3d tube bender

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Design Process 3D Tube Bender Sponsor: RH systems Nicholas Loftis, Marisa Downey, Corbin Womack, Samantha Burkhart Abstract Our objective was to design a 3-Dimensional automated tube bending apparatus capable of bending indicated wall thicknesses into helixes without crimping or crushing. The focal goal was to bend 1/4” copper tubing at a 9/16” bend radius. We collaborated with an Electrical Engineering team to ensure the future implementation of motor control. The design consists of two components: the driving mechanism and the bending instrument. Introduction Applications of bended tubing are heating, ventilation, and air conditioning (HVAC), and the automotive industry. Presently, tube bending is performed manually. For large tubing, automation has become a satisfactory approach, however small diameter tubing still requires hand bending. RH Systems has recruited Texas State University to design and prototype a 3D automated tube bending machine. We will be working in collaboration with an Electrical Engineering team providing them with necessary calculations along with ensuring the design is compatible with implementing motorized control systems. This project will take place over the next 2-3 semesters, each with different scopes. Our primary goal Objectives Goal: Bend copper tubing with a wall thickness between 0.020” to 0.065” into a helix without crimping or crushing tube Material: Copper - Nom. ¼” Type L 0.030Guidelines: Eliminate repeatability issues with hand bending Save time Increase complexity of bends Stay within tolerances Methods This work has been completed with funding from Texas State University and the Ingram School of Engineering. The authors would like to thank Dr. Austin Talley, Dustin Hardy, Jason Wagner, Ruben Villarreal, Charles Fry, Joseph Kiser, and Texas State University for providing funding, materials, and access to tools, infrastructure, and laboratories. Conclusion After testing the finished manual tube bending machine, it could be concluded that the manual bending device is successful in terms of bending the copper tubing. We still have a few challenges to overcome in our design. A primary concern is material removal. Since this is a manual apparatus, we must return the system back to its original parameters in order to extract the bent coil. Another challenge we faced is the length limitation. Currently, we can only bend 10 inches of material. Our next goal is to amend the coil removal issue and expand the machine’s drive mechanism in order to bend a larger length of material. Acknowledgements Customer requirements had to be assessed and then applied to the House of Quality. The House of Quality aided in identifying and prioritizing the customer needs for the design. Each customer requirement was given an importance weighting to compare in the concept selection matrix. After participating in concept generation activities such as brainstorming and 6-3-5 methods, five methods were left to be compared and evaluated. After assessing our methods, we chose to go with the Capillary Bending method. Capillary Bending applies similar techniques to roll bending with the addition of the moving dies to implement the 3 dimensional aspect. Results Initially, our driving mechanism along with our bending mechanism were two components that were crucial to the design. A CAD drawing of the prototyped driving system is shown below. By utilizing a drill chuck as a workpiece holder, all-thread, and a mill turning wheel, a driving device could be constructed. As for the bending mechanism, a steel lazy-susan combined with 3D printed dies was assembled. The prototype Concept Selection Matrix Die 1: Restrict pipe from bending in the positive X-direction Die 2: Stationary die which determines the inner bend radius Die 3: Outer die which bends tubing around the stationary die Die 4: Moves in +/- Z-direction to change pitch of the spiral Ultimately, when the copper tubing is bent up to 80 degrees (from the initial starting point) the tube bending device can produce a quality bend of around a 1.5 inch bend radius. Results of a 70, 80, and 90 degree bend are shown below, respectively from top to bottom. for this semester is to design the necessary dies, work piece holder, and technique for the operations to take place.

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Page 1: 3D Tube Bender

Design Process

3D Tube BenderSponsor: RH systems

Nicholas Loftis, Marisa Downey, Corbin Womack, Samantha Burkhart

AbstractOur objective was to design a 3-Dimensional automatedtube bending apparatus capable of bending indicated wallthicknesses into helixes without crimping or crushing.The focal goal was to bend 1/4” copper tubing at a 9/16”bend radius. We collaborated with an ElectricalEngineering team to ensure the future implementation ofmotor control. The design consists of two components:the driving mechanism and the bending instrument.

IntroductionApplications of bended tubing are heating, ventilation,and air conditioning (HVAC), and the automotiveindustry. Presently, tube bending is performed manually.For large tubing, automation has become a satisfactoryapproach, however small diameter tubing still requireshand bending. RH Systems has recruited Texas StateUniversity to design and prototype a 3D automated tubebending machine. We will be working in collaborationwith an Electrical Engineering team providing them withnecessary calculations along with ensuring the design iscompatible with implementing motorized controlsystems. This project will take place over the next 2-3semesters, each with different scopes. Our primary goal

ObjectivesGoal: Bend copper tubing with a wall thickness between 0.020”to 0.065” into a helix without crimping or crushing tubeMaterial: Copper - Nom. ¼” Type L 0.030”Guidelines:• Eliminate repeatability issues

with hand bending• Save time• Increase complexity of bends• Stay within tolerances

Methods

This work has been completed with funding from TexasState University and the Ingram School of Engineering.The authors would like to thank Dr. Austin Talley,Dustin Hardy, Jason Wagner, Ruben Villarreal, CharlesFry, Joseph Kiser, and Texas State University forproviding funding, materials, and access to tools,infrastructure, and laboratories.

ConclusionAfter testing the finished manual tube bending machine, itcould be concluded that the manual bending device issuccessful in terms of bending the copper tubing. We stillhave a few challenges to overcome in our design. Aprimary concern is material removal. Since this is amanual apparatus, we must return the system back to itsoriginal parameters in order to extract the bent coil.Another challenge we faced is the length limitation.Currently, we can only bend 10 inches of material. Ournext goal is to amend the coil removal issue and expandthe machine’s drive mechanism in order to bend a largerlength of material.

Acknowledgements

Customer requirements had to be assessed and then applied to the House of Quality. The House of Quality aided in identifyingand prioritizing the customer needs for the design. Each customer requirement was given an importance weighting to comparein the concept selection matrix. After participating in concept generation activities such as brainstorming and 6-3-5 methods,five methods were left to be compared and evaluated. After assessing our methods, we chose to go with the Capillary Bendingmethod. Capillary Bending applies similar techniques to roll bending with the addition of the moving dies to implement the 3dimensional aspect.

Results

Initially, our driving mechanism along with our bending mechanism were two components that were crucial to the design. A CAD drawing of the prototyped driving system is shown below. By utilizing a drill chuck as a workpiece holder, all-thread, and a mill turning wheel, a driving device could be constructed. As for the bending mechanism, a steel lazy-susan combined with 3D printed dies was assembled. The prototype

Concept Selection Matrix

• Die 1: Restrict pipe from bending in the positive X-direction• Die 2: Stationary die which determines the inner bend radius• Die 3: Outer die which bends tubing around the stationary die• Die 4: Moves in +/- Z-direction to change pitch of the spiral

Ultimately, when the copper tubing is bent up to 80degrees (from the initial starting point) the tube bendingdevice can produce a quality bend of around a 1.5 inchbend radius. Results of a 70, 80, and 90 degree bend areshown below, respectivelyfrom top to bottom.

for this semester is todesign the necessarydies, work piece holder,and technique for theoperations to take place.