MTNet benefit = Rs 360 Lakhs/annum
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ACHIEVEMENTS: FINANCIAL ASPECT
Idea generation Trial implementationTriggers Results Benefits
Total saving for FAP Joda = Rs. 336 Lakhs/annumTotal saving for SiMn industry = Rs. 412 Lakhs/annum
BENEFITS to SiMn INDUSTRY:
[B] COKE:
Reduction in coke consumption = 320 MT/annum.Cost of coke = Rs 10000/MTNet benefit to SiMn industry = Rs 32 Lakhs/yr.
BENEFITS to SiMn INDUSTRY:
[C] POWER: Reduction in power = 50 KWH/MT of SiMn Cost of power = Rs 4 /KWH Cost saving = Rs 20 Lakhs/yr
[D] QUALITY: Slag substitution helps to reduce detrimental Phosphorus contribution to Steel.
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ACHIEVEMENTS: CUSTOMER APPRECIATION
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FLOW DIAGRAM OF SALEABLE SLAG RECOVERY PROCESS