strategy for extennding gap between og overhaul

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  • 7/31/2019 Strategy for Extennding Gap Between Og Overhaul

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    Strategy to increase the gap

    betweenOH of ST-I units

    By Boiler Maint Dept

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    WATER WALL

    LIMITING FACTORS

    Erosion at S panel. Steam erosion due to

    wall blower

    Fatigue failure at

    bottom end finsbetween panels

    Weld joint

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    Strategy for water wall

    Present practices Tube rep after 20% erosion

    Soot blower operated fromremote.

    There is no interlock for wallblower opn from steamtemp.

    Wall blower is beingoperated 6 times a day.

    Radiography of all welded jts

    Proposed Strategy Tube rep after 10% erosion

    Welding of sacrificial bar Soot blower operation from

    local.

    Incorporation of interlock forWB opn drain temp.

    Optimization and intelligentsoot blowing

    Radiography of all welded jts

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    Radiant Super heater

    LIMITING FACTORS

    Steam erosion due towall blower

    Weld joint

    Mechanical rubbing of

    clamps. Blockage of tube during

    maint

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    Strategy for Radiant Super heater

    Present practices

    Tube rep after 20% erosion

    Soot blower operated fromremote.

    There is no interlock for wallblower opn from steam temp.

    Wall blower is being operated 6times a day.

    No gas cutting plastic capping

    Radiography of all jts

    Proposed Strategy

    Tube rep after 10% erosion

    Soot blower operation fromlocal.

    Incorporation of interlock forWB opn drain temp.

    Optimization and intelligent

    soot blowing Cutting by tube cutting m/c

    and using metal caps.

    Radiography of all jts

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    Platen Super heaters

    LIMITING FACTORS

    Mechanical rubbing dueto binders, connectorsand shop joints.

    Weld joint

    Long term overheating

    Blockage of tube duringmaint

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    Strategy for Platen Super heater

    Present practices Thorough inspection.

    Tube rep after 20% erosion.

    Insitu oxide scalemeasurement everyalternate year

    No gas cutting plastic capping

    Radiography of all jts

    Proposed Strategy Thorough inspection by team.

    Tube rep after 10% erosion Insitu oxide scale measurement

    every alternate year

    Replacement of tubes havinghigher oxide scale.

    Cutting by tube cutting m/c and

    using metal caps. Radiography of all jts

    Reinspection by team whereever maint work is done.

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    Reheaters-II & III

    LIMITING FACTORS

    Mechanical rubbing dueto T spacers.

    Weld joint

    Long term overheating

    Maint induced defect

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    Strategy for Reheater II &III

    Present practice Thorough inspection.

    Tube rep after 20% erosion.

    Insitu oxide scalemeasurement everyalternate year

    No gas cutting plastic capping

    Radiography of all jts

    Proposed Strategy Thorough inspection by team.

    Tube rep after 10% erosion Insitu oxide scale measurement

    every alternate year

    Replacement of tubes havinghigher oxide scale.

    Cutting by tube cutting m/c and

    using metal caps. Radiography of all jts

    Reinspection by team whereever maint work is done.

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    Regulating Stage Reheater

    LIMITING FACTORS

    Long term overheating.

    Random flue gaserosion.

    Constraint forinspection

    Weld joint

    Maint induced defect

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    Strategy for Regulating Stage Reheater

    Present practice Thorough inspection of

    approachable area. Tube rep after 20% erosion. Insitu oxide scale measurement

    every alternate year No gas cutting plastic capping Radiography of all jts 3 way valve optimisation to control

    metal temp.

    Proposed Strategy Thorough inspection of

    approachable by team.

    Tube rep after 10% erosion Insitu oxide scale measurement

    every alternate year Replacement of tubes having

    higher oxide scale. Cutting by tube cutting m/c and

    using metal caps.

    Radiography of all jts Reinspection by team where ever

    maint work is done. Monitoring metal temp and alarm

    provision in UCB.

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    Economiser

    LIMITING FACTORS

    Constraint forinspection

    Flue gas erosion.

    Weld joint

    Maint induced defect

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    Strategy for Economiser

    Present practice Thorough inspection of

    approachable area.

    Modular replacement

    Tube rep after 20% erosion.

    Inspection and repair of

    lower bank coils No gas cutting at vertical.

    plastic capping

    Radiography of all jts

    Proposed Strategy Thorough inspection by team.

    Replacement of upper bankcoils in every 6 years in phasedmanner.

    Inspection and repair of lowerbank coils

    Cutting by tube cutting m/c and

    using metal caps. Radiography of all jts

    Reinspection by team whereever maint work is done.

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    Steam cooled wall & hanger tubes

    LIMITING FACTORS

    Fatigue failure at

    bottom end finsbetween panels atsecond pass and gooseneck side walls.

    Flue gas erosion. Weld joint

    Maint induced defect

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    Strategy for SCW & Hangers

    Present practice Thorough inspection of

    approachable area.

    Tube rep after 20% erosion.

    DPT of end fins betweenpanels

    No gas cutting at vertical.

    plastic capping

    Radiography of all jts

    Proposed Strategy Thorough inspection by team. Tube replacement after 10%

    erosion and shielding. DPT of end fins between panels Ensuring through ness of panel

    drains before unit shut down. Checking for free expansion of

    panels. Cutting by tube using tube cutting

    m/c and using metal caps. Radiography of all jts Reinspection by team where ever

    maint work is done.

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    vents and drains

    LIMITING FACTORS

    Corrosion.

    Stub joint

    Weld joint

    Mechanical rubbing of

    lines at pent houseentry.

    Maint induced defect

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    Strategy for Vents and drains

    Present practice Thorough inspection after

    removal of insulation. DPT of stubs.

    Radiography of all jts

    Proposed Strategy Thorough inspection after removal

    of insulation for corrosion and

    mechanical rubbing. Replacement of all vents and drains

    after one lakh running hours.

    Replacement of corroded tubes. DPT of stubs. Radiography of all jts

    Reinspection by team where evermaint work is done.

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    Pent house

    LIMITING FACTORS

    Mechanical rubbing

    Stub joint.

    Weld joint

    Spray line stubs

    Maint induced defect

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    Strategy for Pent house

    Present practice Thorough inspection by team. DPT of stubs.

    Radiography of all jts

    Proposed Strategy Thorough inspection for corrosion

    and mechanical rubbing of lines.

    DPT of stubs. Inspection adjustment o hangers. Replacement of all vents and drains

    after one lakh running hours. Replacement of corroded tubes. DPT of stubs. Radiography of all jts

    Reinspection by team where evermaint work is done.

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    Coal burners

    LIMITING FACTORS

    Minor erosion of coalnozzle

    Erosion in coal nozzletips is minimum.

    Coal nozzle area oferosion can bestrengthened life canbe extended.

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    Milling system

    LIMITING FACTORS

    More than 50 percentbends are MSfabricated.

    Coal pipe orifice.

    MDVs, MPOs

    RCfeeder chute

    Mill inner cone

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    Strategy for Milling system

    Present practice

    Replacement of eroded coal

    pipe bends (35-40 nos)every year

    Replacement of50 percentMPOs.

    Replacement of30 percentMDVs

    Replacement of30 percentMDVs

    Replacement all orifices

    Proposed Strategy

    Provision electrical operated

    gate at burner inlet to isolatemilling system.

    Replacement of all MSbends with ceramic linedbends

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    Airpreheaters

    LIMITING FACTORS

    CE baskets lattice andtheir support.

    APH support bearing

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    Strategy for Airpreheaters

    Present practice

    Replacement of erodedlattice.

    Replacement of erodedlattice supports.

    Wear debris analysis ofAPH bearing and gearbox lub oil once in 3months

    Proposed Strategy

    Replacement of all lattice

    Replacement of all latticesupports

    Withdrawal and inspection ofAPH support bearing duringcapital OH.

    Wear debris analysis of APHbearing and gear box lub oilonce in 3 months

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    Conclusion

    Following action can increase OH Gap Replacing eroded tubes below 10%.

    Extensive DPT as identified locations. Replacement of ECO upper bank coils once in six

    years. Optimization and careful operation of wall blowers. Insitu oxide scale measurement once in two years and

    replacing higher oxide scale tubes. Installation of gate for isolating milling system near

    burner.

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    Conclusion

    Educating the maintenance contract personnel aboutpossible maintenance induced defect.

    Radiography of all welded joints.

    Replacing vents and drains periodically.

    Heating and cooling boiler in normal way.

    Wear debris analysis of APH lub oil. Withdrawal of APH bearing for inspection during

    capital OH.

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