challenges in coke dry quenching...

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11/12/2018 1 Maintenance challenges in Coke Dry Quenching plant(CDQ) COKE OVEN#3 Capacity- 1.5MTPA CDQ1 CDQ2 BATTERY#1 (56 OVENS) BATTERY#2 (56 OVENS) BATTERY#3 (56 OVENS) BATTERY#4 (56 OVENS) CDQ3 CDQ4 2 COKE OVEN#4 Capacity- 1.9MTPA BATTERY#5 (72 OVENS) BATTERY#6 (72 OVENS) BATTERY#7 (72 OVENS) BATTERY#8 (72 OVENS)

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Page 1: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

11/12/2018

1

Maintenance challenges in Coke Dry Quenching plant(CDQ)

COKE OVEN#3Capacity- 1.5MTPA

CDQ1 CDQ2

BATTERY#1

(56 OVENS)

BATTERY#2

(56 OVENS)

BATTERY#3

(56 OVENS)

BATTERY#4

(56 OVENS)

CDQ3 CDQ4

2

COKE OVEN#4Capacity- 1.9MTPA

BATTERY#5

(72 OVENS)

BATTERY#6

(72 OVENS)

BATTERY#7

(72 OVENS)

BATTERY#8

(72 OVENS)

Page 2: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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2

COKE DRY QUENCHING

3

MAIN SPECIFICATIONS OF CDQ PLANTNo. Description CDQ 1 & 2 CDQ 3 & 4

1 Maximum coke throughput (charging amount to the chamber) 120 T/H

2 Rated coke throughput (charging amount to chamber) 85 T/H 112 T/H

3 Coke solution loss Approx. 1%

4 Red hot coke temperature 1000±500C4 Red hot coke temperature 1000±50 C

5 Cooled coke temperature 2000C or less 

6 Pre‐ chamber volume 1.5 hours or more

7 Cycle time of charging crane 10.5 min/cycle 8.2 min/cycle

8 Boiler max. steam production capacity Max. 72 T/H

9 Steam production at rated coke throughput without BFG Max. 49.3 T/H   (85 T/H* 0.58)

Max. 65T/H    (112 T/H*0.58)

10 Steam production ratio without BFG 580 kg/T of coke

11 Steam production ratio with BFG 750 kg/T of coke

4

12 Steam pressure 9.5 ± 0.2 MPa

13 Steam temperature 540 ± 50C

14 Circulation gas volume Max. 180,000 Nm3/H

15 Circulation gas temperature at inlet of boiler 9800C

16 Circulation gas temperature at inlet of cooling chamber 1300C

17 Operation hours per day 24 hours/day

18 Operation day per year 345 days/year

19 2 years once 22 days

Page 3: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

11/12/2018

3

CRANE

CHAMBER

BOILER

PRIMARY DUST CATCHER

5

5

ROTARY SEAL VALVE

CONVEYOR GAS CIRCULATION BLOWER

SECONDARY DUST CATCHER

CASESTUDIES  COVERED

1. Increase in life of CDQ Bucket liners.

2. Modifications in Discharging facility to reduce maintenance.

6

Page 4: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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INCREASE IN LIFE OF CDQ BUCKET LINER PLATE’S.

7

SITUATION BEFORE IMPLEMENTATION

• Initially the liners are of cast iron with single fastener.

• Due to which any fluctuations in battery temperatures  coke sticking y y p gproblems  leads to damage of liners(CDQ Bucket )

• During breakdowns of charging crane/CDQ loco the hot coke will be in bucket for longer time this leads to damage of liners

LINER PLATE DESIGN & MOC

8

• Immediately stop pushings in that particular bucket and cooling starts followed by wet quenching.

• Shutdown for liner plate changing after cooling.

LINER PLATE MISSING IN CDQ BUCKET

Page 5: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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SITUATION BEFORE IMPLEMENTATION

• As the discharge of coke is continuous the missing liner is found at RSV and discharge is stopped.

• As soon as discharge stops the boiler inlet temperature drops results in low steam generation.

Discharging facility Rotary Seal Valve(RSV) Jam 

9

CHANGES MADE IN SYSTEM

10

Page 6: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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Liner Plate Modification

11

Liner plate MOC was changed from (cast iron to HN grade). Further Up gradation 

142.4

120

140

160

Average Liner life

of liner MOC (HN grade to HK grade). At some Critical locations liner plate rib design improved and modifications in fastening methods further added to the life of bucket liners.

44 45

68.5

0

20

40

60

80

100

FY1415 FY1516 FY1617 FY1718

CI SS304 SS 310 HN SS310HK

98 66

99.24

99

99.5

Equpt Availability

12

96.7

97.44

98.66

95

95.5

96

96.5

97

97.5

98

98.5

99

14‐15 15‐16 16‐17 17‐18

Availability %

Time period

Page 7: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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ADVANTAGES

Increased the Availability of Loco car.

Reduced production delay by conveying hot coke to the chamber Reduced production delay by conveying hot coke to the chamber

Reduced bucket cooling time for liner plate changing during shutdown

Enhanced steam generation in Boiler

13

Modifications in Discharging facility to reduce Maintenance.

14

Page 8: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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MODIFICATIONS IN DISCHARGING FACILITY TO REDUCE MAINTENANCE

Vibrofeeder drain line     

Design modification in suction line  

Slide gate hopper           

15

Vibrofeeder drain line

In vibrofeeder, dust collected & drained in to de‐d ti i i h

Problem’s faced

dusting mains as pic shown . It’s a continuous process. Over a period of            ttime, drain line  get choked due to angle of r  rrepose for dust flow. 

Choked lines hamper the performance of vibrofeeder.indirectly restrict the coke discharge with heating upof coils.

CO gas beyond safe limit due to this improper

16

CO gas beyond safe limit due to this improperinspection of conveyors.

Stoppage of coke discharge leads to production loss.

Page 9: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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Modification‐

Increase in the Angle of connecting pipe .

Vibrofeeder Drain Line

g g p p

Smooth flow of dust in Pipe reduce the

damages.

The line has been connected directly to de‐

dusting header.

17

Result‐

It has enhanced the performance of It has enhanced the performance of

vibrofeeder. Low maintenance required.

Coil temp maintained normal.

Increase of suction pressure as it is directly

d d d i h d

18

connected to de‐dusting header.

Conveyor stoppage frequency reduced &

there is no pipe damage here after.

Page 10: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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Accumulation of coke fines in hopper.

Slide Gate Hopper

Problems ‐

pp

Due to which slide gate getting jam 

frequently.

During stoppage of discharge slide gate 

cannot be closed for maintenance so CO

19

cannot be closed for maintenance, so CO 

gas leakage at discharging area.

Modification‐

Angle of drain line and pipe size has g p pbeen changed.

Provision of man hole for  periodic cleaning of hopper.

20

Page 11: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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Result‐

Reduced the frequency of slide gate malfunctioning(full open/close).

Slide Gate Hopper

q y g g( p / )

No CO gas was found at discharge area ,hence easy maintenance of discharging equipment's can be done.  

21

Refractory Maintenance Challenges

LIFE ENHANCEMENT OF CDQ SLOPING FLUE PILLAR BRICKS

Page 12: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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View of CDQ Pillar, Flat Arch & Ring Duct

Ring Duct

Flat ArchFlat Arch

Flue Post Pillars

23

JSW CDQ Chamber General Arrangement Drawing

Flue postFlue hole

Pre-chamber

Cone

Dust catcherPassage channel

Ring Duct

Cooling chamber

24

Page 13: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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• In CDQ refractory lining is there in Chamber, PDC and Boiler.

Details of CDQ Refractory

• Chamber is divided into three zones first zone, second zone and third zone.

• Total there are 36 nos of pillars in the second zone.

• In one CDQ 1300 Tons of Refractory is there and 500 shapes is used .

• The pillar bricks are getting cracked and falling down after doing the refractory

Refractory Problems faced during Operation

maintenance job .

• The cooling chamber refractory bricks are getting eroded .

• The Jack Arch portion of the bricks are getting eroded.

• The life of the refractory pillar is less than one year.

• Erosion in the top layer of the third zone bricks.

Page 14: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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14

Seal Pot

CDQ sloping flue pillar Refractory life improvement.

Target Wall

Sloping Flue Pillar

2‐way ChuteCooling Chamber

Failure Analysis Chart.

91

98 100

80

90

100

50

45

75

30

40

50

60

70

20

30

40

Cumm %

Occurance

25

16

94 1

0

10

20

0

10

CDQ sloping pillar Cooling Zone PDC Joint Seal port 2‐Way chute

Occurance Cumm. %

Page 15: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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Possible ideas Generated:

1. Repair of Complete pillar during yearly maintenance.

2. Filling of Cracks by Refractory mortar.

Failure Analysis Chart.

3. Upgrading the Quality of Refractory bricks.

4. Reducing CDQ process temperature fluctuation.

5. Strengthening of Pillar lining by repairing the first layer

completely.

6. Strengthening of pillar lining by repairing 2 layers

C Type Cracks Dislodging of Bricks

namely 9,3 series bricks.

7. Coating the erosion area to avoid unwanted gaps.

8. Increase the width of pillar bricks.

9. Providing a sliding expansion joint between 9,3 series

bricks

Erosion of bricks (Cooling Zone)

Total Load of Ring Duct is distributed on -

JSW CDQ Design Aspects

Slope Provided in the Flat Arch Skew Brick

On the Pillar BricksOn the Pillar Bricks

30

Page 16: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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PDCA-1

Validation of Ideas: -

BeforeCheck

Plan: - 1. Strengthening of pillar lining for having

better Mechanical & thermal stability.

2. Gunning of cooling zone area .

Do: - 1.Dismantling & relining of Sloping flue pillar

refractory to first layer

2. Gunning of cooling zone area with 60 % Castable.

After

Results (after 1-year operation): -

1 C type cracks minimized

PDCA#1 Conclusion: -

1. C type cracks minimized.

2. No improvement in dislodging of Refractory bricks.

3. Relined bricks found at the discharge chute within 3-4 months of installation.

4. Due to gunning in cooling zone area further brick damage is controlled.

Inference of PDCA-1: -

Understood that dislodging of bricks is due to 2 factors namely improper locking & inclination of 76

degree provided in the pillar design. so planned for dismantling & relining of sloping flue pillar up to 2nd

layer.

Page 17: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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Plan: - Strengthening of pillar lining by repair up to 2 layers namely (9,3 series bricks) with upgradation in quality of bricks. D 1 U d ti i lit f R f t b i k f b tt th l & h i l

PDCA#2 : -

Do: - 1. Upgradation in quality of Refractory bricks for better thermal & mechanical stability. 2. Irrespective of damages of sloping flue pillars it is being decided to dismantle & Reline of Pillar Refractory brick up to 2 layers.

Actual Damaged Repaired

Before

Results (after 2-year operation): -

Check

PDCA#2 Conclusion: -

1. Dislodging of Bricks was minimized.2. No cracks develop during the operation.3. Minor erosion in pillar bricks.4. No bricks were found at discharge end .

Inference:

After

Inference: -1. Pillar lining service life improved to 2

years .

Page 18: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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Electrical Maintenance Challenges

ESTABLISHING WIRELESS COMMUNICATION BETWEEN LOCO BUCKET ‐ LOCO PLC ‐ CDQ PLC

VIJAYANAGAR WORKS

The loco bucket will receive the hot coke

from ovensfrom ovens

This bucket is aligned properly in auto

positioning system

Then the hot coke is charged in CDQ

chamber through crane

36

chamber through crane

There is a sequence of operation to chargethe hot coke.

Page 19: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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During this sequence of operation several 

signals get exchange between locomotive PLC 

and CDQ PLC CDQ PLC

LOCO PLC

and CDQ PLC. 

To achieve this signal exchange we have set of 

magnetic sensors  and switches,

Here sensors will play a major role .

Two sensors for bucket centring

CDQ PLC

Two sensors for bucket centring

One for APS* order 

One for APS* Lock feedback

One for CDQ order

*APS: Auto positioning system37

This sensors and switches were getting 

damaged due to harsh working BUCKET 1BUCKET 2

CDQ LOCO

condition 

When the locomotive moving along the 

battery area sensors are getting 

damaged due to the impact of the coke CDQ

CABLE & SENSORSDAMAGE

Cables are getting damaged due to hot 

coke near wharf.

38

CDQ

SENSORS STAND

Page 20: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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MODIFICATION IN THE SYSTEMMODIFICATION IN THE SYSTEM

CDQ LOCO

CABLE & SENSORSELEMINATED

BLUE TOOTH MUXSET

BUCKET 1BUCKET 2

CDQ LOCO

39

CDQCDQ

SENSORS STAND

During the initial stage we tried to protect the

sensors by putting scraper on both side of sensor

stand

In the next step, in order to further reduce the

problem we replaced the sensors with wireless

Bluetooth muxset .

For the wireless muxset power supply , we used heat

resistance cable

40

Page 21: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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Wireless interface Wireless standard Bluetooth 1.2

Frequency range 2.402 GHz ... 2.48 GHz (ISM bandwidth) 

T i i 16 dB (40 W t ll d t ti ll ) Transmission power 16 dBm (40 mW, controlled automatically) 

Antenna connection method MCX (female) 

Power supply for module 24 V DC

Connection technology 1‐wire

Number of inputs 16 Digital inputs

Number of outputs 16 Digital outputs

41

Number of outputs 16 Digital outputs

Analog inputs 2 Voltage input signal 0 V ... 10 V and

Current input signal 0 mA ... 20 mA

Analog outputs 2 Voltage input signal 0 V ... 10 V and 

Current input signal 0 mA ... 20 mA

Operating Range: Up to 100 m With antenna.

ADVANTAGESADVANTAGES

Increased the availability of Loco car.

Reduced production delay by conveying hot coke to the chamber

Reduced usage of sensors ,hence frequent damage of sensors isreduced .

Reduced usage of cable ,hence Frequent damage of cables is reduced.

Reduced the damage of loco wagon liner plates.

Enhanced steam generation in Boiler Enhanced steam generation in Boiler

42

Page 22: challenges in Coke Dry Quenching plant(CDQ)oc4.tksranchi.in/49thOc4/Presentations/Session-3/JSW.pdf · JSW CDQ Chamber General Arrangement Drawing Flue post Flue hole Pre-chamber

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