remote monitoring & diagnostics system for an lng … lng loading arm issues due to lack of data...

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© Copyright 2014 OSIsoft, LLC. Presented by Remote Monitoring & Diagnostics System for an LNG Loading Arm with the PI System Infrastructure Walter Flores Instrument Maintenance Supervisor Hunt LNG

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© Copyr i gh t 2014 O SIs o f t , LLC .

Presented by

Remote Monitoring &

Diagnostics System for an

LNG Loading Arm with the

PI System Infrastructure

Walter Flores

Instrument Maintenance Supervisor

Hunt LNG

© Copyr i gh t 2014 O SIs o f t , LLC .

Agenda

• About Hunt LNG & Peru LNG

• LNG Loading Faculty/Arm Overview

• Business Challenge

• Solution

• Results and Benefits

• Summary

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© Copyr i gh t 2014 O SIs o f t , LLC .

Peru LNG Overview

• 1st LNG plant in South America

• Commissioned in June, 2010

• 4.4 MTPA Capacity

• Gas is supplied from Repsol YPF and Petrobras

developed fields near the Camisea fields via a 34-

inch (860 mm) supply pipeline runs 408 kilometres

• The LNG plant is operated by Peru LNG which is a

consortium of Hunt Oil Company (50%), SK Energy

(20%), Shell (20%), and Marubeni (10%)

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© Copyr i gh t 2014 O SIs o f t , LLC .

LNG Loading Arm – A Complex & Critical Asset

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© Copyr i gh t 2014 O SIs o f t , LLC .

Business Challenge – Time is

• Loading Arm issue resolution delayed due to:– No Limit switch status in any HMI

– Limited field data in the HMI including limit switches

– Distance between loading arm and instrument maintenance shop

– Different descriptors in DCS and PLC/HMI for same failures

– Very difficult to troubleshoot and resolve issues in a timely manner

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Inability to quickly resolve loading arm issues

resulted in over 700 hrs downtime/yr (~2%)

resulting in increased demerge cost and lost

capacity equating to over $1M/yr

© Copyr i gh t 2014 O SIs o f t , LLC .

Instrument Maintenance

Workshop

Jetty Control Room

Illustration of Challenge

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© Copyr i gh t 2014 O SIs o f t , LLC .

Loading Arm HMI - Limited Infomration

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© Copyr i gh t 2014 O SIs o f t , LLC .

Many descriptions, one Failure

DESCRIPTION IN TRAINING MANUAL

DESCRIPTION CONTROL LOGIC DIADRAM

DESCRIPTION IN DCS Low Oil Press in HPU ACCU

Low oil pressure in HPU Accumulator

Oil Low pressure

DESCRIPTION IN HMI FROM FMC Low Pressure in HPU ACCU on Berth1

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© Copyr i gh t 2014 O SIs o f t , LLC .

We had to be fortune tellers to see what

the instrument alarm refers to…….

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© Copyr i gh t 2014 O SIs o f t , LLC .

Solution – Leverage the PI System to:

Identify Tag number

Identify place in plantFind information

quickly

Solve the problem in less time

Identify location

in plant from

any part of the

networkColabórate with

stakeholders

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© Copyr i gh t 2014 O SIs o f t , LLC .

Predictive

Maintenance

Solution Overview- PI System to the Rescue!

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© Copyr i gh t 2014 O SIs o f t , LLC .

Description from FMC panel

Tag from description

Show Alarm

Show Trend for Analysis

Loading Arms Monitoring Screen

Loading arms status

HPU readings

PMS alarms

Complete information

Manuals from vendor

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© Copyr i gh t 2014 O SIs o f t , LLC .

Window Application per tag

Available pictures

Available

information

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© Copyr i gh t 2014 O SIs o f t , LLC .

Identification

picture

Using Pictures to Help Identification

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© Copyr i gh t 2014 O SIs o f t , LLC .

Limit switches overview for Loading Arms

Limit switches

name

Limit switches

tag and status

Trend of limit

switches

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© Copyr i gh t 2014 O SIs o f t , LLC .

Limit switches locations overvirew

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© Copyr i gh t 2014 O SIs o f t , LLC .

Window application per limit switch

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© Copyr i gh t 2014 O SIs o f t , LLC .

Limit Switches Trends

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© Copyr i gh t 2014 O SIs o f t , LLC .

Predictive

MaintenanceALARM

Send Notification if there are some Failures

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© Copyr i gh t 2014 O SIs o f t , LLC .

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Send Notification if there are some Failures

© Copyr i gh t 2014 O SIs o f t , LLC .

Results and Benefits• Deduced LNG Carrier demurrage

• Reduced LNG Loading arm downtime by >700 hrs/yr

• Increased LNG loading capacity by >2%

• Improved overall plant utilization

• Annual savings are estimated to be >$1MM/yr

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Leveraging the PI System to solve this business

challenge is illustrative of the “art of the possible”

and value now, value over time

© Copyr i gh t 2014 O SIs o f t , LLC .

• Reduced loading arm

downtime by >2% resulting in:

– Decreased LNG carrier

demurrage

– Increase LNG loading

utilization and capacity

– Annual savings >$1MM/yr

Solution Results and Benefits

When Loading LNG, Time is Money

Business Challenge

• Inability to quickly

troubleshoot LNG loading arm

issues due to lack of data and

information in context led to:

– Increased demurrage

– Decreased LNG loading &

plant capacity

• Use the PI System to

integrate, normalize,

analyze, visualize, and

notify enabling a proactive,

efficient approach to LNG

loading arm issues

“Using the PI System to integrate, normalize, analyze,

visualize and notify instrument alarms and related information

on 4 LNG loading arms reduced downtime, demerge costs,

and increased LNG loading capacity by over 2% resulting in

annual savings >$1M/yr”.

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Mr. Walter Florez, Instrument Maintenance Supervisor

Hunt LNG

© Copyr i gh t 2014 O SIs o f t , LLC .

Walter Flores

[email protected]

• Instrument Maintenance Supervisor

• Hunt LNG

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© Copyr i gh t 2014 O SIs o f t , LLC .

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