what’s this hwa design thing all about???
DESCRIPTION
What’s This HWA Design Thing All About???. Design Capacity HWA Info from one POTW CITY OF GREENSBORO North Buffalo POTW. NORTH BUFFALO POTW. Design Flow: 16 MGD Current Flow = ~10.0 MGD Primary Treatment Secondary Treatment Trickling Filters Activated Sludge with Nitrification - PowerPoint PPT PresentationTRANSCRIPT
What’s This HWA Design Thing All About???
Design Capacity HWA Info from one POTWCITY OF GREENSBORO North Buffalo POTW
NORTH BUFFALO POTW Design Flow: 16 MGD
Current Flow = ~10.0 MGD Primary Treatment Secondary Treatment
Trickling Filters Activated Sludge with Nitrification
Tertiary Treatment Phosphorus removal
Chemical Addition/Precipitation Effluent Sand Filters
NB CURRENT MAHL CALCULATIONCBOD [Actual Removal/Actual Flow]
NPDES Permit Limit: 8.0 mg/l (summer)Removal Rate: 98.8% (270 data points/MRE)Actual Flow: 14.2 MGD** 8.0 mg/l = 8.0 = 666 mg/l max. allowable1.0-.988 .012 influent conc.
666 * 8.34 * 14.2 MGD = 78,952 pounds
**DWQ required use of actual flow..flow has dropped since then. These are the approved headworks calculations from December 2003
“DESIGN CRITERIA”NORTH BUFFALO POTW
From Hazen and Sawyer Engineers Original Design (~1980 Upgrade)
BOD = 196 mg/l TSS = 245 mg/l Total Phosphorus = 6.0 mg/l NH3-N = 18.5 mg/l
NB “DESIGN CRITERIA” per DWQMAHL CALCULATION: CBOD
Engineering Design BOD = 196 mg/l Used BOD as CBOD
Engineering Design Flow = 16 MGD 196 * 8.34 * 16.0 = 26,154 pounds MAHL Current Domestic BOD Loading: 27,615 lbs 20 of last 24 monthly average influent
concentrations exceeded 196 mg/l while resulting in average effluent CBOD of <2 mg/l
CAN YOU SPELL OVERALLOCATED?????
NB CURRENT HWA CALCULATIONTSS [Actual Removal/Actual Flow]
NPDES Permit Limit: 30.0 mg/l Removal Rate: 97.8% (271 data points/MRE)Actual Flow: 14.2 MGD
30.0 mg/l = 30.0 = 1363 mg/l max. allow.1.0 -.978 .022 influent conc.
1363 * 8.34 * 14.2 MGD = 161,492 pounds**DWQ required use of actual flow..flow has dropped since then.These are the approved headworks calculations from December 2003
NB “DESIGN CRITERIA”CALCULATIONS: TSS
Engineering Design TSS = 245 mg/l Engineering Design Flow = 16 MGD
245 * 8.34 * 16.0 = 32,693 pounds
[Current Domestic TSS Loading: 22,289] Not overallocated now, but flow is only ~10.0
MGD Domestic alone will use up the rest of the
allocation
IMPLICATIONS Underestimating POTW Conventional
Pollutant Capacities and Capabilities Potential Over-Allocation With Just Domestic
Loading! Loss of Potential New Industrial Users Potential Moratorium
“Domestic concentration” is rising due to newer plumbing fixtures
BOD Limits for All SIUs North Carolina Local Limits Policy
North BuffaloCurrent Loading Situation: DISMAL
Actual Influent CBOD Loading = 19,718 lbs 213 mg/l * 8.34 * 11.1 MGD [24 mo. avg]
DWQ Design Loading = 26,154 lbs 6436 lbs CBOD left…[“domestic” on paper is >MAHL] BOD Limits for Everyone!!!! [75.4% “loaded”]
Actual Influent TSS Loading = 32,401 lbs 350 * 8.34 * 11.1 MGD [24 mo. avg]
DWQ Design Loading = 32,693 lbs Only 292 Pounds of TSS Left…but over 4 MGD of
hydraulic capacity left… TSS Limits for Everyone!!!! [~100% “loaded”]
North Buffalo SUMMARY
CALCULATIONMETHOD
Influent mg/l
MAHL pounds
BOD
Pass-Thru Cal/Actual Flow 666 78,952
O&M “Design” (Proposed DWQ) 196 26,154
TSS
Pass-Thru Cal/Actual Flow 1363 161,493
O&M “Design” (Proposed DWQ) 245 32,693